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ABOUT INDO GULF FERTILIZERS
• Indo Gulf Fertilizers is one of the blue chip companies of ADITYA BIRLA GROUP,
which was commissioned in October 1988.
• The urea complex located at Jagdishpur industrial area of District Sultanpur, situated at
about 80 km from Lucknow on the National Highway No.56.
The company is engaged in the business of manufacturing nitrogenous fertilizers under the
brand name of BIRLA SHAKTIMAN.
Fertilizer complex has
Ammonia plant based on Haldor Topsoe Technology.
Urea plant based on Snamprogetti Technology.
Service Boilers, Gas turbine, DM plant, Effluent treatment plant etc.
The feed stock is natural gas which is supplied by M/s. GAIL through HBJ
pipeline.
Company is committed to continual improvement in its environmental & production
performance.
VISION - 2014
SEEDS PESTICIDES
INDIA
IGFL
Indo-Gulf Located on Cross Country HBJ gas pipe line at Jagdishpur, Uttar
Pradesh, North India
PROFILE
Employs about 850 people and offers indirect employment to over 4000 people.
Direct contact with over 0.3 million customers per year through service programs.
Maintenance Q&EC
Carbon Dioxide
Natural
Steam
Power
Steam
Power
Power
Gas
Water
Power Plant
& Utilities 50 Kg Urea bags
Naphtha
General Engg.
Fire & Safety
Process Engg.
13
BRIEF PROCESS
DESCRIPTION
14
AMMONIA PLANT
INSTALLED CAPACITY 1350 MTPD
REASSESED CAPACITY 1520 MTPD (April 2000)
PROCESS LICENSOR
AMMONIA HTAS, DENMARK
PGR PLANT BHPV, INDIA
CDR PLANT KTI, USA
PROCESS TECHNOLOGY NG – STEAM REFORMING
RAW MATERIAL FEED – NATURAL GAS
FUEL – NATURAL GAS, NAPHTHA
FEED/FUEL Ratio:70/30
Ammonia process is a highly complex in nature due to :
Handling of highly toxic and explosive gases
Temperatures and pressures in the process vary from extra high (1050°C/ 200 Kg/Cm 2) to
absolute low (-180°C/Vacuum).
Use of catalysts (Zinc, Nickel, Chromium, Copper and Iron)
Three high speed, high pressure turbo compressors being operated (Process Air Compressor:
13 MW, Synthesis Gas Compressor: 24 MW, and Ammonia Compressor: 3.0 MW).
Tail gas from PGR Plant is processed in AGR Plant to recover Argon.
15
AMMONIA PROCESS
AIR H.P.
STEAM
COMPRESSOR STEAM
CO 2 TO UREA PLANT
REFRIG.
COMPRESSOR
TO UREA PLANT
TO AMMONIA PLANT
16
UREA PLANT
NH3 (LIQUID)
HOT
AIR
U 99.7 %
OVERHEAD CONDENSOR CONDENSOR
CONDENSOR
TREATED WATER
TO D.M. PLANT
TO
BAGGING
18
UREA PLANT - PRODUCT QUALITY
SL. PARAMETERS SPECIFICATIONS ACTUALS KEY CONTROLS
NO.
UREA PRODUCT QUALITY
2 HRSG
UNITS 01 2 DIESEL GENERATOR
CAPACITY 5000 MT
7000 M3
COMPLETELY
ELIMINATED
BY ZEOLITE
SOFTENING
EFFLUENT UREA
KATHAURA NALLA TREATMENT COOLING COOLING
PLANT TOWER WATER
EFFLUENT FROM
AT PRESENT AMMONIA, UREA
EFFLUENT IS BEING & PPU
UTILIZED FOR
HORTICULTURE
PURPOSE
23
BAGGING PLANT
Buffer
Screening
hoppers
section
(7 nos.)
SILO
CAPACITY
45000 MT Reclaimed
Weighing machines
urea
(14 nos.)
transfer
conveyor
Filling & stitching
(7 No. of streams)
Silo Diversion (Hrs)
Target Actual
Despatch Bagged urea Despatch
05-06 94 46 transfer
by Road by Rail
06-07 75 Conveyors &
20% 80% 25
loaders
ARGON PLANT
27
PROCESS ENGINEERING
MANAGEMENT INFORMATION SYSTEM
DOF/FICC
GAIL
GAS DETAILS
BENCHMARKING
THINK TANK
TECHNICAL SUPPORT
TROUBLE SHOOTING
ASSISSTANCE IN CORE TEAM
CATALYST EVALUATION
MACHINE PERFORMANCE EVALUATION
PLANT PERFORMANCE MONITORING
TO MONITOR THE OVERALL PLANT PERFORMANCE FOR
ACHIEVING THE IDENTIFIED TARGETS IN RELATION TO
PRODUCTION, RAW MATERIALS, UTILITIES & ENERGY
CONSUMPTION. 29
GENERAL ENGINEERING
Key Functions
Cost estimation of new schemes, provided by Process
Engineering Department.
Preparation of specifications, detail engineering of piping,
equipment & isometrics.
Project management
Documentation of drawings and specifications of complete
plant since inception and updating time to time by
incorporating modifications through electronic media.
Rendering services to maintenance and operation
departments.
Focus Area
Optimization of project cost
Adherence to Project Schedule 30
MECHANICAL MAINTENANCE
Maintenance Practices
Preventive or Time Based Maintenance
• Manufacturer Recommendation, Plant Experience & Insurance
Requirements
Condition Based Maintenance
• Daily check List, On line and off line Condition monitoring &
equipment performance analysis.
Identification & elimination of weak areas in plant with proactive
approach, using tools like TPM, COPQ, RCM & Six Sigma
Learning from incidents at similar plants.
Turn Around Maintenance Management
Condition Monitoring Practices
• On-line vibration & temperature monitoring
• Off line vibration & temperature monitoring for all machines
• Off line monitoring as per weekly, fortnightly, monthly schedules
decided based on criticality, severity of operation etc
31
MECHANICAL MAINTENANCE
Maintenance Practices
Why-Why Analysis
• An analytical tool to identify root cause of abnormality by
questioning “Why” for probable causes to reach logical conclusion.
• Analysis of abnormalities/breakdowns having cross functional
implications, by cross functional team.
• Analysis of near miss incidents like abnormalities observed during
routine maintenance by grass root level person, in their pocket book
(KARAN VISHLASHEN PUSTIKA).
• Horizontal replication and training based on why-why analysis
recommendations, good to find, one point lessons etc.
Cost Control
• Procurement from OEM sub-vendors, standardization & development
of alternate vendors for spares & consumables.
• Utilization of in-house expertise and developing local contractors.
• Recycling of lubricating oil wherever possible 32
MECHANICAL MAINTENANCE
Workshop Facilities
IGFL workshop fully equipped to support plant maintenance, consists
of Machine, Fabrication, Auto and A/C shops with facilities for
• Precision machining, boring, drilling, milling
• Welding, Plasma Cutting, Stress Relieving
• Rolling
• Automobile Shop with material handling equipments
Can fabricate small & medium size heat exchangers, pressure vessels,
spares
Can handle erection up to 75 Tons at small heights and 3 Tons up to
50 Meters
With fabrication of heat exchangers, pressure vessels, we could reduce
project implementation time and equipments fabricated in Workshop
are giving trouble free service.
34
CONDITION MONITORING & N.D.T.
Key Functions
Condition Monitoring & Non Destructive Testing of plant
equipment to improve reliability by prediction of failure which
results in maximisation of on-stream days in order to achieve
overall objective of the company.
Spark Testing of
Thickness Coated Lines &
Measurement Vessels
Temperature
monitoring of
Steam Trap
Rotary equipment
Survey
Insulation
Ultrasonic testing at
Survey
Elevated temperature
Oil Contamination Boroscopic
Analysis Inspection
36
INSTRUMENTATION
ROLE OF DEPARTMENT:
• TO MAINTAIN ONLINE INSTRUMENTATION PROVIDED FOR
PARAMETERS.
SUPPLY TO INSTRUMENTS.
CALIBRATION FACILITIES
• HIGH ACCURACY MASTER INSTRUMENTS AVAILABLE
FOR VERIFYING CALIBRATION OF INSTRUMENTS
• CALIBRATION OF INSTRUMENTS TRACABLE
TO NATIONAL STANDARD. 38
ELECTRICAL DEPARTMENT
To AGR
Power from
132/11kv UPSEB grid 132/11kv
16 MVA 16 MVA
11 KV
11 KV
3.3 KV
LOAD
• Own generation : 11KV 19 MW gas turbine generators (2 Nos.) – One running & One
kept as standby.
• Purchased power : From UPSEB grid at 132KV (4000kva contract demand) as standby
power (with automatic change-over facility within 4 sec., in case of own
generation failure)
• Emergency supply : From own 2MW 11KV Emergency Diesel Generator (to meet the
power demand for safe shut-down of plant in case of total power failure) 39
ELECTRICAL DEPARTMENT
CUSTOMER
QUALITY ENVIRONMENT
SUPPORT
ASSURANCE CONTROL
SERVICES
42
Q&EC - QUALITY ASSURANCE ACTIVITIES
45
AWARDS & RECOGNITIONS
AWARDS YEAR
AWARDS YEAR
48
KEY DRIVERS
50
UREA PRODUCTION – PAST PERFORMANCE
1200
1020 1042 GOVERNMENT RESTRICTION
ON PRODUCTION
1000 879 865 862
850
800
Lacs MT
600
200
0
98-99 99-00 00-01 01-02 02-03 03-04
AFTER RESTRICTIONS IN OCT’ 2000, ACTIVITIES WERE MORE FOCUSSED
ON ENERGY CONSERVATION. ENERGY CONSUMPTION CONTRIBUTES TO
75% OF TOTAL COST OF PRODUCTION. 51
UREA PRODUCTION PERFORMANCE
AFTER GOI ALLOWED HIGHER PRODUCTION
1200
985 996 996
1000
800
600
356 *
349
**
400 335
200
0
'04-05 '05-06 06-07 P&B
NG/ Naphtha Ratio
Production ( '000 MT ) OSD
04-05 : 78 / 22
05-06 : 96 / 04
Longest Uninterrupted Operation of Ammonia plant for 615 days
* 05-06 - 8 days S/D from 25th Nov to 2nd Dec 2005 for Revamp Phase I
** 06-07 – 8 days Shut down taken in May ’06 for Urea Strippers replacement. 25
days S/D planned for Revamp Ph II in March/April 2007. 52
UREA ENERGY - PAST PERFORMANCE
6.20 UREA ENERGY INCREASED DUE
TO LOW LOAD OPERATION
5.95
6.00 5.89
REDUCTION
OF 0.26 REDUCTION
5.80 5.69 OF 0.14
M KCal/MT
REDUCTION
5.55
5.60 OF 0.11
5.36
5.40
5.20
5.00
99-00 00-01 01-02 02-03 03-04
5.5
5.42
MKCAL/MT
5.4
5.37
5.4 5.33
5.3
'04-05 '05-06 'P&B 06-07
Savings 0.458
20 19.67
0.45
18.87
18
Investment
16.83 0.4
16
14.87
0.35
14
0.333
0.3
11.89
12
9.8 0.25
10
0.23
8 0.2
2001-02 2002-03 2003-04
Saving w.r.t previous year
Gain Rs Crs/ Yr Investment Rs Crs Eenrgy Saving MKCal/MT 55
ENERGY BENCHMARKING
GLOBAL
8
7.3
7.2
7
1999-00 UREA PLANT BATTERY LIMIT
IGFL 6.4
MKCal/Te of Urea
6
5.3
5.1
5 4.6
3.9
3.8
4 3.6
3.4
8
3.1 7.3
7.2
3
7 2001-02 6.4
M KCal/Te of Urea
2 IGFL
1 2 3 4 5 6 7 8 9 10 11 6
5.3
Plants 5.1
5 4.6
3.9
3.8
4 3.6
3.4
3.1
3
5.70
5.63
5.60
5.60 5.55
M KCal/Te
5.47 5.48
5.50
5.30
5.20
5.20
5.10
OCFL NFL V1 IFFCO-1 CFCL-1 IGFL CFCL-2 IFFCO-2 NFL V2 TATA IGFL 57
BASIS OF ENERGY FOR 2006-07
Energy consumption for the year was 5.37 MKcal/MT of Urea. We had taken shut
down in Nov/Dec 2005 where in we carried out cleaning of heat exchangers and
implemented energy saving schemes.
59
RAW MATERIAL & THEIR SOURCE
NG NAPHTHA
UTILITIES
TOTAL 1.82 50
60
NG SUPPLY NETWORK
DADRI 24”
DELHI
TCL, BABARALA
ORIGINAL ROUTE
REVISED ROUTE
24”
IFFCO, AONLA
36”
24”
CFCL, KOTA OCFL, SHAHAJAHANPUR
18” 24”
18” THULANDI
30” IGFL, JAGDISHPUR
36” DIBIYAPUR (220 KM)
BIJAIPUR
HAZIRA
IFFCO, PHULPUR
After commissioning of Phulpur line, supply pressure is expected go down. As per contract,
GAIL shall maintain 45 kg/cm2g pressure at IGF battery limit. In case, GAIL is not able to
maintain the pressure, then it may become difficult to meet the requirement after revamp. GAIL
has already assured. 61
TYPES OF GASES AND CONTRACT
Indo Gulf has contracted with GAIL for three different kind of gases. The details are
as follows:
Gas Type Contracted Quantity Valid up to Price (USD / MMBTU)
APM 0.78 Msm3/day May 2008 3.19
R-LNG 0.76 Msm3/day Jan 2008 4.64
JV-PMT 0.28 Msm3/day April 2008 3.19
Total 1.82 Msm3/day
• Highlights of R-LNG Contract
– Contract for 9200 BBTU. Take or pay and supply or pay obligations.
– In each contract year (Jan-Dec) annual take or pay quantity is 95% of the
annual contracted quantity.
– The take or pay obligation will be on the difference between the actual quantity
drawn and 8740 BBTU.
– We can exercise 5% upward / downward flexibility, if required.
– At a plant load of 3000 MTPD, there would not be any possibility of take or pay
obligation on R-LNG. 62
TYPES OF GASES AND CONTRACT
Current NG Scenario
We are getting adequate quantity of gas for current operation of 3000 MTPD of
urea. The current gas allocations are as follows:
APM - 0.78 Msm3/day
R-LNG - 0.76 Msm3/day
JV-PMT - 0.28 Msm3/day
Total - 1.82 Msm3/day
GAIL has communicated that any overdrawl of gas shall be treated as
unauthorized over drawl and shall be priced at spot price of gas, which is about
12 USD MMBTU.
We are daily monitoring the gas consumption so as to avoid any overdrawl.
Consuming naphtha to keep consumption below allocation.
We also got permission from DOF for drawing gas at spot price of about 12
USD/MMBTU for one month. 64
CURRENT AND FUTURE NG SCENARIO
Future NG Scenario / Requirement:
Gas supply situation likely to remain very tight till 2008-09.
The renewal of all the contracts is due in 2008. The pricing of the gas shall be
based on the market price prevailing at that time and availability of gas.
The requirement of gas shall be as follows:
Contracted quantity :1.82 Msm3/day
Add. Quantity Required for current production @ 3000MPD :0.12Msm3/day
Add. Quantity Required for Ph I Revamp (1850/3215 MTPD) :0.14 Msm3/day
Add. Quantity Required for Ph II Revamp (1910/3320 MTPD) :0.06 Msm3/day
Total :0.32Msm3/day
Current requirement can be met by drawing gas at spot price (Current spot Price
USD12/MMBTU) for which approval shall be obtained from DOF time to time
and/or use of Naphtha.
We have already entered into Heads Of Agreement with GAIL for our additional
requirement. We need to enter in to agreement with GAIL for add gas.
We will also initiate dialogue for entering into agreement with GAIL for existing
gas quantities from 2008. 65
COST EFFECTIVE
INITIATIVES
66
CHEMICALS CONSUMPTION COST &
MAINTENANCE EXPENDITURE
70 1600
Due to higher Rs. /MT of Urea
MEA unit cost 1400
65
61
1200
59
60
1000
RsLakhs
55 52 52 800
600
50
400
45
200
40 0
03-04 04-05 05-06 'P&B 06-07 00-01 01-02 02-03 03-04 '04-05 '05-06
Initiatives Taken
Use of imported carbon instead of indigenous Carbon. This is having longer life and thus less
replacement required.
Optimization of COC in cooling water and trough puts in DM plant 67
BAGGING PLANT
KEY QUALITY REQUIREMENTS
IN-PROCESS DEFECT REDUCTION
UNSTITCHED BAGS
MANUFACTURING DEFECT IN BAGS
BAG RUPTURE
SWEPT UREA
PRODUCT GIVE AWAY
UNSTITCHED BAGS
0.080
0.07
0.070
PERCENTAGE
0.060
0.05
0.050
0.040
0.030
0.02
Good
0.020 0.01 0.008
0.005 0.0050
0.010
0.000
1999-00 2000-01 2001-02 2002-03 2003-04 2004-05 2005-06
YEAR 68
BAGGING PLANT
PERCENTAGE MANUFACTURING DEFECT BAGS
0.04
0.04
0.030
0.03
0.03
0.020
0.02
0.02
0.010 Good
0.01
0.006
0.01 0.002
0.001 0.001
0.00
1999-00 2000-01 2001-02 2002-03 2003-04 2004-05 2005-06
YEAR
BAG RUPTURE
0.08
0.07
0.07
PERCENTAGE
0.06
0.05
0.04
0.04
Good
0.03
0.02
0.02
0.01 0.007
0.01 0.005
0.002
0.00
1999-00 2000-01 2001-02 2002-03 2003-04 2004-05 2005-06
YEAR 69
BAGGING PLANT
BAGS CONSUMPTION/MT OF UREA BAGGED
20.0160
20.0140 20.013
N o. of B ags
20.0120
Good
20.0100
20.008
20.0080
20.0060
20.004
20.0040 20.0020
20.002 20.002
20.0020 20.001
20.0000
1999-00 2000-01 2001-02 2002-03 2003-04 2004-05 2005-06
YEAR
35
31.45
30
23.22
25
20 Good
15
8.16
10 6.33 6.06 6.00 6.00
0
1999-00 2000-01 2001-02 2002-03 2003-04 2004-05 2005-06
YEAR
70
SAFETY PRACTICES
71
SAFETY PRACTICES
73
KEY ENVIRONMENT ACHIEVEMENT
Planting about 5000 trees every year. So far planted 1.33 Lacs trees
since inception. 36% of total available area is covered under green belt.
Plant final effluent is being utilized for horticulture in plant and township.
About 66% of effluent is being utilized.
Environment clearance (EIA) for proposed de-bottlenecking (1910
MTPD) is under active consideration at UP Pollution Control Board,
Lucknow. Public Hearing conducted, which was very successful.
74
WATER CONSUMPTION & EFFLUENT
DISCHARGE
70
SPECIFIC WATER CONSUMPTION EFFLUENT UTILIZATION 66.5
9 8 60
% Use of efflu en t
M3/ Te of Urea
50
6 .0 3
5 .7
40 34.6
5 .2 3 5 .2 2 28.6
30
20
11 14
10
3
Go vt .No rm 2 0 0 2 -0 3 2 0 0 3 -0 4 2 0 0 4 -0 5 2 0 0 5-0 6
Ye a r 0
2001-02 2002-03 2003-04 2004-05 2005-06
400 120
360
SPM AT FACTORY BOUNDARY AMMONIA AT FACTORY BOUNDARY
3 50 100
100
300
80
2 50
200 60
15 0
40 27
71 25
10 0 61 61 60 20 20
20
50
0 0
Govt. 2002-03 2003-04 2004-05 2005-06 Go vt. 2002-03 2003-04 2004-05 2004-05
Norms No rm s 75
Q&EC - CORPORATE RESPONSIBILITY FOR
ENV. PROTECTION
S.No Recommendation of CREP Activities & Status
1. Efforts to conserve water with In compliance. Water
a target to have < 8 M /Te of consumption is 5.3M /Te of Urea
3 3
4. Storm water drain to be kept Storm water drains are being kept
dry except rainy season. dry other than in rainy season.
76
Q&EC - CORPORATE RESPONSIBILITY FOR
ENV. PROTECTION
6. Action plan for proper handling, Spent catalyst is sold to user party who
storage and disposal of spent has got the approval from PCB as per
catalyst. Hazardous Waste Rule.
7. Chalk shall be properly Totally eliminated Calcium Carbonate
managed and disposed off in sludge by installing Zeolite softening plant.
secured landfill.
77
OTHER PRACTICES
78
PRACTICES TO ACHIEVE EXCELLENCE
THINK
TANK
BENCH CORE
MARKING COMMITTEE
PROCESS INTERNAL
CAPABILITY COUSTOMER
SATISFACTION
FERTILISERS
RCM & WCM
WHY WHY
ANALYSIS
CROSS
COPQ FUNCTIONAL
SAFETY
PRACTICES
79
PRACTICES
Practices Owner
• Think Tank – N.K.Thakur
• Benchmarking – A.K. Gupta
• Core Team
– Ammonia – N.K.Thakur
– Urea – K.K.Singh
– Bagging – Md.Anwar
– Power Plant – S.N.Sharma
• Internal Customer Satisfaction – A.K. Bhargava
• Process Capability – S. Venkatraman
• R.C.M. and Why-Why Analysis – S.K.Singh
• Condition Monitoring – S.K. Sipani
• New Safety Practices – R. Kapoor
• Delegation – N.C. Bansal
• Cost of Poor Quality – D.Sahai
• Farmer interaction by Op.Staff – B.P.Padhee
• Cross Functional Teams – A.K. Bhargava
80
CORE TEAM
problems or issues.
PURPOSE
TYPES
GLOBAL
BENCHMARKING
EXTERNAL INTERNAL
82
BENCHMARKING
Global Benchmarking
• We appointed M/s. PDC, Netherlands to carry out
benchmarking study for urea plant energy efficiency.
• Based on the data Obtained from Japan Institute of
Planned Maintenance (JIPM)
3 projects in improve /control phase, target for sign off : 15th July ’07.
85
THINK TANK
PROCESS :
HOD compiles problems of previous day related to safety, quality, reliability, environment, cost,
energy and system failure
All problems are discussed one by one. All present put fourth their ideas / analysis to overcome
the problem.
HOD monitors the performance and if problem continues, it is taken up by Core Team for
minute analysis. 88
INTERNAL CUSTOMER SATISFACTION
What is Multi-skilling
• To impart knowledge of areas other than “Core”.
• To enable individuals to perform jobs of other discipline with little
guidance.
Purpose
• Increase availability of manpower having interdisciplinary skills.
• Improve analytical capabilities with cross functional knowledge
• Improvement in response time.
• Improved safety.
Status
• Training commenced wef 02.06.2003 under a task force
• Covered total 68 employees till date
• Methodology for training is explanation with cut models, simulations,
dynamic models, drawings, theory etc.
91
SKILL BASED TRAINING
1 MOTORS :
6 .0 0
TRANSFORMER
4.69 4.93
4 .0 0
4.53
3.58
3.78 2 .0 0
3.00
3.22 1 .0 0
2.43 3.67
4.58 1.84
9 BATTERY BANKS 2.58 4 AVR
3.22 3.40
3.83 3.80
93
AREAS OF CONCERN
94
AREAS OF CONCERN
RG Boiler:-
The existing RG Boiler has become week as more than 10% tubes are plugged.
We have new RG Boiler available with us which we are planning to replace in
March/April 2007 Phase II revamp.
Steam Super Heat Coil:
Coil is installed in convection section of primary reformer.
Upper Coil has bowing and tube sheets are damaged. Order has been placed on
M/s L&T. Planned replacement in Phase II revamp shut down
Carbamate Condenser
Installed in both Urea streams. Produces LP steam utilizing heat of condensation
During May’06 shut down inspection reveled thinning of baffle plates & liner
thickness reduction. Working out action plant with technology suppliers.
AREAS OF CONCERN
Synthesis Turbine Parting Plane Leak
Turbine casing is two halves. Steam is leaking from parting plane. In long run
may cause damage to casing. Planned repair in Phase II revamp S/D.
Urea Reactor Liner
Reactor shell is made of CS. Lined from inside to protect from corrosive liquid.
Liner thickness has reduced from original 7 mm to 3.5 mm (minimum). Planned
relining in Phase II revamp shut down
Exit of talented & qualified professionals
Talented engineers are leaving organization. After revamp, plant operation will
be very stretched and therefore for sustained superior performance, retaining the
talent is a key driver. The reasons for exit are:
• Opportunities are available in India as well as abroad.
• No growth at site
• Higher pay packages
• Better positions.
VALUE ADDED
PRODUCTS
97
NEW PRODUCT DEVELOPMENT
NEEM COATED UREA
450
400
400
350
'0 0 0 M T
300
300
250 251 Plan
Actual
250
200 175
150
100
'04-05 '05-06 '06-07 '07-08
Results of trial at our farm & NDUAT are more or less same as that of IARI
Sulphur Coated and Boronated Urea
We also produced small quantities of Sulphur coated and Boronated Urea
using the infrastructure for Zinc coating.
99
THRUST AREAS
CDM
DEBOTELLNECKING
ENERGY CONSERVATION
100
CLEAN DEVELOPMENT
MECHANISM (CDM)
101
CLEAN DEVELOPMENT MECHANISM
Global initiative taken in Rio earth summit in 1992. Initiative further strengthened
in 1997 under Kyoto protocol. Countries agreed to reduce aggregate emission by
5.2% below 1990 levels by 2008-12.
Under CDM, developed countries can buy carbon emission from the developing
countries so as to reduce their equivalent obligations.
Prevailing carbon credit rate is about 20 Euro/ MT of CO2.
Registered GV system up-gradation under CDM. CERs 60,239 MT (net) issued on
11th March 06 by UNFCCC
Globally First project in Fertilizer Industry. Entered into Contract with M/s
Barclays @ EURO 20/MT
Gain on accrued CERs (60,239 MT) Rs.6.25 Cr. In future Rs.2.6 Cr. per
annum on 25000 T of CO2 p.a.. 102
CLEAN DEVELOPMENT MECHANISM
Future Potential Projects - Expected Gain Rs 25 Crs/Yr
106
DEBOTTLENECKING JOURNEY
Step-3: Optimization of 1950 MTPD Ammonia Revamp cost by utilizing in-house talent.
We brought down project cost to Rs.112.5Crores. Financial Indicators were:
Revised Project Cost - 112.5
Revised IRR/ Pay back Period - 20 % / 7.8 years
Step-4: Innovative Thinking to further make project more attractive
• Original sanctioned was for 1950 MTPD revamp at Rs 137.7 Crs (with IRR of 15%) which
was revised in March 05 P&B to Rs 112 Crs with IRR of 20%
Process Adopted :.
• In March 2005 P&B we presented to Chairman to implement revamp in two phases as
approval from DOF was awaited for revamp.
• In phase I revamp up to 1850 MTPD with an investment of only Rs 13 Crs with in
shortest time by Sept/October 2005.
• Till we get approval from DOF, to work most optimum capacity with minimum investment
and implement as phase II in March 2007 108
DE-BOTTLENECK
INNOVATIVE THINKING
Step-4: Innovative Thinking to further make project more attractive
OUTCOME :.
Implement Phase I revamp of 1850 MTPD ammonia in Sept/Oct 2005 at an
investment of Rs 13 Crs which was very attractive ( IRR of 96%). We obtained
approval in March 2005 P&B from Chairman.
1910 MTPD was found to be most optimum capacity for Phase II Revamp at a
cost of about Rs 65 Crs.
We obtained Chairman approval in March 2006 P&B.
Total project cost reduced from Rs 112 Crs to Rs 78 Crs (IRR 22%).
Phase I (1850 MTPD Ammonia) Successfully implemented in Nov/December
2005 within 8 days. Start up was vertical. Sanctioned Amount. Rs13 Crs
DE-BOTTLENECK STATUS
Putting both the existing converters in series along with new loop boiler
Order has been placed for following items Basic & Detail Engg. Of suction chilling
IFFCO (P)
IFFCO (A)
IGFL
IGFL - Under
Implementatio
140
IMPLEMENT
140 ED
n
120 110.0
64.5
100
' R s C rs
80 115
60
13.0
40
20
0
'1750MTPD 1750MTPD 1850 MTPD 1910 MTPD 2020 MTPD
112
ENERGY
CONSERVATION
113
BENCHMARKING WITH
TATA CHEMICALS
YEARWISE ENERGY COMPARSION
IGFL Vs. TATA
• TATA incorporate many energy saving features like S 50 converter, MTS, HP
HRSG, condensing/extraction PAC turbine, since inception which resulted in their
higher project cost, however giving advantage on best energy consumption.
• The energy consumption reduction at TATA w.r.t. IGFL is given below:
6.00
TCL HP steam balance gives a
5.871 gain of 0.08 Mkcal / MT
5.90
5.50
5.38
5.40
5.30 5.20
5.20
5.10
5.00
FICC Norm IGFL FICC Norm TCL TCL'05-06 IGFL'05-06 116
TECHNOLOGICAL DIFFERENCE
IGFL Vs. TATA
Area IGFL TCL Energy Impact
MKCal/Te of urea
Condensing load in Compressor 58 Te/hr 38 Te/hr 0.11
GT WHB GT WHB
44 TPH MP
CONDENSATE Steam CONDENSATE
(min.) 40 Te
51 Te
Problem-
More heat
dumping in
OTHER USERS AND BACK PRESS. TURBINES
CW
Path Ahead
We are exploring possibilities of recovering heat being dumped in
considered in P&B.
Visit to latest generation fertiliser plants to identify new areas of
Future Energy
After Part I Revamp Expected Energy consumption shall be about
122
BROWNFIELD EXPANSION
Crs.
DOF requires Detailed Project Report.
Out sourcing of some items viz Phosphoric acid and utilities like, steam,
3 Reducing heat loss in to atmosphere along with the flue gases from the Apr-02
service boiler by utilizing it for preheating of combustion air for service 3200
boiler
4 Reducing heat loss in to atmosphere along with the flue gases from the Oct-02
primary reformer by utilizing it for further preheating of combustion air. 7500
5 Enhancing the power generation capacity of gas turbine by inlet air Apr-01
cooling employing concept of water fogging and utilizing electric power 15,000
for energy conservation by reducing heat dumping in cooling water.
6 Utilization of low grade heat getting dumped in CW and utilizing it as Mar-07
heat source in VAM for producing chilled water for suction chilling of 2700
process air compressor.
TOTAL ESTIMATED CERS 57,900
128
ENERGY SAVING INITIATIVES
DETAILS
Sl. Schemes Energy Saving Saving Investment
No. (MKCal/Te of (Rs/Lacs/Yr) (Rs. Lacs)
Urea)
March 06 P&B
1910 MTPD
March 05 P&B Rs.64.5 Crs
1950 MTPD
Rs 99 Crs
Investment Rs/Crs.
2
s e-
a
Ph
1850 MTPD
Ammonia
Rs.13 Crs D)
Revamp Journey
ETE
P L • Sept’04 - Sanctioned Rs.138 Crs. for 1950 MTPD
M revamp. IRR: 15%
O
(C • Mar’05 – Revised Project cost to Rs.112 Crs. for
e -1 1950 MTPD. IRR: 20%.
has
P • Nov/Dec’05 – Implemented 1850 MTPD Revamp
with Rs.13 Crs. IRR:96%
• Mar/Apr’07 – Revamp to 1910 MTPD with addl.
Rs.64.5 Crs. Overall IRR: 22%.
1650 MTPD Ammonia
Production capacity
ENERGY CONSUMPTION – TARGET Vs. ACTUAL
6.0
5.9 (ACTUAL- NOV.00)
TARGET SET IN NOV.00
5.74
(ACTUAL) 5.66 (AUG.01) 5.63(APR.02)
JUL’01
(ACTUAL)
5.6
FEB.02 5.51 5.55 (APR.03)
(ACTUAL)
5.45
AUG’02
5.4 (ACTUAL) 5.36
TARGET REVISED IN AUG.01
5.205 (APR.04)
5.2