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MM440 PLI Parameter Explain

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0% found this document useful (0 votes)
84 views12 pages

MM440 PLI Parameter Explain

Uploaded by

Dinh Vo
Copyright
© © All Rights Reserved
We take content rights seriously. If you suspect this is your content, claim it here.
Available Formats
Download as PDF, TXT or read online on Scribd
You are on page 1/ 12

Issue 12/01 Faults and Alarms

3 Faults and Alarms

3.1 Fault messages


In the event of a failure, the inverter switches off and a fault code appears on the
display.

NOTE
To reset the fault code, one of three methods listed below can be used:
1. Cycle the power to the drive.
2. Press the button on the BOP or AOP.
3. Via Digital Input 3 (default setting)

Fault Possible Causes Diagnose & Remedy Quit


F0001  Motor power (P0307) does not Check the following: OFF2
OverCurrent correspond to the inverter power (r0206) 1. Motor power (P0307) must correspond to inverter
 Motor lead short circuit power (r0206).
 Earth faults 2. Cable length limits must not be exceeded.
3. Motor cable and motor must have no short-
circuits or earth faults
4. Motor parameters must match the motor in use
5. Value of stator resistance (P0350) must be
correct
6. Motor must not be obstructed or overloaded
 Increase the ramp time
 Reduce the boost level
F0002  DC-link voltage (r0026) exceeds trip level Check the following: OFF2
OverVoltage (P2172) 1. Supply voltage (P0210) must lie within limits
indicated on rating plate .
 Overvoltage can be caused either by too 2. DC-link voltage controller must be enabled
high main supply voltage or if motor is in (P1240) and parameterized properly.
regenerative mode. 3. Ramp-down time (P1121) must match inertia of
Regenerative mode can be cause by fast load.
ramp downs or if the motor is driven from 4. Required braking power must lie within specified
an active load. limits.
NOTE
Higher inertia requires longer ramp times; otherwise,
apply braking resistor.
F0003  Main supply failed. Check the following: OFF2
UnderVoltage  Shock load outside specified limits. 1. Supply voltage (P0210) must lie within limits
indicated on rating plate.
2. Supply must not be susceptible to temporary
failures or voltage reductions.
F0004  Ventilation inadequate Check the following: OFF2
Inverter Over  Fan must turn when inverter is running
Temperature  Ambient temperature is too high.  Pulse frequency must be set to default value
 Ambient temperature could be higher than
specified for the inverter
 Additional meaning for Mega Master:
 P949 = 1: Rectifiere overtemperature
 P949 = 2: Ambient overtemperature
 P949 = 3: EBOX overtemperature
F0005  Inverter overloaded. Check the following: OFF2
Inverter I2T  Duty cycle too demanding. 1. Load duty cycle must lie within specified limits.
 Motor power (P0307) exceeds inverter 2. Motor power (P0307) must match inverter power
power capability (r0206). (r0206)
F0011  Motor overloaded Check the following: OFF1
Motor Over 1. Load duty cycle must be correct
Temperature 2. Motor nominal overtemperatures (P0626-P0628)
must be correct
3. Motor temperature warning level (P0604) must
match
F0012 Wire breakage of inverter temperature OFF2
Inverter temp. (heatsink) sensor
signal lost

MICROMASTER 440 Parameter List


6SE6400-5BB00-0BP0 229
Faults and Alarms Issue 12/01

Fault Possible Causes Diagnose & Remedy Quit


F0015 Open or short circuit of motor temperature OFF2
Motor temperature sensor. If signal loss is detected, temperature
signal lost monitoring switches over to monitoring with
the motor thermal model.
F0020 Fault occurs if one of the three input phases Check the input wiring of the mains phases OFF2
Mains Phase are missed and the pulses are enabled and
Missing drive is loaded
F0021 Fault occurs if the sum of the phase currents OFF2
Earth fault is higher than 5 % of the nominal inverter
current.
NOTE - Framesizes D to F
This fault only occurs on inverters that have 3
current sensors.
F0022 That hardware fault (P0947 = 22 and Check the I/O board. It has to be fully pressed home. OFF2
Powerstack fault P0949 = 1) caused by the following events:
(1) DC-link overcurrent = short circuit of IGBT
(2) Short circuit of chopper
(3) Earth fault
(4) I/O board is not poperly inserted.
 Framesizes A to C (1),(2),(3),(4)
 Framesizes D to E (1),(2),(4)
 FramesizeF(2),(4)
 Since all these faults are assigned to one
signal on the power stack, it is
notpossible to establish which one
actually occurred.
 UCE failure was detected, when P0947 =
22 and fault value P0949 =12 or 13 or 14,
depending on UCE (for MegaMaster
only).
F0023 One phase of output is disconnected OFF2
Output fault
F0024  Ventilation inadequate Check the following: OFF2
Rectifier Over  Fan inoperative  Fan must turn when inverter is running
Temperature  Ambient temperature is too high.  Pulse frequency must be set to default value
 Ambient temperature could be higher than
specified for the inverter
F0030 Fan no longer working  Fault cannot be masked while options module OFF2
Fan has failed (AOP or BOP) is connected.
 Need a new fan.
F0035 Auto restart fault after n-restart try OFF2
Auto restart after n
F0040 MICROMASTER 440 only OFF2
Automatic
Calibration Failure

MICROMASTER 440 Parameter List


230 6SE6400-5BB00-0BP0
Issue 12/01 Faults and Alarms

Fault Possible Causes Diagnose & Remedy Quit


F0041 Motor data identification failed. 0: Check that the motor is connected to the OFF2
Motor Data  Alarm value =0: Load missing inverter.
Identification  Alarm value =1: Current limit level 1-40: Check if motor data in P304-311 are correct.
Failure reached during identification. Check what type of motor wiring is required (star,
 Alarm value =2: Identified stator delta).
resistance less than 0.1% or greater than
100%.
 Alarm value =3: Identified rotorresistance
less than 0.1% or greater than 100%.
 Alarm value =4: Identified stator
reactance less than 50% and greater than
500%
 Alarm value =5: Identified main reactance
less than 50% and greater than 500%
 Alarm value =6: Identified rotor time
constant less than 10ms or greater than
5s
 Alarm value =7: Identified total leakage
reactance less than 5% and greater than
50%
 Alarm value =8: Identified stator leakage
reactance less than 25% and greater than
250%
 Alarm value =9: Identified rotor leakage
inductance less than 25% and greater
than 250%
 Alarm value = 20: Identified IGBT on-
voltage less than 0.5 or greater than 10V
 Alarm value = 30: Current controller at
voltage limit
 Alarm value = 40: Inconsistence of
identified data set, at least one
identification failed
Percentage values based on the impedance
Zb = Vmot,nom / sqrt(3) / Imot,nom
F0042  Motor data identification failed. OFF2
Speed Control  Alarm value =0: Time out waiting for
Optimisation Failure stable speed
 Alarm value =1: Inconsistent readings
F0051  Read or write failure while saving non-  Factory Reset and new parameterization OFF2
Parameter EEPROM volatile parameter.  Change drive
Fault
F0052  Read failure for power stack information  Change drive OFF2
power stack Fault or invalid data.
F0053  Read failure for IO EEPROM information  Check data OFF2
IO Eeprom Fault or invalid data.  Change IO module
F0054 1. Wrong IO board is connected.  Check data OFF2
Wrong IO Board 2. No ID detected on IO board, No data.  Change IO module
F0060  Internal communications failure  If fault persists, change inverter OFF2
Asic Timeout  Contact Service Department
F0070  No setpoint values from CB  Check CB and communication partner OFF2
CB setpoint fault (communication board) during telegram
off time
F0071  No setpoint values from USS during  Check USS master OFF2
USS (BOP-link) telegram off time
setpoint fault
F0072  No setpoint values from USS during  Check USS master OFF2
USS (COMM link) telegram off time
setpoint fault
F0080  Broken wire OFF2
ADC lost input  Signal out of limits
signal
F0085  External fault triggered via terminal inputs  Disable terminal input for fault trigger. OFF2
External Fault
F0090  Signal from Encoder lost 1. Check encoder fitted. If encoder not fitted, set OFF2
Encoder feedback P400 = 0 and select SLVC mode (P1300 = 20 or
loss 22)
2. Check connections between encoder and inverter
3. Check encoder not faulty (select P1300 = 0, run
at fixed speed, check encoder feedback signal in
P66)
Increase encoder loss threshold in P492
F0101  Software error or processor failure  Run self test routines OFF2
Stack Overflow

MICROMASTER 440 Parameter List


6SE6400-5BB00-0BP0 231
Faults and Alarms Issue 12/01

Fault Possible Causes Diagnose & Remedy Quit


F0221  PID Feedback below min. value P2268.  Change value of P2268.Adjust feedback gain. OFF2
PID Feedback below
min. value
F0222  PID feedback above max. value P2267.  Change value of P2267.Adjust feedback gain. OFF2
PID Feedback above
max. value
F0450 Fault value:  Drive may run but some features will not work OFF2
BIST Tests Failure 1. Some power section tests have failed properly.
2. Some control board tests have failed  Replace drive.
4. Some functional tests have failed
8. Some IO module tests have failed. (MM
420 only)
16. Internal RAM failed on power-up check
F0452  Load conditions on motor indicate belt Check the following: OFF2
Belt Failure failure or mechanical fault. 1. No breakage, seizure or obstruction of drive train.
Detected 1. If using an external speed sensor, check for
correct function.Check parameters:
 P0409 (pulse per min at rated speed).
 P2191 (Belt failure speed tolerance).
 P2192 (delay time for permitted deviation)
2. If using the torque envelope, check parameters:
 P2182 (threshold frequency f1)
 P2183 (threshold frequency f2)
 P2184 (threshold frequency f3)
 P2185 (upper torque threshold 1)
 P2186 (lower torque threshold 1)
 P2187 (upper torque threshold 2)
 P2188 (lower torque threshold 2)
 P2189 (upper torque threshold 3
 P2190 (lower torque threshold 3)
 P2192 (delay time for permitted deviation)
4. Apply lubrication if required.

MICROMASTER 440 Parameter List


232 6SE6400-5BB00-0BP0
Issue 12/01 Faults and Alarms

3.2 Alarm messages

Alarms Possible Causes Diagnose & Remedy Quit


A0501  Motor power does not correspond to the Check the following: ---
Current Limit inverter power 1. Motor power (P0307) must correspond to inverter
 Motor leads are too long power (r0206).
 Earth faults 2. Cable length limits must not be exceeded.
3. Motor cable and motor must have no short-
circuits or earth faults
4. Motor parameters must match the motor in use
5. Value of stator resistance (P0350) must be
correct
6. Motor must not be obstructed or overloaded
 Increase the ramp-up-time.
 Reduce the boost.
A0502 Overvoltage limit is reached. If this warning is displayed permanently, check drive ---
Overvoltage limit This warning can occur during ramp down, if input voltage .
the dc-link controller is disabled (P1240 = 0).
A0503 Main supply failed Check main supply voltage (P0210). ---
UnderVoltage Limit Main supply (P0210) and consequently DC-
link voltage (R0026) below specified limit
(P2172).
A0504 Warning level of inverter heat-sink Check the following: ---
Inverter temperature (P0614) is exceeded, resulting in 1. Ambient temperature must lie within specified
OverTemperature pulse frequency limits
reduction and/or output frequency reduction 2. Load conditions and duty cycle must be
(depending on parametrization in (P0610) appropriate
A0505  Warning level exceeded, current will be  Check that duty cycle lies within specified limits ---
Inverter I2T reduced if parameterized (P0610 = 1)
A0506  Difference between heatsink and IGBT  Check that duty cycle and shock loads lie within ---
Inverter duty cycle junction temperature exceeds warning specified limits
limits
A0511  Motor overloaded. Independently of the kind of temperature ---
Motor  Load duty cycle too high. determination check:
OverTemperature  P0604 motor temperature warning threshold
I2T  P0625 motor ambient temperature
 If (P601 = 0 or 1) Check the following:
1. Check if name plate data are correct (if not
perform quick commissioning)
2. Accurate equivalent circuit data can be found
by performing motor identification (P1910=1).
3. Check if motor weight (P344) is reasonable.
Change if neccesary.
4. Via P626, P627, P628 the standard
overtemperatures can be changed, if the
motor is nota Siemens standard motor.
 If (P601 = 2) Check the following:
1. Check if temperature shown in r35 is
reasonable.
2. Check if the sensor is a KTY84 (other
sensors are not supported)
A0512 Wire break to motor temperature sensor. If a ---
Motor temperature wire breakage is be detected, temperature
signal lost monitoring switches over to monitoring with
the motor thermal model.
A0520 Warning level of rectifier heat-sink Check the following: ---
Rectifier temperature (P) is exceeded 1. Ambient temperature must lie within specified
OverTemperature limits
2. Load conditions and duty cycle must be
appropriate
3. Fan must turn when drive is running
A0521 Warning level of ambient temperature (P) is Check the following: ---
Ambient exceeded 1. Ambient temperature must lie within specified
OverTemperature limits
2. Fan must turn when drive is running
3. Fan intake air has to be without any resistance
A0522 The cyclic access to the UCE Values and ---
I2C read out timeout powerstack temperatures via the i2c bus
(Mega Master) is disturbed
A0523 One phase of output is disconnected Warning can be masked. ---
Output fault
A0535 ---
Braking Resistor
Hot

MICROMASTER 440 Parameter List


6SE6400-5BB00-0BP0 233
Faults and Alarms Issue 12/01

Alarms Possible Causes Diagnose & Remedy Quit


A0541 Motor data identification (P1910) selected or ---
Motor Data running
Identification Active
A0542 Speed Control Optimisation (P1960) is ---
Speed Control selected or running
Optimisation Active
A0590 Signal from Encoder lost and Inverter has Stop inverter and then ---
Encoder feedback switched to sensorless vector control 1. Check encoder fitted. If encoder not fitted, set
loss warning P400 = 0 and select SLVC mode (P1300 = 20 or
22)
2. Check connections between encoder and inverter
3. Check encoder not faulty (select P1300 = 0, run
at fixed speed, check encoder feedback signal in
P66)
4. Increase encoder loss threshold in P492
A0600 ---
RTOS Overrun
Warning
A0700 CB (communication board) specific See CB user manual ---
CB warning 1 see
CB manual for
details.
A0701 CB (communication board) specific See CB user manual ---
CB warning 2 see
CB manual for
details.
A0702 CB (communication board) specific See CB user manual ---
CB warning 3 see
CB manual for
details.
A0703 CB (communication board) specific See CB user manual ---
CB warning 4 see
CB manual for
details.
A0704 CB (communication board) specific See CB user manual ---
CB warning 5 see
CB manual for
details.
A0705 CB (communication board) specific See CB user manual ---
CB warning 6 see
CB manual for
details.
A0706 CB (communication board) specific See CB user manual ---
CB warning 7 see
CB manual for
details.
A0707 CB (communication board) specific See CB user manual ---
CB warning 8 see
CB manual for
details.
A0708 CB (communication board) specific See CB user manual ---
CB warning 9 see
CB manual for
details.
A0709 CB (communication board) specific See CB user manual ---
CB warning 10 see
CB manual for
details.
A0710 Communication with CB (communication Check CB hardware ---
CB communication board) is lost
error
A0711 CB (communication board) reports a Check CB parameters ---
CB configuration configuration error.
error
A0910 Vdc max controller has been de-activated, Check the following: ---
Vdc-max controller since controller is not capable of keeping DC- 1. Input voltage (P0210) must lie within range.
de-activated link voltage (r0026) within limits (P2172). 2. Load must be match.
 Occurs if main supply voltage (P0210) is
permanently too high.
 Occurs if motor is driven by an active
load, causing motor to goes into
regenerative mode.
 Occurs at very high load inertias, when
ramping down.

MICROMASTER 440 Parameter List


234 6SE6400-5BB00-0BP0
Issue 12/01 Faults and Alarms

Alarms Possible Causes Diagnose & Remedy Quit


A0911  Vdc max controller is active; so ramp- ---
Vdc-max controller down times will be increased
active automatically to keep DC-link voltage
(r0026) within limits (P2172).
A0912 Vdc min controller will be activated if DC-link ---
Vdc-min controller voltage (r0026) falls below minimum level
active (P2172).
 The kinetic energy of the motor is used to
buffer the DC-link voltage, thus causing
deceleration of the drive!
 So short mains failures do not necessarily
lead to an undervoltage trip.
A0920 ADC parameters should not be set to  ---
ADC parameters not identical values, since this would produce
set properly. illogical results.
 Index 0: Parameter settings for output
identical
 Index 1: Parameter settings for input
identical
 Index 2: Parameter settings for input do
not correspond to ADC type
A0921 DAC parameters should not be set to  ---
DAC parameters not identical values, since this would produce
set properly. illogical results.
 Index 0: Parameter settings for output
identical
 Index 1: Parameter settings for input
identical
 Index 2: Parameter settings for output do
not correspond to DAC type
A0922 No Load is applied to the inverter.  ---
No load applied to As a result, some functions may not work as
inverter under normal load conditions.
A0923 Both JOG right and JOG left (P1055/P1056)  ---
Both JOG Left and have been requested. This freezes the RFG
JOG Right are output frequency at its current value.
requested
A0952 Load conditions on motor indicate belt failure Apply lubrication if required. ---
Belt Failure or mechanical fault. Check the following:
Detected 1. No breakage, seizure or obstruction of drive train.
2. If using an external speed sensor, check for
correct function.Check parameters:
 P0409 (pulse per min at rated speed).
 P2191 (Belt failure speed tolerance).
 P2192 (delay time for permitted deviation)
3. If using the torque envelope, check
parameters:
 P2182 (threshold frequency f1)
 P2183 (threshold frequency f2)
 P2184 (threshold frequency f3)
 P2185 (upper torque threshold 1)
 P2186 (lower torque threshold 1)
 P2187 (upper torque threshold 2)
 P2188 (lower torque threshold 2)
 P2189 (upper torque threshold 3)
 P2190 (lower torque threshold 3)
 P2192 (delay time for permitted deviation)
4. Apply lubrication if required.
A0936 PID Autotuning (P2350) selected or running ---
PID Autouning
Active

MICROMASTER 440 Parameter List


6SE6400-5BB00-0BP0 235
Suggestions and/or Corrections
To Suggestions
Corrections
Siemens AG
For Publication/Manual:
Automation & Drives MICROMASTER 440
Group Parameter List
SD VM 4
P.O. Box 3269

D-91050 Erlangen
Federal Republic of Germany

Suggestions for technical documentation User Documentation


From
Name: Order number: 6SE6400-5BB00-0BP0
Date of Issue: 12/01
Company/Service Department Should you come across any printing
Address: errors when reading this publication,
please notify us on this sheet.
Phone: __________ /
Suggestions for improvement are also
Fax: ________ /
welcome.
Siemens AG
Automation and Drives Group (A&D)
Standard Drives (SD) Division
Postfach 3269, D-91050 Erlangen © Siemens AG, 2001
Federal Republic of Germany Subject to change without prior notice

Siemens Aktiengesellschaft Order No.: 6SE6400-5BB00-0BP0

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