Spe 170487 Ms
Spe 170487 Ms
Spe 170487 Ms
This paper was prepared for presentation at the IADC/SPE Asia Pacific Drilling Technology Conference held in Bangkok, Thailand, 25–27 August 2014.
This paper was selected for presentation by an IADC/SPE program committee following review of information contained in an abstract submitted by the author(s).
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Abstract
When first discovered, the gas field located in New Zealand was one of the largest gas fields in the world.
After more than 30 years of production however, the reserves have declined drastically. To manage the
decline, infill drilling campaigns have recently been initiated to access previously bypassed gas reservoirs
in the field.
A development campaign to boost the field recovery factor was kicked off with the objective of
boosting recoverable reserves and extending the life of the field by drilling four sidetracks from existing
depleted wells. A lightweight, compact and modular hydraulic workover unit (HWU) was installed on the
previously unmanned, small footprint production platform with a small crew size of 32 people. While
slimhole drilling and completion with a HWU had proven cost effective and a successful concept during
previous workover campaigns, sidetracking from larger casing sizes at 2000-2400 metres depth with a
HWU, including one dual casing exit design in this campaign, was the first of its kind for the operator.
The four sidetracks were completed and the operation was a technical success, in large part due to the
pre-job planning, project management and identification of unique challenges to this particular project.
This paper will discuss the operational challenges encountered by the HWU including BHA handling
and tripping in of the whipstock assembly when working with only a 12-foot jack stroke and minimal deck
space. Additionally, the minimal rig capabilities of the HWU created challenges with regards to optimum
whipstock and milling configurations/operations resulting from limitations on rotary torque capacity,
rotary speed, pumping capacity and drill string racking capability, all of which were resolved by creative
applications of the simple, robust yet versatile design of the casing exit technology.
Introduction
In the past the field operator embarked on the first Through Tubing Rotary Drilling (TTRD) campaign on
one of the platforms to maximize remaining recovery through infill drilling into previously uneconomic
and therefore bypassed pockets of gas. The campaign included drilling three new sidetrack wells from
existing wellbores through dual casing exits from the existing 5 - 1/2” completion and 7-5/8” production
casing. From the window a new 4-3/8” open hole section was then drilled to TD and completed with
slotted liner, swellable packers and sections of blank liner in order to provide necessary sand control.
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Although technically a success, the TTRD campaign had presented many technological and economic
constraints and challenges. The operational objective was to implement the most cost-effective solution
to extend the life of the wells. The field operator had initially considered a large number of options from
ERD wells, to short radius drain holes, and coiled tubing drilling. From past experiences, the platform rigs
had proven to be expensive due to the high mobilization costs into the region. As another potential
solution, coiled tubing could drill the wells but modeling showed there was a real risk of not being able
to run the liners to depth in the resulting drilled hole. Further more coiled tubing also didn’t offer the
synergies with other activities including water shut off, downward re-completions and well integrity work.
Tripping In
The HWU was designed to handle double joints of tubing or pipe and so tripping in and out of the hole
could be time consuming, particularly on deep wells. Additionally, the whipstock assembly was tripped
in with the 12-foot stroke hydraulic jack of the HWU, and this “snubbing” action meant constantly picking
up and stopping for setting between the stationary and travelling slips every 10-12 feet while tripping in
to the setting depth between 2000 to 2400 metres. This constant jerking of pipe action could potentially
create stress and metal fatigue on the attachment bolt leading to pre-mature shearing of the bolt and release
4 IADC/SPE-170487-MS
of the whipstock from the milling assembly. The 9-5/8” whipstock system was designed to utilize one of
the different three shear bolts with 40,000 lbs, 48,000 lbs or 59,000 lbs rating. In this campaign the 40,000
lbs shear bolt was used due to the limited string weight available with the HWU. However, lower shear
rating bolt meant higher risk of metal fatigue from the tripping operation.
Pump Capability
The HWU was equipped with two PZ8 Gardner Denver mud pumps and dressed with 6” liner, capable
of delivering a maximum of 400 GPM flow rate and 2800 psi pressure. The hydraulic 9-5/8” whipstock
was designed to be set by flow rate, and the minimum set up of 6 shear pins requires 350-450 GPM flow
Job Planning
Overcoming these challenges required thorough and careful planning at all stages of the operation along
with selections of specific technologies to mitigate the risk and technical constraint arising from the
unconventional drilling unit. Optimizing the installation requires working closely with the operator and
other drilling contractors during all wellbore planning, preparation and execution phases to ensure that the
best options were used and contingency measures were in place in advance of mobilizing and installing
the whipstock. The pre- job planning was focused primarily on the major five areas previously discussed.
Project Date August 2011 March 2012 June 2012 September 2012
Casing Size 9 5/8” 47ppf, L80 9 5/8” 43.5ppf, L80 ⫻ 13 9 5/8” 47ppf, L80 9 5/8” 47ppf, C95
3/8” 54.5ppf, K55
Whipstock Face (°) 3 3 3 3
Acchor Type Hydraulic Hydraulic Hydraulic Hydraulic
Attachment Bolt (lbs) 40,000 40,000 40,000 40,000
Setting Depth (m) 2067 1987 2410 2120
HSE
A few operational hazards were identified in the casing exit operation, such as potential for dropped
objects from the work basket, steel cuttings handling, SBM handling and spillage control, and also heavy
lifting issues. Job hazard analysis, risk assessment and mitigation, dropped objects prevention schemes
and complex lifting plans were carried out ahead of time to address all of these HSE issues. Training was
also provided to the crew to ensure cuttings handling equipment was fully commissioned and that spillage
reporting requirements were understood by everyone before the milling operation commenced.
Results
This section will discuss the operational sequence, milling event, milling parameter and the performance
in each well. A summary of this information can be found in Table 1.
Well #1
This was the first well of the campaign and the 9-5/8” casing exit job was the first major operation for
the well after completing the well abandonment and de-completion activities. The operation was crucial
to assess the readiness of the HWU before entering into the drilling phase, especially the performance
testing of the rotary head. The initial set up for setting of the hydraulic whipstock anchor was 380 GPM
tubular flow rate based on information provided during the pre-job planning. However it was reduced to
340 GPM to provide error tolerance for the pump capability. The MWD operating flow rate was set up
at 170 GPM for tool face reading. Before the whipstock operation, a simulation assembly comprised of
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8-1/2” window mill, 8-1/2” watermelon mill and 12 joints of 4” HWDP was tripped in hole to setting
depth. This trip provided the opportunity to ensure a clean wellbore at setting depth while also verifying
that proper casing ID was still available for running the casing exit system to depth. Additionally, this trip
was used to displace the well to 8.7ppg SBM and provided the opportunity to test the pumps’ performance.
The rotary test was performed at this stage also to confirm sufficient torque and rotary speed could be
delivered by the rotary head. The DP was racked back in double while tripping out.
The 9-5/8” whipstock was picked up with the platform crane and lifted to the work basket, and was
then set down on top of the hydraulic jack supported by a T-bar at working height. The pre-made up
Well #2
The original plan for this well was to exit from the 9-5/8” casing, however the cut and pull of
5-1/2”completion tubing at original planned depth was unsuccessful. As a result of the second tubing cut
at a higher than planned depth, the casing exit target depth was now located at a depth above the 13-3/8”
casing shoe. Fortunately, the resulting unplanned dual casing exit job from 9-5/8” and 13-3/8” casing was
well within the casing exit design and capability, and no modification was needed on either the whipstock
IADC/SPE-170487-MS 9
or the milling assembly. However this change to a dual exit pushed the HWU to the absolute limits of its
capabilities. Generally much higher rotary torque and rotary speed is required for milling two casing
strings at the same time, and much higher pump capability is also required for cleaning the higher volume
of steel cuttings generated.
The 9-5/8” whipstock and 8-1/2” milling assembly was made up and tripped in hole using the same
process as previously discussed to the setting depth at 1987 metres. Instead of using MWD to determine
tool face orientation as occurred in the first well, a wireline Gyro was instead used for the orientation
survey due to the straight hole profile. The wireline operation required much longer time as compared to
Well #3
The 9-5/8” whipstock and 8-1/2” milling assembly on this third well was made up and tripped in hole with
the same procedures previously discussed to the setting depth at 2412 metres. It was the deepest setting
depth among the four wells in this campaign, and also had the highest wellbore inclination at 30 degrees.
The whipstock was oriented with MWD to 63 degrees right of high side and the hydraulic whipstock
anchor was again set using water at a 330 GPM flow rate, and 1800 psi pump pressure. The well was then
displaced to 9.1 ppg SBM in preparation for the milling operation. After all the parameters were agreed
upon, the string was rotated at 70 RPM and free rotating torque reading was recorded at 10,000 ft-lb. The
window milling commenced from 2406 metres with 5,000 lbs WOM, 70 RPM, and 12,000 ft-lb milling
torque. Unfortunately, as milling progressed and more weight was applied, the rotary head started stalling
constantly due to the rotary torque exceeding its capacity limit. In response, the string was then picked up
to release the trapped torque and lowered back to the top of whipstock, after which all the parameters had
to be re-established before the milling could be resumed. After a few attempts, the rotary speed was
10 IADC/SPE-170487-MS
eventually dropped to 50 RPM before continuous milling could be achieved with 10,000 lbs WOM and
14,000 ft-lb of milling torque. After milling for 2 metres and reaching the lead mill’s “core point”, the
mills would not progress further. “Core point” is the terminology used to describe a milling event where
the lead mill has almost half way penetrated into the casing. At that point, the pilot tip of the mill with
the small cutting surface area is spinning directly onto the casing, likely causing the slow milling action
and dropping of milling torque that was seen. In response to such an event, the WOM should be applied
aggressively in order to push the mill over so that the casing can be exposed to bigger cutting structure.
Working with this HWU however and faced with the constant stalling of the rotary head, applying higher
Well #4
The 9-5/8” whipstock and 8-1/2” milling assembly was made up similar to the previous wells and tripped
in to the setting depth at 2120 metres. The whipstock was oriented with MWD to 30 degrees left of high
side and preparation began to set the whipstock anchor. Unfortunately, just before setting the hydraulic
anchor one of the pumps went down. With just one pump running, it was not possible to deliver the
maximum 350GPM flow rate needed to set the whipstock with water. According to the design and
hydraulic set up, the anchor should have been capable of setting at the range of 250-350 GPM. This rate
range was just a bit higher than the 245 GPM flow rate possible with the single pump. With the available
flow rate so close to the lower point in that setting range, and the whipstock anchor already oriented and
on depth, the decision was made to attempt to set the anchor. The setting attempt was successful and the
anchor was set and performed exactly as per design without any resulting downtime.
After shearing off the 40,000 lbs single attachment bolt to release the whipstock from the milling
assembly, the well was then displaced to 9.1 ppg SBM before suspending the operations for 24 hours
while waiting for the parts for pump repair. The operator wanted to get both the pumps back on line before
the milling operation commenced. Once the second pump was back in service, the milling operation
started with 70 RPM and a free rotating torque reading of 6,000 ft-lb. Helping this casing exit operation
was a new rotary head which had been installed following the poor performace encountered on the
previous well operation, which had led to the additional trip milling the window. On this fourth well of
the project, the window milling was completed in a single trip from 2122 metres to 2126 metres with
20,000lbs WOM, 70 RPM, and 12,000 ft-lb of milling torque. The total milling time was 3 hour and 48
minutes and average ROP was 1.05m/hr. Following the window milling an additional 3 metres rathole was
then drilled and the window was reamed to minimal drag and circulated clean with hi-viscosity sweep.
The mills were inspected and seen to have negligible wear and the 6-1/8” directional drilling BHA was
able to pass through the window without difficulty.
IADC/SPE-170487-MS 11
Conclusion
Despite the significant challenges encountered during this workover campaign, the experience of setting
a larger whipstock and milling larger casing window at deeper depth with HWU can be considered a
complete success. Excellent HSE, milling and operational performance was delivered throughout the
project. This success is, in large part, attributed to the substantial time invested in pre-project planning to
properly understand the challenges presented by the HWU capabilities and the resulting lack of opera-
tional envelope as compared to operations on a normal drilling rig. Whipstock system selection was
critical to ensure that the high flexibility needed to operate in such limited environment was possible.
Nomenclature
BHA ⫽ Bottom Hole Assembly
GPM ⫽ Gallons per Minute
PPG ⫽ Pound per Gallon
WOM ⫽ Weight on Mill
DP ⫽ Drill Pipe
HWDP ⫽ Heavy Weight Drill Pipe
DC ⫽ Drill Collar
MWD ⫽ Measurement While Drilling
SBM ⫽ Synthetic Oil Base Mud
ROP ⫽ Rate of Penetration
RPM ⫽ Revolutions per Minute
NPT ⫽ Non-Productive Time
TD ⫽ Total Depth
MD ⫽ Measured Depth
Acknowledgement
The authors wish to thank Weatherford management for their support and permission to publish this paper.
References
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RuedaH., HocolS.A.; “Milling Low- Side Casing Exit Windows in Horizontal Wells: A Case
Study”, paper IADC/SPE-150347-PP presented at IADC/SPE Drilling Conference and Exhibi-
tion, San Diego, California, USA, March 2012.
2. YunusF., DufourJ., RipayreA, Mercier,M. SuroC., SredensekE.; “A Unique Experience of Using
Hydraulic Workover Unit (HWU) for Re-entry and Drilling Operation Onshore Gabon”, paper
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Exhibition, Dubai, U.A.E. September 2005.