Deeksha
Deeksha
Deeksha
RITU RAJ
DIVYA
DEEKSHA BARGUJAR
Incorporated in 1925 Products:
Jacket
Raymond Ltd. Trouser
Gauribidanur was Vest coat
2
Fabric stored in separate racks - shell, lining, pocketing,
canvas, felt and fusing
Material details are stored in Stage
Supermarket: The materials are stored in advance to be
issued for cutting for easy tracking
Inspection done based on 12 parameters:
4point system Color fastness
Shade band card Hand feel
Face side approval Bowing & skewing
Shrinkage Sponging
Nap CSV
Width report Seam slippage
3
Trims are arranged and stored in racks,
rejected ones separately
The value of materials stored is around
2.5 crores.
30 days inventory is stored in trims store
Issue trims as per production planning &
other material as per requirement
Trims are checked based on AQL 2.5
system
Labels are counted, defects in weave are
checked
Buttons are checked for defects: shade
variation and broken buttons
4
Spreading lines – 7 for jacket, 2 for trouser
Manual spreading is done for shell fabric to avoid bowing and skewing
Auto spreader is used for lining
Face to face spreading is done
Generally 50 plies are laid at a time, but it varies according to the
requirement
Pinning table is used for matching checks
Scope of improvement:
Use of thread within the pins of pinning table itself, to save time of threading
and knotting
5
Cutting machines:
5 CNC cutters
6 band knives
3 straight knives
In jacket –
All parts are ready cut in CNC cutters and sent for 100% inspection for solid
fabric
Back, lapel and collar are block cut and then re-cut in band knife
There are 7 fusing machines in fusing section
50 garment parts are fused in 1 hour
6
Jacket line is divided into:
Front section
Lining, collar, sleeve
Assembly
Unit production system is used in which the parts are moved using
conveyor
Trouser line uses straight line layout
7
6 jacket lines, 5 trouser lines
Jacket line output- 2400 pieces per day
Total manpower – 136
27 workstations consisting of 17 operations
Packing is done according to buyer’s requirement
Maximum 6 pieces in one carton
8
1950 Machines CRITICAL MACHINES
Preventive
Maintenance Auto dart machine
Andon system to Arm hole tape attach
indicate Breast pocket welting
1. Breakdown in
Sham hole
critical machines Blind hem
Zig-zag
2. Quality issues
Front edge machine
Material tracking & Sleeve attach
stacking system in Button hole
store
9
Planning layouts
Monitoring Production flow system
Decide the machines and attachments for all style
Monitoring and improve the operator performance
Operator training
Production control system
Quality control
Develop wage and salary administration systems and job evaluation
programs
Rate and update skill matrix
10
Quality assurance is done at every stage
In case of defects, the garments are sent for alteration or re-cutting
accordingly
Inspection is of 2 types:
Stationary and roaming
TLS audit, internal audit and external audits are done to ensure
quality of products
11
SILVER SPARK APPAREL LTD., UNIT-II
12
PRESENTED BY-
RITU RAJ
B.F.TECH.
BFT/14/870
1 • Observation
2 • Problem Identification
3 • Plan of Action
4 • Implementation
5 • Result
6 • Scope of Improvement
13
1
14
BEFORE
15
PROBLEMS FACED IN PREPARATORY(BEFORE)-
Movement of material, manpower was more
Time consuming for every operations
Material moves from trolley to machine after that pressing table after that WIP trolley
BENEFITS (AFTER)-
From this string diagram we can save time of operators
Movement of material become less
From this new layout we can increase productivity from auto facing m/c because in
this for six lines we are using four auto facing m/c for front pocket facing attach and
for back pocket facing attach, SNLS m/c are used.
16
AFTER
17
LAYOUT
PROBLEMS
Operations in preparatory was not in straight flow direction
Line 4,5 work was done in line 1 & 2.
For eg.- Line 4,5 front pkt. facing o/l done in line 4, this creates problem for production
tracking of individual line .
Movement of material was more
Time consuming for operators
BENEFITS
After changing layout movement of material and manpower reduced.
It saves time of operators
18
Line 2 FIT is interchanged
with line 2 pressing table (for
reducing the movement of
material)
19
LINE 1 AFTER AUTOFACING
M/C O/L M/C EDGE
CUTTER FRONT PKT.
POINTED FRONT PKT.
POINTED C BACK POCKET
FACING LABEL ATTACH
20
Line 6 Auto facing
m/c and fit is
interchanged with
line 4 o/l machine &
SNLS.
21
BEFORE AFTER
AFTER
This type of format was not clear Output of front pkt., Waist band, fly for
for others 8 hrs.
In this format output was shown Line wise is clear to others
as whole (sum of all lines) Visible for others
Line wise output was not clear In this format target and achieved
Time consuming for team leaders target is clear 22
BENEFIT-
From this format hourly
output can be visible to
others
Line wise production output
is clear
Auto facing m/c output is
visible
This format is not time
consuming
23
BEFORE AFTER
PROBLEMS BENEFITS
After m/c breakdown operator or After implementation of ANDON light the time of
team leader had to go to the calling mechanics is reduced
mechanic for solution Sound alarm is for calling mechanics
This was too much time consuming Three types of colour light is used
Attended time is more 24
When Red light is on then mechanics who are in the line can understand there is
some critical problem on machine and machine is not working
When orange light is on- it indicates that there is some small problems in machine
and mechanic has to attend the machine.
When green light is on- it indicates that there is no problem and the machine is
running in proper way.
From this needle time increases and idle time decreases.
After implementation of Andon light in critical machines 3 minutes time
saved for calling mechanics.
25
WORK STATION
REDESIGN IN PREPARATORY
LAYOUT
26
ZIPPER ATTACH M/C
29
W.B. FUSING M/C
BEFORE PICTURE
AFTER PICTURE
30
PROBLEMS- BENEFITS-
There is not proper placement After implementing band roll stand
for Band Rolls (fusing) used the haphazard way of placing rolls is
during waist band fusing abolished.
As we can see from fig. the
band rolls spreads on the floor From this implementation they follow
this is not the right way of 5S
placing anything on floor This we can see from fig. The band
Operators faced problem rolls are not kept on floor
during picking band rolls from
floor because they are under Fusing machine’s upper part become
the fusing machine. clear from band rolls.
Sometime operators kept rolls This shows a managed way of placing
on upper part of Fusing anything.
The average time saving of operator
machine that shows the
haphazard way of placing rolls. per hour is 16 minutes and capacity
There was not proper increased 96 pieces per hour
placement for keeping waist
band pieces join for fusing
under fusing machine.
Operators kept waist band
pieces on the floor for fusing.
31
AUTOZIG M/C
PROBLEMS (BEFORE)-
BENEFITS (AFTER)-
waist band cut pieces have not proper
After implementing waist band stand for
place for keeping them
waist band cut pieces there becomes a proper
Time consuming in finding waist band line
placement for waist band fused pieces
wise
Cycle time reduced per piece is 2
Re -cutting waist bands are less in no. that’s
second
why it has more chance to replace.
Capacity increase is 60 pieces per hour
Wastage of time is 15 minutes per hour 32
CONTD....
BEFORE
PICTURE
AFTER PICTURE
35
PROBLEM- BENEFITS-
In fly binding machine there was not After adding roller stand in fly binding
proper placement for keeping binders machine the WIP trolley become vacate.
Operators placed them in WIP trolley that Fly binding machine become more
was not right place for placing them spacious.
From this WIP trolley saw always Easy access of the rolls and hourly
overloaded, because of this the place for time saving is 4 minutes.
placing small parts in WIP trolley
reduced.
Some of them placed on fly binding
machine. From this the sewing area on
table reduced.
36
AUTO BOBBIN WINDER FOR LOOP
LOOP M/C
37
PROBLEM- BENEFITS-
There was not proper space for loop After implementing loop binder the work
after loop ready machine, from this flow becomes easy to operate
floor becomes very unclean Time saving for line operators
Time consuming for operators who Loop is binded in bobbin as line wise
come in preparatory from lines, they
first clear the knots from loop after that There are total 12 bobbins for loop
they rolled in hand for save loop from binding 6 for lines and 6 for preparatory
knotting.
The total capacity of one bobbin is for
Fusing machine bin were always full 160 pcs. Trousers
with loops, it is not easy to find out line
wise loop after fusing machine. This implementation is automatic that’s
why it takes less time
From loop floor in front of blind hem
machine becomes very messy. Air motor is attached with loop ready
machine from this when the machine
moves the loop binder moves with the
same speed of loop ready machine.
Easy to feed material to lines as
Bobbin winded form
There is no chances of Loop knotting
Rework time for unknotting by
operator is saved upto 12 minutes per
hour
38
SL No Improvement Area Before After
capacity/day Capacity/da
y
1 Auto Facing machine(per machine) 800 960
40
OBSERVATIONS
Autofacing m/c output- capacity of Auto facing m/c is 150pcs./Hr but output comes 90-
105 pcs./Hr
Operators skill- operators are not Multi skilled that creates problem during more
absenteeism.
Absenteeism on workstations
FREQUENT M/C BREAKDOWN
PROBLEMS
CAPACITY OF PREPARATORY-
CAPACITY= MANPOWER * EFFICIENCY * SHIFT TIME/SAM
Calculation:
Manpower: 34
Expected Efficiency: 80%
Shift Time: 480 minutes
41
Capacity = 35*80*480 /5.2*100
SOLUTION
1) AUTOFACING M/C ELEMENTAL BREAKDOWN REPORT
Problem- bundle loading time
Solution- reduced bundle loading time after implementing
stickers after per 50 pc.
Trolley arrangement according to parts
42
BENEFIT OF TROLLEY AND ITS SEGREGATION ACCORDING TO
SMALL PARTS-
Visible for others where the small parts are kept according to line.
This reduces bundle loading time of Auto facing m/c operators.
Maximum time for bundle loading for operators is 3-4 min. from this it becomes
1min.
Before this implementation pkt. Bag was kept one upon another bundle of 50 pcs.
From this same serial no. pkt. bag is placed in opposite column of trolley and
facing is placed in the upper part of trolley.
There are 4 rows and 3 columns in trolley two lines are divided for one line .
43
STICKERS AFTER
EACH 50 PCS. IN
POCKET BAG
45
PROBLEMS (BEFORE)- BENEFITS (AFTER)-
After segregation of trolley according to parts, visibility of
WIP trolley was not segregated according to parts
WIP becomes more clear for everyone.
Line 1-6 trolleys segregation was not matched with each
It saves time of line operators
other.
Line operators takes time for finding small parts. From this line 1-6 parts arrangement looks similar.
The searching time for parts and the serial no is The searching time reduced from 2 minutes to 10
more than 2 minutes. seconds for finding correct parts 46
3
OPERATION BULLETIN
SKILL MATRIX
PITCH DIAGRAM
TIME STUDY & BALANCE CHART
MULTI SKILL
7 DAYS WORKING DAY PLAN
47
48
4
Reduced bundle loading time after implementing stickers after per 50 pc.
Trolley arrangement according to parts
Segregation of WIP trolley parts wise
Layout
49
5 From this data we can find the output of
Auto Facing machine per week. In
Preparatory section Auto facing machine
AUTOFACING REPORT-JUNE
is the critical machine and it was the main
2000
source for output of front pocket bag
1800 There were 4 auto facing machine in
1600
preparatory, from each machine there
were a set target of 120 pcs./ hr. And the
1400
output came approx. 80-90 pcs. /hr.
1200
P
I 1000 AUTOFACING
E 800 REPORT-JUNE
C
600
E
S 400
200
0
1ST WEEK 2ND WEEK 3RD WEEK 4TH WEEK
50
REPORT
After implementing sticker system
AUTOFACING REPORT - JULY
2120
for bundle loading, 3 minutes of time
reduced and adding ANDON light in
Auto Facing machine, 10 minutes
2100
time reduced, from this the output of
Auto Facing machine increased day
P 2080 by day. This implementation is done
I in July 3rd week and the output came,
E we can differentiate with the output
2060
C of June month and can find the
E difference.
S 2040
2020 AUTOFACING
REPORT JULY
2000
1ST WEEK 2ND WEEK 3RD WEEK 4TH WEEK
51
AUTOFACING REPORT- AUGUST In august report we can see the
2300 production incensement as
compared to June and July month
2200
The auto facing machine output
will come 110 pcs/hr. from this
2100
type of implementation.
P
I
E 2000
C
AUTOFACING
E 1900
REPORT- AUGUST
S
1800
1700
1ST WEEK 2ND WEEK 3RD WEEK 4TH WEEK
52
6
54
55