Lubrication issues
Rolling Element skidding
Pulverized Fuel Mill
Laurence-Scott
985 RPM 522KW
Driving a bowl
mill
Continuous
operation
12 Across the site
Details
Drive End Bearing - NU322
Greased weekly with 8 ‘shots’
Audible screech from bearing
on various motors
Cavity shows grease exiting
grease relief, some more than
others
VBLR - Mill 5C
MILL5C -M2X Motor DE Vertical (ACC)
Max Amp
.27 Hay stacks around 4000 Hz
Plot
Scale
0.14
RMS Acceleration in G-s
25-Aug-10
15:51:31
25-May-10
10:55:11
22-Apr-10
14:18:47
0 2000 4000 6000 8000
Frequency in Hz
Autocorrelation
VBLR - Mill 5C
MILL5C -M2X Motor DE Vertical (ACC)
1.0
Route ACorr(Wf)
25-May-10 10: 55: 11
RMS = .0352
LOAD = 100.0
RPM = 975. (16.24 Hz)
0.5
PK(+) = .7861
PK(-) = .9181
CRESTF= 26.11
Correlation Factor
-0.5
-1.0
3.0 3.3 3.6 3.9 4.2
Rev olution Number
Autocorrelation indicates random noise
VBLR - Mill 5C
MILL5C -M2X Motor DE Vertical (ACC)
2.4
Trend Display
of
2.1 Ov erall Value
-- Baseline --
1.8 Value: .460
Date: 09-Feb-10
RMS Acceleration in G-s
1.5
1.2
0.9
0.6
0.3
FAULT
ALERT
0
Date: 25-May-10
0 50 100 150 200 Time: 10: 55:10
Days: 09-Feb-10 To 25-Aug-10 Ampl: 2.025
Overall acceleration trend is erratic
VBLR - Mill 5C
MILL5C -M2P Motor DE Horiz Peakv ue
Max Amp
.20
Plot
Scale
0.10
RMS Acceleration in G-s
25-Aug-10
15:51:06
25-May-10
10:54:38
22-Apr-10
14:18:17
0 200 400 600 800 1000
Frequency in Hz
PeakVue spectrum shows no significant changes
60 Orders (990 Hz)
1600 LOR
1kHz HP
VBLR - Mill 5C
MILL5C -M2P Motor DE Horiz Peakv ue
3.53
25-Aug-10 15:51
.0
Acceleration in G-s
7.55
25-May-10 10:54
.0
6.40
22-Apr-10 14:18
.0
0 2 4 6 8 10 12 14
Rev olution Number
PeakVue waveforms show no significant impacting events, but a slight increase in
amplitudes.
VBLR - Mill 5C
MILL5C -M2P Motor DE Horiz Peakv ue
2.7
Trend Display
of
2.4 WARNING Ov erall Value
2.1 -- Baseline --
FAULT Value: 1.714
Date: 09-Feb-10
1.8
RMS Acceleration in G-s
1.5
1.2
ALERT
0.9
0.6
0.3
0
Date: 22-Apr-10
0 50 100 150 200 Time: 14:18:16
Days: 09-Feb-10 To 25-Aug-10 Ampl: .910
Overall PeakVue trend shows no increase in stress wave activity.
Downward trend could indicate that the reduction in grease quantity
could be heading in the right direction.
Primary Air Fans
Laurence-Scott
2130kW
1485 RPM
Four in continuous operation
Similar noise from Drive End bearing
NU330
Greased weekly on a ‘shot’ basis
Temperature spike coincides with the weekly lubrication program. In
some cases up to 90 Degrees C.
VBLR - Primary Air Fan 5A
PAF5A -M2X Motor DE Vertical (ACC)
2.8
Max Amp
2.72
0
25-Aug-10
16:04:59
20-Jul-10
14:33:22
23-Jun-10
RMS AccelerationinG-s
09:21:13
25-May-10
12:09:05
01-Apr-10
14:10:59
09-Mar-10
10:48:38
09-Feb-10
13:12:25
0 2000 4000 6000 8000 10000
Frequency in Hz
Broadband non synchronous energy
VBLR - Primary Air Fan 5A
PAF5A -M2P Motor DE Horiz Peakv ue
5
Max Amp 4
4.25 3
2
1
0
25-Aug-10
16:04:08
RMS Acceleration in G-s
20-Jul-10
14:21:59
23-Jun-10
09:15:02
01-Apr-10
15:41:44
0 400 800 1200 1600
Frequency in Hz
PeakVue shows fault frequency’s
Autocorrelation shows a BPFO
VBLR - Primary Air Fan 5A
PAF5A -M2P Motor DE Horiz Peakv ue
1.0
Route ACorr(Wf)
F F F F F F F F F F F F F F F F F F F F F F F F F F F F F F F F 20-Jul-10 14:21: 59
(PkVue-HP 2000 Hz)
RMS = .1208
LOAD = 80.0
0.5 RPM = 1480. (24.67 Hz)
PK(+) = .9579
PK(-) = .2318
Correlation Factor
CRESTF= 7.93
0 >SKF NU330
F=BPFO
-0.5
-1.0
Rev : 2.439
0 1 2 3 4 5 6 Ampl: .539
Rev olution Number
PA Fan 6A
VBLR - Primary Air Fan 6A
PAF6A -M2X Motor DE Vertical (ACC)
1.8
Route Spectrum
24-Sep-10 09: 37:12
OVERALL= 5.14 A-DG
1.5
RMS = 5.15
LOAD = 100.0
RPM = 1493. (24.89 Hz)
1.2
RMS Acceleration in G-s
0.9
0.6
0.3
0
0 2000 4000 6000 8000 10000
Frequency in Hz
VBLR - Primary Air Fan 6A
PAF6A -M2X Motor DE Vertical (ACC)
1.0
Route ACorr(Wf)
D D D D 24-Sep-10 09: 37:12
RMS = .0901
LOAD = 100.0
RPM = 1480. (24.67 Hz)
0.5
PK(+) = .7620
PK(-) = .6932
Autocorrelation shows FTF CRESTF= 8.46
Correlation Factor
>SKF NU330
and BPFO 0 D=FTF
-0.5
-1.0
Rev : 2.440
0 1 2 3 4 5 6 7 8 Ampl: -.460
Rev olution Number
VBLR - Primary Air Fan 6A
PAF6A -M2P Motor DE Horiz Peakv ue
1.5
Route Spectrum
DDDDDDDDDD 24-Sep-10 09: 36:49
(PkVue-HP 2000 Hz)
1.2 OVERALL= 3.13 A-DG
RMS = 2.46
LOAD = 100.0
RPM = 1493. (24.88 Hz)
RMS Acceleration in G-s
>SKF NU330
0.9 D=FTF
0.6
0.3
0
Freq: 10.00
0 80 160 240 320 400 480 Ordr: .402
Frequency in Hz Spec: 1.102
Other Symptoms
•During lubrication, little or no grease will exit
the grease relief
Why? As grease is worked by the rolling
elements oil is squeezed out of the matrix,
causing the grease to harden in service. This
can block the grease relief and grease can no
longer be flushed through the bearing. When
lubricated the fresh grease will take the path
of least resistance, on older motors this is
usually the inboard motor bearing seal. This
results in the grease entering the windings or
armature.
•Using a strobe can detect irregular
movement of the rolling element
•However the noise is an obvious method to
detect skidding. Skidding sounds like a high
pitched screech that goes away with a pump
of grease but usually comes back shortly
after.
Adding grease can increase the overall trend
VBLR - Mill 5D
MILL5D -M2P Motor DE Horiz Peakv
8
Strip Chart
of
Ov erall
7
6
RMS Acceleration in G-s
1
Time: .00000
0 30 60 90 120 150 180 Ampl: 2.439
Time in Seconds
VBLR - Mill 5D
VBLR-Mill 6A MILL6A
VBLR-Mill 6F MILL6F (09-Feb-10) MILL5D -M2P Motor DE Horiz Peakvue
0.6
0.14 Route Spectrum
Max Amp 0.12
F F F F F F F F F F 22-Jun-10 16:53:26
.14 (PkVue-HP 1000 Hz)
0.10 0.5
OVERALL= 1.04 A-DG
0.08 RMS = 1.04
LOAD = 100.0
0.06 RPM = 990. (16.50 Hz)
0.4
0.04 >SKF NU330E
F=BPFO
0.02
ninG-s
0.3
ninG-s
0
celeratio
MILL6F
tio
celera
MSAc
c
R
MSA
0.2
R
0.1
MILL6A
0 2000 4000 6000 8000
0
Frequency in Hz
Freq: 93.75
0 200 400 600 800 1000 Ordr: 5.682
Frequency in Hz Spec: .408
Spectrum will show haystacks PeakVue can show BPFO (not always)
Bearing skidding
Causes
• Over lubrication
If a grease cavity is full, the rollers can
pull in (churn) extra grease causing
over lubrication
• Blocked grease relief (causes over
lubrication)
• Grease too thick for the application
• Light radial loading i.e. Minimum load
requirements have not been met;
gearbox is taking all of the load;
magnetic centering of the motor has
unloaded the bearing.
Minimum load requirement
NU 322 ECJ
Dynamic load rating 468 kN (47 tonne)
Minimum load rating 3.36 kN (340
kg’s)
Rotor weight 17% – 33% of total
weight
Total weight=5080 kg
Rotor weight = 864 kg’s – 1524 kg’s
At the most each bearing is supporting
762 kg’s without taking into
consideration magnetic centering, and
weight supported by the gearbox.
Action by the Client
The charge of grease has been
reduced significantly. This has resulted
in less over temperature alarms
However vibration data does not
suggest a significant reduction in
skidding.
Why no more action?Lack of
conclusive evidence. Lack of
understanding of vibration analysis, no
acoustic data, no grease analysis
performed.
No recommendation for specific action
and fear of inducing further damage
by changing current practice i.e.
overheating a bearing by flushing out
the cavity with fresh grease.
Solutions
Most desirable Least desirable
• Convert to oil lubricated • Utilise an out of round
bearings raceway
• Purge old hard grease from • Use two preloaded hollow
the cavity rollers
• Reduce the amount of
grease Not recommended
• Machine down the shaft and • Misaligning the driver to
install the appropriate driven component
bearing
• Replace the cylindrical roller
with a deep groove roller
Other possibilities:
The noise and non synchronous broadband energy could be from a rub e.g. A
bearing seal. This would also cause a temperature increase.
There could be metal to metal contact occurring. Why? If the grease has thickened
in service metal to metal contact could be occurring due to the increased base oil
separation and lack of fluid film thickness.
What effect does skidding have on longevity of the bearing?
Actions:
Utilise Acoustic monitoring
Inspect the bearing
Take a grease sample
Clear the grease path/grease relief
Alter the lubrication interval – Reduce the lubrication frequency, increase the
charge
Change the lubrication method – Use the appropriate technology
Change grease
What is missing?
More data:
•Acoustic
•Temperature
•A structured approach to problem solving
•Evidence:- Strobe the rolling elements,
inner and outer race inspection
Useful Web Resources
Emerson CSi Technical Notes
http://www2.emersonprocess.com/en-US/brands/csitechnologies/productsupport/Pages/TechnicalNotes.aspx
Svenska Kullagerfabriken (SKF) calculators
http://www.skf.com/skf/productcatalogue/jsp/calculation/calculationIndex.jsp?&maincatalogue=1&lang=en
References:
Drayton M, case studies viewed 28th September 2010 at
http://www.lubrication.com.au/cs_bearing_skidding.htm
Goodman M, 2006, Using PdM technologies to determine, optimize lube condition, viewed 1 October 2010
at http://www.reliableplant.com/Read/23990/pdm-technologies-optimize-lube
Granger M, 2006, Using Sound Analysis to Monitor Lubrication Condition in Greased Roller Element
Bearings, Doctor Know application paper, Computational Systems incorporated
Hall J, 2006, Acoustic/Ultrasonic Lubrication, viewed 16th April 2010 at
www.reliabilityweb.com/art07/hall_lube_doc.pdf
Honeycutt J, et al, How To Design An Electric Motor Re-greasing Program, Tennessee Valley Authority, cited
Johnson W, Electrical Power Research Institute
Jacobyansky B, et al, 2009, Changing Greasing Habits with Predictive Maintenance, Guardian Industries
Bearings Reference Centre, viewed 1 October 2010 at
http://www.bearings.machinedesign.com/guiEdits/Content/BDE_6_4/bdemech6_30.aspx