VAS Report - GRP Ankaleshwar
VAS Report - GRP Ankaleshwar
VAS Report - GRP Ankaleshwar
ULTRASOUND TECHNOLOGY
(Report No. MTSPL/12/2023-24 dated 14 July 2023)
Client details:-
Page 1 of 4
(1) Introduction: - An Ultrasound Technology based Compressed Air, Natural Gas & Steam
leak Audit was undertaken on 5th July 2023 at GRP Pvt. Ltd.
GRP Pvt. Ltd. is a leading manufacturing company of recycling rubber and reusing rubber for
new manufacturing in India. The brief details of the exercise are as follows: -
• Natural gas Incomer, Transmission lines between Natural gas Incomer and Production
Area, all external distribution system of Natural gas Incomer
Objective: - The main objectives of this exercise was to detect all minor and major leaks in
Compressed Air, Natural Gas & Steam System to find energy losses due to these leaks so that a
strategic action plancan be initiated to enhance plant’s Pneumatic System Hygiene, operational
availability and overall productivity.
High Voltage Electrical Asset were also inspected to detect presence of any Partial Discharge
(PD) related problems.
(A) Expected benefits: - All the leaking points were identified and documented. Plugging
these leaks will result in monetary savings, operational excellence, and improvement in plant
hygiene. Rectification of PD related problems will improve the reliability of High Voltage Electrical
assets resulting in safe operation and seamless production.
Page 2 of 4
(2) Executive Summary: -
(A) Jobs Undertaken: Leak detection using Ultrasound Technology for Energy Saving by finding
leaks in Compressed Air Systems, Natural Gas Lines, Steam line. These leaks, being very small in
intensity but large in numbers,could not be traced normally in noisy and activity laden shop floors.
(B) Results of Inspection: A total of 14 leakages were found in compressed air system accounting
for about 77.13 Ltrs/Min loss of air. Steam system accounted for about 128.16 Ltr/min. Expected
monitory savings post rectification of these leaks is about ₹1,79,482 per annum. A detailed
report indicating location, picture and extent of leaks is attached at Appendix A of this report. As a
general industry standard, an annual saving between 20% to 30% can be achieved by a complete
rectification of identified leaks. Savings will result from lesser running hours of compressors for
catering same requirement of shop floor, thus reducing overall Compressor’s power consumption
and allied maintenance work.
(C) Electrical Inspection: Integrated Electrical Asset Condition Assessment exercise was
undertaken using both Air-Borne and Structure-Borne Ultrasound Technology to assess Voltage
related defects like Partial Discharge (PD), Corona, Tracking and Arcing at an early stage,
especially applicable for High Voltage System (>1000V) to avoid catastrophic failures like Arc flash
and Arc blasts.
Following two positions were identified to be having Partial Discharge related defects: -
Page 3 of 4
(3) Summary of Report: -
The Leak detection audit brought forward a new avenue for energy saving by rectifying the identified
leaks. This will also prolong the life of Compressors by reducing their running hours, and thus MTBF
and overall maintenance.
It is highly recommended that such audit be conducted on at least half-yearly basis to bring about a
positive change in maintenance and production activities thus raising overall reliability, reducing
maintenance cost and enhancing profitability of the firm.
Page 4 of 4
Report | 7 Jul 2023
GRP ANKLESHWAR
created by:
Ajay Rajendra Yelve
SONAPHONE Serial:
10488
Leak Expert:
V1.6.3
number of measurements:
14
first - last measurement:
5 Jul 2023 - 5 Jul 2023
address: comment:
Mahadyuta Technical Solutions
Navi Mumbai, Cont: 9961854160
SUMMARY
7 Jul 2023
GRP ANKLESHWAR
2|11
Class 1: ≤ 1 l/min
Potential savings
Savings
The process of estimating the amount of leakage in a compressed air system is part of DIN EN
ISO 11011. This process provides data for energy management systems in accordance with DIN
EN ISO 50001. In this report, the total loss is indicated in l/min and can be used to estimate the
financial losses associated with the leakage, if data on the energy costs incurred when
generating 1m³ of compressed air is available.
Disclaimer: SONOTEC has developed a process for classifying and estimating the total leakage losses of a system to the best of its knowledge and ability, based on flow
acoustics methods. SONOTEC shall in no way be held liable for the results generated through the application of this process, nor for any decisions made on the basis of such
results. All actions taken by the end user based on the results are the sole responsibility of the end user, who accepts full liability for any such actions.
OVERVIEW
7 Jul 2023
GRP ANKLESHWAR
4|11
1 10488-055 14.05 70 9.9 Air High Ajay 5 Jul 2023 …PRESSOR/…/Compressor tank Inlet To be repaired
2 10488-057 9.45 38 9.9 Air High Ajay 5 Jul 2023 …let pipe/…/coupling compressor side To be repaired
3 10488-058 9.31 37 9.9 Air High Ajay 5 Jul 2023 …Air tank inlet pipe/middle coupling/… To be repaired
4 10488-059 11.12 49 9.9 Air High Ajay 5 Jul 2023 … compressor line/middle coupling/… To be repaired
5 10488-060 10.53 45 9.9 Air High Ajay 5 Jul 2023 …compressor line/coupling and To be repaired
valve/…
6 10488-061 14.74 75 9.9 Air Low Ajay 5 Jul 2023 …compressor line/coupling and To be repaired
valve/…
7 10488-062 7.91 57 5.0 Air High Ajay 5 Jul 2023 …ey Viscometer/coupling and valve/… To be repaired
8 10488-063 0.00 34 5.0 NG Low Ajay 5 Jul 2023 …ey Viscometer/coupling and valve/… Not repaired
9 10488-064 0.00 51 23.0 STEAM High Ajay 5 Jul 2023 Autoclave/A2/1st floor/… To be repaired
10 10488-065 0.00 48 25.0 STEAM High Ajay 5 Jul 2023 Boiler 1/…/…/… To be repaired
11 10488-066 0.00 52 25.0 STEAM High Ajay 5 Jul 2023 Boiler 1/…/…/… To be repaired
12 10488-067 0.00 47 6.0 Unkno… Low Ajay 5 Jul 2023 Thermopac 2 delivery pipe/…/…/… To be repaired
13 10488-068 0.00 51 25.0 STEAM High Ajay 5 Jul 2023 B plant Autoclave 1/…/…/… To be repaired
14 10488-069 0.00 50 25.0 STEAM High Ajay 5 Jul 2023 B plant Autoclave 1/…/…/… To be repaired
DETAILS
7 Jul 2023
GRP ANKLESHWAR
5|11
Loss Leq p
Rating ID Gas Priority Tester Date
[l/min] [dB] [bar g]
Loss Leq p
Rating ID Gas Priority Tester Date
[l/min] [dB] [bar g]
Loss Leq p
Rating ID Gas Priority Tester Date
[l/min] [dB] [bar g]
Loss Leq p
Rating ID Gas Priority Tester Date
[l/min] [dB] [bar g]
System: K1
Location: Main compressor line
Gas: Air
Remarks: Leakage detected at
Valve waterdroplets also
observed
Loss Leq p
Rating ID Gas Priority Tester Date
[l/min] [dB] [bar g]
Loss Leq p
Rating ID Gas Priority Tester Date
[l/min] [dB] [bar g]
Loss Leq p
Rating ID Gas Priority Tester Date
[l/min] [dB] [bar g]
Loss Leq p
Rating ID Gas Priority Tester Date
[l/min] [dB] [bar g]
System: Autoclave A2
Location: Inlet pipe of steam
Gas: Stem
Remarks: 3leakges found on the
pipe line
Loss Leq p
Rating ID Gas Priority Tester Date
[l/min] [dB] [bar g]
System: Boiler 2
Location: Valve near the Gauge
Gas: Air
Remarks: Leakage detected at
valve
Loss Leq p
Rating ID Gas Priority Tester Date
[l/min] [dB] [bar g]
System: Boiler 1
Location: Safety valve at upper
side of boiler
Gas: Steam
Remarks: Poor condition of
safety valve
Loss Leq p
Rating ID Gas Priority Tester Date
[l/min] [dB] [bar g]
System: Thermopac 2
Location: Thermopac Pipeline
overhead in Boiler room
Gas:
Remarks: Leakage of oil from
delivery line of Thermopac 2
Loss Leq p
Rating ID Gas Priority Tester Date
[l/min] [dB] [bar g]
Loss Leq p
Rating ID Gas Priority Tester Date
[l/min] [dB] [bar g]