JK Cement Jharli Best Power Optimize Plant
JK Cement Jharli Best Power Optimize Plant
JK Cement Jharli Best Power Optimize Plant
Mr. Anirudh Dani (Unit Head) Mr. Rajeev Agarwal (Head – E&I)
[email protected] Mr. Ashish Khulve (Head – Process)
Cont. No. 9717002938 Mr. Lokesh Pancholi (Energy Manager)
About JK Cement Ltd.
J.K. Cement Ltd. is a part of Industrial conglomerate JK
Organization. The Company is promoted by Late Mr.
Yadupati Singhania . The group entered the cement
manufacturing business in 1975.
• Type: RP+BM Combo • 4 Nos. FLS Gen Ventosem 8 • 300 KWp Ground Mounted
• Make: ThyssenKrupp Rotary Packer Solar Plant
Industries India • 8 Spout Single Discharge • Total Area 4650 m2
• Capacity: 240 TPH PPC • Capacity: 120 TPH
@3800 Blaine • 4 Nos. FLS TLM:1016J
• Polycom size: D-2050/ L- Manual Loader
1300 • 1 No. FLS CDA-1020
• Ball mill size: 4.4 m*11.0m Hanging Loader
• Separator size: SEPOL PC • 1 No. Beumer Autopac
32/27-410 Loader
• Design power: 28 Kwh/Ton
Throughput Journey TPH
285
262
238 234
231
222
23 TPH , 9 %
40 TPH , 18%
FY 18 FY 19 FY 20 FY 21 FY 22 Q1 FY23
Grinding Power (KWH/T)
30 28.87
27.29
25.11 24.93
25
20.56
20 18.67
4.37 Kwh , 18%
15
10 1.89 Kwh , 9%
0
FY-18 FY-19 FY-20 FY-21 FY-22 Q1-23
Total Plant Power (KWH/T)
34.66
35 32.08
29.67 28.84
30
25 24.22
22.37
20 4.62 Kwh , 16 %
15
1.85 Kwh , 8 %
10
0
FY-18 FY-19 FY-20 FY-21 FY-22 Q1-23
Equipment Wise Power (KWH/T)
1 1.00
FY 18 FY 19 FY 20 FY 21 FY 22 Q1-23 FY 18 FY 19 FY 20 FY 21 FY 22 Q1-23
Kwh/MT
Target 0.0092
0.0077
0.0072
4% Reduction
Technology
Upgradation -
Plant Improvement
Sustainability
Internal Benchmark-
• Goal Setting
• KPI
Brainstorming-
• Involvement
• Development
Major Encon Project planned for FY-23
Estimated Energy
Investment Estimated Saving
Sr. No. Project Description Saving
(Rs. In Lakh) (INR Lakh)
(MWH)
1. Installation of 2MWp Solar Power plant 700 2775 87.41
Reduce pressure drop across cement mill circuit (CFD
2. study and modification of duct) potential 30-40 mmWc. 10 317 23.3
Reduce the gap between vanes and casing in RAL.
Replacement of plant water pumps with high efficient
3. 4.2 60 4.41
pumps
Reduce Process Fluctuations Across The Plant by PID Loop
4. 6 160 11.70
Optimization
Install Level Based Auto Drain Valves For Compressed Air
5. 1 5 0.37
Receiver Drain
Methodology used:
64.00 Clinker Factor %
We have done various trails in phase manner for a long 62.20
62.00
period of time which includes –
60.00 58.90
• Optimization in residue and blain as per requirement. 58.00
• Increase Anhydride Gypsum by adding Mould Gypsum. 56.00 55.22 55.16
• Blending of different grinding aids.
• Use of Grinding Aid Endura SAK0026 with inter blending 54.00
of grinding Aid. 52.00
• Consistent Clinker quality from mother plant (min 30 50.00
Mpa). FY-20 FY-21 FY-22 Q1 FY-23
• Improvement in Particle Size Distribution.
Innovative Project
Use of BLDC Air Conditioner
Technology Innovation:
The BLDC AC consumes 800 watt Per Hrs ( 20 Kwh Per Day )
against the conventional 1730 watt Per Hour with Saving of 15
Kwh Per Day
Payback is 14 Months (@ Power Cost of Rs 7.25 / Kwh)
Methodology used:
• Brainstorming
• Inter Team coordination Annual Saving of 24 KL Diesel
• Kizen Monitory Saving Rs. 16 Lakh
Co2 Reduction 63.36 MT.
Strategic Project
Reduction in Ball Mill Power Consumption
Objective: Result:
Methodology used: Roller replacement and roller gap Roller Press SEC
optimization. 10
• Replacement of Bainite Rollers by Compound cast Rollers 8.85 9.09
which has low wearing pattern. 8.36
8.09
• Continue monitoring the gap and roller profiling as per
roller wearing pattern to maintain working gap. 7.41
7.12
Benefits:
• Low wear tear helped in maintaining constant gap
between rollers.
5
• Reduction in recirculation load.
FY 18 FY 19 FY 20 FY 21 FY 22 Q1-23
• Reduction in separator RPM.
• Increase in Throughput and reduction in Specific Power. Annual Saving of 0.68 KWH/T
Monitory Saving Rs. 0.71 Cr.
Utilization of Renewable Energy
R.P.O (Lacs No of R.E.C
Generation % of overall Power KWH) Solar (in Lacs)
Technology
Year (million electrical Year Consumption Generation
(electrical)
kWh) energy (Lacs KWH) Non (Lacs Kwh) Non
Solar Solar
solar solar
FY-20 0.385 0.88% FY-20 114.52 3.3 6.2 3.9 3.4 2.4
Ground
FY-21 Mounted (PV 0.383 1.06% FY-21 181.16 5.4 12.7 3.8 5.4 8.8
Cell)
FY-22 0.399 1.09% FY-22 33.87 1.01 2.71 3.9 1.02 -1.3
Yearly RPO %
▪ Non Solar - 3% /3%/3%
▪ Solar - 5.5% / 7%/8%
Use of Mould Gypsum Mould Gypsum is Waste of the Gypsum industry and by using the
2 (Waste Gypsum) as same for Cement production as an alternate raw material for
Alternate Raw Material Mineral Gypsum
Bulk transportation of We increase our Bulk Cement dispatch. This enable us to reduce
3
Cement the standard vehicle trips.
Cement dispatch lead
We have installed GPS in all trucks and drivers are instructed to
4 distance reduction by GPS
follow the shortest route which is validated by our Logistics dept.
tracking
Green Supply Chain Management
1 August,21 Direct Fly Ash unloading in fly ash silo extraction bin Rs. 4.0 Lacs Power Savings 1 Year
2 August,21 Group LOTO box and personal locks Rs. 1.0 Lacs Safety NA
Power savings & Throughput
3 August,21 Installation of VFD in Cement silo feeding elevator. Rs. 6.0 Lacs 6 Months
increase
4 August,21 Purging of bag House in DP mode Nil Power Savings via less Comp. run Immediate
5 August,21 Packer bin aeration blower auto start Nil Power Savings Immediate
Connection of Rotary feeder motors changed in Star mode
6 Sept, 21 Nil Power Savings of Rs. 1.3 Lacs/Year Immediate
from Delta
Stack Monitor Blower motor interlock provided with Bag Power Saving of Rs. 10625/Year
10 Oct,21 Nil Immediate
house fan due to idle running stop
23 Jan, 21 Shift Operator Performance Report Nil Operators performance shift wise Immediate
Involvement of employee - Kaizen
Sr.
Month Kaizen Investment Benefits Payback
No.
Installation of new Transmitter in Sector gate and logic It will reduce downtime and safety of
24 Feb-22 23500/- -
modification technician.
Installation of VFD in packer-2 bag filter fan motor of 75KW
25 Feb-22 5.2L Power Saving 21 Month
for power saving.
26 Feb-22 Installation of AC power saver in 4 nos. split AC. 8000/- Power Saving 16 Month
Installation of 4 nos. 1.5T, 800W BLDC split AC for power
27 Feb-22 1.66 L Power Saving 14 Month
saving.
28 Mar-22 Installation of Thermo- Hygrometer data logger 5000/- Data recording through mobile App -
Merging of belt BC170, BAC175, and CW180 in to belt
29 Apr-22 25800/- Power saving , ease of maintenance 3 Moths
BC190 in packing plant.
Centre gap reduced by 4-5 mm resultant
30 Apr-22 RP Profiling as per RP wearing Pattern - -
production increase by 5-10 TPH
Energy Management
• EMS
Energy
• Total 28 Energy Meters for all section and major drives. (>5% of total
Data power)
Collection • KW Transducers for All MCC incomers
EMS System
Various events and training programs conducted by CII are extended learning and
knowledge sharing platforms where we can unearth the best practices, latest
technologies and future roadmaps to achieve Excellence in energy efficiency.
Various Energy saving projects implemented in our plant are replicated from
Knowledge sharing programs and events by CII. Some of these projects are as
follows:
CII Circle Award (2022) - Best Energy Efficiency Unit in CII Best Fly Ash Utilization Best Fly Ash Utilization Green Co Gold Award – 2018
Energy Efficient DC (Under National Award for Award – 2022 by Mission Award – 2022 by Mission
PAT Scheme) Excellence in Energy Energy Foundation Energy Foundation
Management- 2021
Way Forward for Sustainability
Mr. Rajeev Agarwal (Head – E&I) Mr. Ashish Khulve (Head - Process) Mr. Lokesh Pancholi (Energy Manager)
[email protected] [email protected] [email protected]
9729991628 7419711250 7419711230