Paper Reliability Card Final 090817 IRTB
Paper Reliability Card Final 090817 IRTB
Paper Reliability Card Final 090817 IRTB
Abstract
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ls [kjhn dj batuksa dk mRiknu fd;k tkus yxk A vUrr% ;s midj.k Lons'kh rduhd }kjk eSllZ ckEckfMZ;j]
Hksy] usYdks ,oa dzkEiVu xzhOl }kjk fodflr fd;s x;s A bu midj.kksa esa bysDVªkfud dkM~Zl dh foQyrk ,d
fpark dk fo"k; jgk gS] D;ksfa d budh foQyrk ls rhu Qst batuksa dh fo'oluh;rk ,oa miyC/krk ij /kkrd
vlj iM+rk gS A bl isij esa bysDVªkfud dkM~Zl dh foQyrkvksa ds dkj.kksa dk foLrkj ls fo'ys"k.k fd;k x;k gS
,oa fofHkUu ijh{k.kksa ij vk/kkfjr lq>kvksa dk lekos'k fd;k x;k gS rkfd rhu Qst fo|qr jsy batuksa dh
fo'oluh;rk dks c<+k;k tk lds A
Indian Railways imported 22 WAG9 locomotives and 11 WAP5 locomotives from M/s.
ABB, Switzerland in 1996-97. Later on, CLW started manufacturing these locomotives by
procuring Power Converter, Auxiliary Converter & Control Electronics from ABB,
Switzerland. These equipments were subsequently indigenised by M/s. BTIL, M/s.
NELCO, M/s. BHEL and M/s. CGL through transfer of technology. The failure of electronic
cards of Power Converter, Auxiliary Converter and Central Electronics has always been a
source of concern which has not only been adversely affecting the reliability but availability
also of these locomotives. An effort through this paper has been made to analyse the
causes of failures of electronic cards, validate it through test trials and suggest remedial
measures to reduce the failures.
1.0 Introduction:
There are 05 locations in which 29 types of electronic cards, totalling 113 in
numbers are provided. There are three main equipments in which these cards
have been used in the locomotives. These electronic cards form part of Control
Cubicle of Power Converter, Gate unit & Gate unit power supply, Auxiliary
Converter and Vehicle Control Unit. The cards are identical for WAP5, WAP7 and
WAG9 class of locomotives.
1.1 Control Cubicle for Power Converter (SR):
There are total 13 types of electronic cards in power converter control cubicle
(figure-1). Mainly classified as power supply card, single board computer
(processor) card signal conditioning cards, NS/AS controller and peripheral card,
GTO optical pulse card, bus coupler card, analog & digital I/O cards. These cards
are placed in a dust proof housing as shown below.
1
GU GUSP
There are five cards for controlling auxiliary Converter (figure-3). These are power
supply card, controller card (processor card), chopper / WRE/GG controller cards,
auxiliary interface card and bus coupler cards. Besides this there is gate driver
card of WRE (inverter) module.
There are two cubicles provided in three phase locomotive in which cards for
vehicle control are housed (figure-4). Total 11 types of cards have been used in
each VCU. These are power supply cards, digital and analog I/O cards, single
board computer card, bus administrator cards (for vehicle bus & train bus), bus
coupler cards, signal routing board and display & diagnostic computer cards.
Figure-4: VCU
2
2.0 Failure analysis of cards:
Failure details of electronic cards of SR, BUR and VCU have been collected from
loco sheds. The failures of various cards of last five years are shown in table-1, 2,
3 and 4 in annex-I.
From the analysis of the cards it is clear that there are 11 types of cards (given in
table-A below) which have contributed approximately 70-75% of the total card
failures of the equipment in last three-four years: Item 1 to 4 contributes maximum
failures followed by 5-11.
UAB630A36/
5 Signal Conditioning Board 91/93 A/B/C slot of SR
2.1 Component wise analysis of failures of these cards has been done and are
summarised in table-B,C and D which are given as under.
4 IC 29.2% - 4.5% -
5 Resistor 18.5% - - -
7 PS 2022 - - 13.6% -
3
8 Fiber optic - 27.7% - -
transmitter
QFBR-1478C
(A101)
3 IC 6.25% - - -
5 EPROM - - 20% -
Table-C: Component wise failure analysis of card at S .No. 5,6,7 &8 of table A
Electrolytic - 9% 50%
2 capcitor
3 IC - 45.5% -
5 Transistor 16.6% - -
Table-D: Component wise failure analysis of cards at S.No. 9,10 &11 of table A.
2.2 Shed wise and make wise failure analysis of these cards of last three years have
been done. The analysis is given in table-5 and 6 of annex-II.
4
3.0 Conclusions from the failure analysis:
From the above analysis (table-B, C & D) it is clear that electrolytic capacitors are
the major cause of failures of cards. The other major causes are failures of
EPROMs, fibre optic components and hybrid module. As per the analysis the
failure cases are high after a period of 4 years of service which can be seen from
table-E below.
It is observed that the failure of electrolytic capacitor shows rising trends after 4
years of service mainly due to higher ambient temperatures in India. M/s BT has
informed that the rising trend of failure of such capacitors in European countries
has been observed after 9 years of service. Temperature measurements were
carried out at ½ inch away from the cards in locomotives which shows 15oC higher
temperature above ambient in power converter cards. The temperature rise in the
vicinity of auxiliary converter cards and VCU cards are comparatively less (table-
F). High rate of failure of power converter cards as compared to auxiliary converter
and VCU cards also substantiates it (table-1 to 4 of Annex-I). It seems that the
electronics of these three phase locomotive has been designed for European
climatic conditions (85oC class components have been used) where maximum
ambient temperature goes up to 40oC. In Indian conditions where ambient goes up
to 50oC, the temperature in the vicinity of cards goes up to 65oC, which means
temperature of components may be rising beyond 85oC particularly during
summers against the limit of 75oC for 85oC class components (margin of 10oC is
required for better life and reliability of components). This has been causing
premature failures of components and erratic behaviour of components, especially
during summers, which results in transient failures of cards. This is evident from
the failure analysis (table-B, C & D) where cases of NFF (no fault found) are
maximum and are generally more during summer.
5
Sl Locatio Ambient Machine Temp 1/2 inch away Temperature rise
No n Temp Room from card
Temp
1 SR2 43 48 58 15
2 BUR2 43 48 52 9
3 BUR3 43 48 54 11
4 VCU2 43 48 50 7
Table-F: Temperature recorded near cards of WAP7 locomotive
At 1.5 Times Expected Life of capacitors at ambient temperature and at 1.5 times Ripple Current based
Ripple on above graph.
Current
at 40 ºC Rehabilitation at 50 ºC Rehabilitation at 60 ºC Rehabilitation
expected required expected required after expected required after
life (Hrs) after year life (Hrs) year life (Hrs) year
10A 22mm 90000 12.84 48000 6.85 25000 3.56
dia Ir x 1.5
Table-G: Life expectancy of electrolytic capacitors
6
3.2 Card Specific failures & their remedial measures:
There have been increase in failures of this card in last 3 years (table-1). Make
wise analysis of these cards (table 6) indicates that the failures are in BTIL make
who have indigenised these cards in 2001 whereas BHEL and NELCO are still
importing this card. Shed wise failures of this card (table 5) also indicates that the
failures are predominantly in Ajni and Lallaguda sheds where BTIL make NS/AS
controller card mostly manufactured after 2001 have been provided in the
locomotives. After detailed analysis it is found that IC14C88, zener diodes and
resistors associated with this IC are failing (table-B). This is due to non
implementation of a modification of ungrounding pin no. 8 and 11 of the IC by M/s.
BTIL in their indigenous version (Figure-7), which was done by OEM in 1998.
With the grounding, IC picks up 15 V supply faster and during this time inputs to
the IC may be in undetermined state and can in cases causes output to go high
which leads to premature failure of IC, zeners and resistors. The modification of
ungrounding pin no. 8 and 11 is in progress which will eliminate this failure.
7
3.2.2 Gate Unit Card (GVA587A01)
Figure-8: GVA587A01
There have been failures of electrolytic capacitors mainly in Gate Unit cards after a
period of 5-6 years as evident from table-E and table-5 (failures are more in
Gomoh shed where these cards are comparatively older). Premature failure of
fibre optic transmitter (QFBR1478C, component A151) (figure-9) (table-B),
recently supplied in Gate unit cards, is also cause of concern. This component is
failing due to manufacturing problem of OEM, M/s AVAGO. As per the
investigation, this component is failing due to ‘back line effect’ where the output dB
level of the component goes down prematurely within a short span of time. It has
been learnt that manufacturing of the wafer of this optical transmitter was shifted
from USA to Singapore and final packaging of this optical transmitter was done in
Phillipines from January 2005 and onwards. Earlier, after manufacturing,
screening test of this component, comprising of burn-in cycle of 5000 hours from -
25OC to +75OC used to be done in USA. This practice was stopped when
manufacturing was shifted to Phillipines. Later on, this practice was reintroduced in
the end of year 2007 at Phillipines. Hence the lot supplied between Jan 2005 to
Sep 2007 is the source of this problem. RDSO has issued a testing procedure by
means of which output level of this component can be measured inside the
locomotives in simulation mode and if found below -18 dBM, the component has to
be replaced. This will eliminate the problem of premature failures of QFBR1478C
in suspected lot. It can also be used to weed out over aged defective fibre optic
transmitter.
QFBR1478C
8
3.2.3 Digital I/O Board Card (URB512D15)
As evident from table-6, the main cause of failure of this card is failure of 24V reed
relay. This relay controls closing (holding) and opening of VCB thereby making
and breaking inductive current of VCB coil. This results in flashing and welding of
contacts of the relay. The existing RC network (R=220 ohm, C=0.1 microfarad) is
not sufficient to prevent arc across the contacts while opening the VCB. After
detailed study the RC network has been modified (R=100 ohm with diode across
it, C=0.11 microfarad). Two cards having two N/O interlock in series and modified
RC network in reed relay and two cards having two N/O interlock in series and
existing RC network in reed relay are put on trial at ELS Lallaguda. These
modified cards are under trial at Lallaguda shed since May’09.
Figure-11: KUC153A01
3.2.4.1 There have been cases of intermittent tripping of this power supply card of
auxiliary converter on line particularly in summers. The problem was analysed in
detail and it was found that in due course of time the cover of electronics module
of auxiliary converter got changed where the air circulation openings were
reduced, resulting in temperature increase near the card (figure-12). The cover
has been modified to have more air circulation (figure-13), which have helped in
eliminating the problems in modified locos.
9
3.2.4.2 The main cause of failures of this card is electrolytic capacitors (table-B). This card
is being imported by all TOT partners so far. An effort has been made to develop
functionally equivalent power supply card indigenously. M/s BHEL has developed
this card with better output quality and simplified protection logic. One card is
under trial at ELS Ajni since Mar’09 and working satisfactorily. M/s BTIL and
NELCO are in the process of developing this card indigenously.
Gate driver card has been the major cause of failures in WRE modules over the
years (table-H).
Following are the main reasons and action taken to avoid the failures of GD
card:
10
Improved (Indigenous) Old (OEM not known)
This hybrid PCB has now been produced locally by BTIL using the same
facility as for the other MICAS S2 cards and quality has been significantly
improved (figure-14).
Frequent failures of zener diode were found in failed site returned WRE GUs.
(Part BZX55 3.6V 0.5 W, Drawing no. XN400249P0004, position no: V214
and V414). The power rating of zener diode (position 214 & 414) has been
increased. The alternate part is Silicon Planar Power Zener Diode
BZX85C3V6. This is a 1.3 W zener diode as against 0.5 W of earlier one.
Existing Modified
11
Figure-16: Fans in BUR
The failures of GTO have shown an increasing trend in 08-09 (table H). The
make wise and shed wise failures of GTO are tabulated in table-J.
Table-J Make wise and shed wise failure of GTO/Diode of WRE module
It is clear from the above that the GTOs are failing in BHEL make BURs of new
locomotives homed at Lallaguda and GZB shed. The failures are also in BT/S
make in GMO & GZB shed which are old. The matter has been taken up with
M/s BHEL and it is learnt that the failure of fibre optic transmitter (QFBR1478C)
is the main reason of failure of GTOs. This component is of Avago make.
RDSO has issued SMI No. 0256 dated 21.05.09 for testing of this component
(para 5.1.2(v) of the SMI).
12
4.1 Modified heat sink of power converter electronics (ALG rack):
The design of heat sink of traction converter electronics have been studied and
CFD analysis of air flow shows following deficiencies in the design:
The heat sink is of mild steel which is inferior to aluminium heat sink which
is commonly used as heat sink material. The earlier design is also not
effective as air contact with heat sink is minimal (Figure-17).
The air flow is not uniform across the length of heat sink resulting in hot
spots in the middle and opposite end (figure-18).
• .
A modified heat sink of Aluminium has been developed by M/s BTIL and M/s
NELCO through some outside agencies (figure-19 & 20) and trials conducted
have shown improvement in temperature rise by 6oC near traction converter
cards. This design has also made the air flow uniform which can be seen from
table-K.
Location Ambient Temp at card level Temperature rise
Temp
Traction Existing heat Modified heat Existing heat Modified heat
converter sink sink sink sink
near “V” slot 51 67 61 16 10
Temperature measurement
Air flow measurement
Heat sink Hose pipe side Middle Apposite to Hose pipe end
Type
Existing 1.4m/s 0.3m/s 0.6m/s
Modified 1.6m/s 1.3m/s 1.4m/s
Table-K: Temperature and air flow measurements
13
Existing Design Modified Design
Max air passing through outer area Comlete air passing through tubes only
No specific path for air flow, max air passing Specific path for air flow, air is passing
through nearby tubes through all tubes
Figure-19: Improvement in SR heat sink by BTIL
4.2 Another trial was done where heat conducting coating was provided inside the
ALG rack housing (figure-21). The trial results have shown improvement in
temperature rise by 6oC near cards (table-L).
14
Sl No Location Ambient Temp at card level Temperature rise
Temp Normal With coating Normal With coating
condition condition
1 Traction 51 62 57 11 6
converter
near ‘V’
slot
Table-L: Temperature measurements
4.3 Air conditioners of 2.5/3.0 tonnes capacity has been provided in one loco each at
LGD and GZB sheds at MRB outlets which have shown improvement in
temperatures rise by 7-8 OC near cards of SR, BUR and VCU electronics (table-M).
5.0 Use of better rated electrolytic capacitors having higher operating life:
The capacitors which were prone to failures have been identified for replacement
with better rated capacitors having better operating life. This will improve reliability
of cards. The details are given in annex-III.
6.1 Another problem associated with electronic card is accumulation of dust in three
phase locomotives. The problem of dust accumulation is attributed to less
pressurisation of machine room and improper filtering of incoming air to machine
room.
6.2 In order to avoid ingress of dust into locomotive, machine room of these locomotives
are pressurised using machine room blowers. The air delivery of machine room
blowers first pass through heat sink of electronic cubical of power converter,
auxiliary converter, vehicle control unit and thereafter it goes to machine room
compartment and finally escapes out through ventilators. It is noted that although
WAP5 locomotives is shorter in length by almost 2 meters but it has only 4
ventilators for escaping out the air, whereas WAG9/WAP7 has 6 ventilators even
though its machine room size is larger in volume.
6.3 The outlet air velocity in WAP7/WAG9 and WAP5 were recorded to evaluate the
pressure inside the machine room. These results are tabulated in table-N below.
15
It can be seen that the air velocity in WAP5 locomotive at ventilator point is almost
twice as compared to WAP7/WAG9 in stationary conditions. Following reasons
were identified for less pressure in WAG9/WAP7:
iii) There were noticeable leakages at the joints of suction side of oil cooling
blower, traction motor blower and scavenger motors which sucks in air
from the machine room (figure-22). Similarly there are leakage points
noticed through earth return cable in some locos (figure-23). These defects
are persisting in some locomotive right from the beginning due to
manufacturing problem.
More trials were conducted by different sheds to evaluate the direction of air flow
from the ventilators in WAG9,WAP7 and WAP5 locomotives at different speed with
four/six ventilators/ (blocking the two centrally located ventilators). Some of these
results are given in annex-IV.
i) The air starts flowing into the locomotive through the rear ventilators after 80
kmph onwards in those WAG9/WAP7 locomotives which have six ventilators
and the velocity of inflow increases with the increase in speed of locomotives.
ii) The air inflow into the machine room of locomotives from the rear ventilators
starts taking place even at lower speed, if there are leakages in machine room.
It can be seen that in WAP-7 Locomotive at 110 Kmph downward in flow of air
has increased up to 4.5 m/sec. which brings dust in locomotive where as in
WAP5 locomotive air flows out at appreciable speed even at 110 Kmph. It may
be appreciated that at higher speed i.e. around 130 Kmph this in flow will
further increase bringing in more dust in locomotive. This is one of the main
reason that air dust in WAP-7 locomotives are found to be more as compared
to WAP-5 during inspection.
6.4 Following action plan need to be taken to arrest the problem of ingress of dust in
locomotives –
i) Increase the blowing capacity of machine room blower by 30% and use
secondary filters after inertial filters in line with WAG6A locomotives.
ii) Block the centrally located two ventilators in all WAP7/WAG9 locomotives.
iii) Cause immediate action to arrest leakages of air from the machine room other
than through ventilators. Special attention should be given to joints of oil cooling
blower and scavenging blowers which are biggest source of problem. It is
noted that initially the gasket of OCB was completely round in shape and in
single piece whereas right now it comes in pieces which could be the main
reason for leakage. CLW should revert back to original design of gasket for
both OCB as well as scavenging blowers. Railways should also procure
complete gasket and replace it wherever it is required.
16
Gap on suction side
7.1 Action plan already issued through SMI/MS and are in the process of
implementation:
7.1.1 RDSO has issued instruction for rehabilitation of cards after six years by
changing electrolytic capacitors and other components such as EPROMS and
fibre optic components vide this office letter no. EL/11.5.5/8 dated 22.12.08.
RDSO has also issued guideline (no. EL/G/2008/01, Rev’1’ Aug’09) for
rehabilitation of these cards indicating the components to be changed during
rehabilitation. This also includes use of better rated capacitors as discussed in
para 5.0 above. This should be implemented by sheds.
7.1.2 To arrest the failure of IC:14C88 in NS/AS controller card, a Modification Sheet
( MS/0378 dated 29.05.09)) has been issued for ungrounding Pin No. 8 & 11,
which should be implemented. This modification needs to be implemented
through M/s BTIL. Loco sheds should pursue it with M/s BTIL and get it
implemented at the earliest.
7.1.3 To avoid premature failure of QFBR1478C in gate unit of power converter, a SMI
(SMI/257 dated 22.05.09) has been issued by RDSO for checking of dB level of
output of the fibre optic transmitter. Similarly to avoid shorting of gate and
cathode terminal of gate units, a Modification Sheet (MS/0378 dated 29.05.09)
17
has been issued by RDSO for inserting an insulated plate between gate and
cathode.
7.1.4 The cover of electronic module of auxiliary converter have been modified to have
more air circulation to avoid intermittent failure of power supply card. RDSO has
issued the instructions for implementation in field vide modification sheet no.
MS/0372 dated 20.01.09.
7.1.5 The reason of failures of gate driver card of WRE module of auxiliary converter
has been identified. RDSO has issued a Modification Sheet (MS/0372 dated
21.01.09) and letter No. EL/11.5.5/2/BT dated 11.11.08 to TOT partners for
doing the following modification in this card:
• Indigenisation of hybrid card
• Improvement in rating of zener diode
• Use of perforated cover on gate driver card
• Working the cooling fans continuously on by shorting thermostat
7.1.6 RDSO has issued SMI No. 0256 dated 21.05.09 for testing of gate driver of WRE
module of auxiliary converter, by which any suspected gate driver card can be
tested. Fibre optic transmitter can also be checked as per this SMI to avoid
failure of GTOs in WRE module.
7.1.8 To improve the pressurisation of machine room in WAP7 and WAG9 locomotives
and to avoid dust ingress in the machine room, RDSO has issued Modification
sheet No. 0380 dated 14.07.09 to block two centrally located ventilators in WAP7
and WAG9 locomotives.
7.1.9 The electrolytic capacitors, which are prone to failure have been identified for
replacement with better rated capacitors having better operating life. This will
improve the reliability of cards. M/s. BTIL and M/s. BHEL have been advised
(vide letter no. EL/11.5.5/5 dated 15.05.09) for manufacturing of cards with these
type of capacitors. All TOT partners have given their technical consent to use
these capacitors.
7.1.10 To avoid failure of 24 V read relay in digital I/O board, modified cards with reed
relays having 2 N/O interlock in series and improved RC network along with
diode across resistance are running successfully on trial in Lallaguda shed since
May/June, 2009. Use of this type of cards with modified reed relays and modified
RC networks for relay K250, K251, K247 and K253 have been decided.
7.2.1 To reduce the temperature near the cards of power converter, the design of heat
exchanger of traction converter electronics have been modified for better cooling.
These types of heat exchangers are in field trial. After field trial, regular use of
modified heat exchanger will be cut-in in future production and replacement in
the existing locomotives. Also for better heat transfer, thermal heat transfer paint
18
(type 20304) has been applied inside SR control cubicle, the temperature rise
inside the cards was recorded less as compared to the control cubicle where
heat transfer paint was not applied.
7.2.2 For improvement of cooling of electronic cards, a 3 ton air conditioner has been
provided in one loco at GZB shed at machine room blower outlet on experimental
basis. The results are very encouraging as an improvement of 7-8 deg. C in
temperature rise near cards have been observed. RDSO has prepared
specification of air conditioning unit. It is recommended to provide air conditioning
units in 10 WAP7 and 10 WAG9 locomotives for extensive field trials.
7.2.3 Functionally equivalent card of power supply card of auxiliary converter has been
developed indigenously by BHEL and is working satisfactorily in field for the last
three months. Similarly, power supply card of traction converter is also under
development indigenously. M/s. BTIL, M/s. NELCO & M/s. BHEL are in the
process of finalizing prototype of these cards. After development of these
indigenous cards, the problem of failures of these cards will be eliminated.
7.2.4 RDSO is working on increasing the capacity of machine room blower by 30%
and use of secondary filters after inertial filters in line with WAG6A locomotives to
avoid problem of dust accumulation. It is decided that an independent single
phase to three phase converter shall be developed to run the MRBs on 65 - 70
Hz frequency so as to increase the capacity by 30%.
The existing machine room blower has already been modified by changing the
design of blower impeller and the capacity has increased by 15%. This shall be
used at present without secondary stage filters to increase the pressurization of
machine room.
References:
1. Report No. RDSO/2007/EL/RM/0123, Rev.0 on issues concerning
reliability / availability of three phase electric locomotives.
2. Report No. RDSO/2008/EL/RM/0127, Rev.0 on repair of Printed Circuit
Boards of three phase locomotives.
3. Printed Circuit Hand Book – By Clyde F. Coombs, Jr
4. Printed and Integrated Circuitry (Materials & Process) – By T.D.Schlabach
& D.K.Rider
19
Annex-I
No. of failures
Single conditioning
1 board-SLG UAB630A36 A slot 4 1 4 5 11 9
Single conditioning
2 board-NSC UAB630A91 B slot 8 10 6 3 3 11
Single conditioning
3 board-ASC UAB630A93 C slot 2 3 6 1 7 10
NS Controller/AS MN/IJ 17 14 27 49 55 75
7 Controller PPA988B02 slot (27%) (31%) (37%) (51%) (39%) (41.2%)
Single board
9 computer PPB622B01 U slot 1 1 4 5 11 11
XYZ
11 Power Supply KUA915B01 slot 4 3 4 11 14 9
12 Rack 2 1 1 0 3 3
13 Unknown 2 0 4 0 0 4
20
SN Item 03-04 04-05 05-06 06-07 07-08 08-09
No. Of Failures
4 3 9 12 29 52
7 Digital I/O board URB512D15 J/L/O/Q slot (16%) (13%) (20%) (22%) (41%) (35.86)
11 Rack Rack 0 0 1 0 0 00
12 Unknown 1 4 0 0 0 02
13 Total 25 24 45 53 70 145
FRPCPY
17 (CARDS) 0.96% 0.78% 1.15% 1.06% 1.2% 1.95%
Table-3: Failures of cards of VCU
21
No. of failures
PPB471A0
1 Controller board 2 CD slot 6 6 10 8 3 18
Chopper
Controller/GG/WRE RDB472A0
2 Controller 1 F slot 3 0 2 0 5 08
Inver
Controller/Aux. UAB476A0
3 Interface 1 G slot 2 0 0 0 1 04
KUC153A0 18 23 36 39
4 Power Supply 1 3 (15%) (62%) 9 (31%) (70%) (68%) (50%)
5 Rack 6 4 8 2 8 08
6 Total 20 29 29 33 53 78
22
Annex-II
SN Name of PCB Type of Slot AJNI GMO GZB LGD Total
card Name 06- 07- 08- 06- 07- 08- 06- 07- 08- 06 07- 08- 06- 07- 08-
07 08 09 07 08 09 07 08 09 - 08 09 07 08 09
07
1. NS/AS PPA988B02 MN/IJ 39 41 22 4 6 12 6 7 15 - 1 26 49 55 75
Controller slot
2. Gate Unit GVA 587 SR 13 10 7 53 79 89 7 3 2 - 10 10 73 102 108
A01
3. Digital I/O board URB512D15 J/L/O/Q 5 13 9 2 10 7 4 3 12 - 3 24 12 29 52
slot
4. Power Supply KUC153A01 I slot 8 15 15 13 11 12 2 6 3 - 0 9 23 36 39
23
SN Name of Type of card Slot BT/S BT/I BHEL NELCO CGL Total
PCB Name 06-07 07- 08- 06- 07- 08- 06- 07- 08- 06- 07- 08- 06- 07- 08- 06- 07- 08-
08 09 07 08 09 07 08 09 07 08 09 07 08 09 07 08 09
1. NS/AS PPA988B02 MN/IJ slot 8 6 15 38 42 52 3 5 6 0 0 2 - - 0 49 55 75
Controller
2. Gate Unit GVA 587 A01 SR 58 85 90 2 6 13 12 9 4 - 2 1 1 0 0 73 102 108
24
Annex-III
For BTIL:
• 33 microfarad, 25V SMD capacitor, position No. C161 & C167, used in
PPB622/624/626/908 cards (table-7).
• 3900 microfarad, 35 volt capacitors, position no. C215 to C239 used in GVA
587A01 (table-8).
Nichicon: Jianghai:
UPL1E392MPH6 EC R 1E LH 392 MLL 75 1835
Temp range deg C -55 to +105 deg C -55 to +105 deg C
Size mm 18 (D) x 35.5 (L) x 7.5 (P) 18 (D) x 35.5 (L) x 7.5 (P)
Tan delta Nil 0.14 (max) at 120 Hz 20 deg.C 0.14 (max) at 120 Hz 20 deg.C
Leakage current µA 0.03 CV or 4uA after 1 min. 0.02 CV or 3uA after 2 min.
Load life Hrs 5000 at 105 deg. C 12000 at 105 deg. C
Ripple current (at mA(rms) 2690 at 10k to 200kHz 2740 at 100kHz
105 deg C)
Table-8: Use of better rated capacitor
25
C39-40/C48-49
For BHEL:
26
• 10MF/50 V, ABB REF: - HETT402382P0259 (For KUB921A0 URB177D15,
URB512D15) (table-12)
27
• 100MF/160 V, ABB REF: - 3BHC510003R0048 (KUB921A01) (table-16)
28
Annex-IV