Ramjet
Ramjet
Ramjet
1991-09
Fruge, Keith J.
Monterey, California. Naval Postgraduate School
http://hdl.handle.net/10945/28115
NAVAL POSTGRADUATE SCHOOL
Monterey, California
THESIS
DESIGN AND TESTING OF A CASELESS
SOLID-FUEL INTEGRAL-ROCKET RAMJET ENGINE
FOR USE IN SMALL TACTICAL MISSILES
by
Keith J. Fruge
September, 1991
T259726
1
Unclassified
Security Classification of this page
13a Type of Report 13b Time Covered 14 Date of Report (year, month.day) 1 5 Page Count
Master's Thesis From To 1991, September 25 60
16 Supplementary Notation The views expressed in this thesis are those of the author and do not reflect the official
policy or position of the Department of Defense or the U.S. Government.
17 Cosati Codes 1 8 Subject Terms (continue on reverse if necessary and identify by block number)
Field Group Subgroup Solid-fuel integral-rocket ramjets, Air-to-ground missiles.
by
Keith J. Fruge
Captain, United States Army
B.S., United States Military Academy, 1981
from the
solid-fuel integral-rocket ramjet (IRSFRJ) that has no ejecta. Analytical design of a ramjet
powered air-to-ground missile capable of being fired from a remotely piloted vehicle or
helicopter was accomplished using current JANNAF and Air Force computer codes. The
results showed that an IRSFRJ powered missile can exceed the velocity and range of
current systems by more than a two to one ratio, without an increase in missile length and
weight. A caseless IRSFRJ with a non-ejecting port cover was designed and tested. The
experimental results of the static tests showed that a low-cost, caseless IRSFRJ with a non-
ejecting port cover is a viable design. Rocket-ramjet transition was demonstrated and
ramjet ignition was found to be insensitive to the booster tail-off to air-injection timing
sequence.
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TABLE OF CONTENTS
I. INTRODUCTION
n. DESIGN METHODOLOGY 6
V. DISCUSSION OF RESULTS 22
A. THEORETICAL STUDY 22
B. EXPERIMENTAL RESULTS 27
VI. CONCLUSIONS 33
LIST OF REFERENCES 34
IV
APPENDIX B - PERFORMANCE CURVES 48
6. VARIABLE DEFINITIONS 35
VI
LIST OF FIGURES
9a. Photograph of the IRSFRJ test apparatus and static test stand 20
10. Chamber pressure-time trace for the caseless IRSFRJ feasibility test 30
apparatus 31
vn
ACKNOWLEDGEMENTS
I cannot fully express the thanks and appreciation deserved by Professor Dave
Netzer. His quest for knowledge and his honest concern for his students were the
inspiration which started me in this project and guided me to its completion. I would also
like to thank the propulsion team of Mr. Pat Hickey, Mr. Don Harvey and Mr. Harry
Conner for their hard work and technical assistance in the construction of the solid-fuel
integral-rocket ramjet apparatus. Most of all, I wish to thank my wife Karen for her care
Vlll
I. INTRODUCTION
The purpose of this study was to investigate the feasibility of using a solid-fuel
launched from a remotely piloted vehicle (RPV) or a helicopter. The general design goal
for the missile was to double the range and velocity of current missile systems while not
There are several reasons for wanting to extend the range and velocities of current
air-to-ground missiles capable of being fired from RPV's and helicopter platforms. Target
detection capabilities of RPV's and attack helicopters are rapidly increasing and in the
near future, systems will be fielded which can acquire and track targets 10 to 20 miles
in distance. Additionally, the capabilities of missile seekers and for autonomous missile
operation are advanced enough for a missile to be launched in the general direction of
enemy targets and automatically acquire, select, and engage these targets. Consequently,
the ability of potential foes to engage our systems at extended ranges will also be
increasing. Thus, a missile with extended range for standoff purposes and high velocity
motors. These motors are simple, reliable and inexpensive and have been quite capable
of performing up to the level required for the missile's mission. However, the relatively
low L of these motors prevents the range or velocities to be increased significantly
without incurring too great a penalty in weight gain to be used in missiles fired from RPV
or helicopter platforms. Additionally, a large part of the missile's flight path occurs after
engine burn out, thus the missile generally is coasting during the final engagement phase,
which enhances the enemy's ability to evade being hit. Table 1 below describes
is listed for comparison purposes since the ERSFRJ is quite capable of powering an air
TABLE 1
Although no current U.S. RPV's carry a weapons payload, the new generation of RPV's
will have the payload capacity to carry at least a limited amount of ordinance.
The IRSFRJ has several attractive features which makes it a very desirable device
for powering an air-to-ground missile of the type under consideration. Typically, one can
expect an increase in range of 200 - 400 % over a comparable size and weight solid
propellant rocket motor [Ref. l:p. 1]. This characteristic of the IRSFRJ is due to it being
an air breathing device, thus the IRSFRJ's specific impulse (1^) is significantly higher
than for a solid propellant rocket as is shown in Figure 1. Simplicity of construction and
little need for esoteric materials allows the IRSFRJ to compete cost-wise very favorably
with solid rockets. They are easily tailored for rugged handling and are readily storable
with long shelf lives. Additionally, the self-throttling with air flow variations capability
allows the IRSFRJ to have a relatively wide operating envelope. Figure 2 depicts a
typical solid propellant rocket powered tactical missile and Figure 3 depicts a typical
The goal of this study was to determine the feasibility of using a small, low cost
IRSFRJ suitable for powering air-to-ground missiles which are capable of being launched
from RPV's or helicopters. Several additional requirements were also placed upon the
design with the emphasis placed on the RPV mission. There were to be no ejectables and
the outside diameter was not to exceed 5 inches. The range requirement was 10 - 20
nautical miles with the launch velocity at Mach 0.3 and the cruise velocity between Mach
2.0 - 2.5. The missile would nominally be launched from and cruise at an altitude of
20,000 ft. The length and weight were to be kept to a minimum while still meeting the
performance requirements.
A two level approach was used to solve this design problem. Initially, an analytical
approach based on SFRJ cycle analysis was used to obtain a missile configuration which
met the design criteria. Concurrent with and following the analytical design, a IRSFRJ
engine was designed and manufactured for evaluation on a test stand. Additionally, static
firings were conducted to determine the feasibility of using an IRSFRJ design with no
ejectables, where the solid ramjet fuel also functioned as the engine casing, in an attempt
Current JANNAF and Air Force computer codes were used to produce a conceptual
design for the IRSFRJ powered missile. A missile with a 5 inch outside diameter was
and missile size and drag characteristics. Typically, a shaped charge is used as the
warhead on air-to-ground missiles and its penetrating ability is related to the diameter of
the shaped charge. To insure the missile's ability to penetrate modern armored vehicles
with its above the target attack trajectory, it was determined that a minimum warhead
was selected because it afforded low drag and weight with good performance and
compatibility with the non-ejectable port cover IRSFRJ engine being developed for this
study. To maintain simplicity of design and to minimize weight and cost, a non-bypass
engine was chosen. Although this prevented the design from achieving the highest
The booster chosen for the IRSFRJ engine was of a nozzleless design, utilizing a
reduced smoke composite propellant. The reduced smoke characteristic of the booster
enhances the non-detection of both the launch vehicle and the missile itself. The
nozzleless booster design was chosen to meet the requirement for no missile ejectables.
Although the nozzleless design degrades the Isp of the booster by 20-25%, several
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IV. EXPERIMENTAL APPARATUS AND PROCEDURE
The main thrust of the experimental aspect of the missile design was to test the
feasibility of using a non-ejectable port cover. This port cover design must be simple and
inexpensive to manufacture, rugged and capable of being sized for a small diameter
missile. The second major thrust of the design was to test the feasibility of a caseless
engine design by having the solid ramjet fuel also function as the outer casing of the
engine. This requires the use of a fuel which is rigid and which has good structural
characteristics. To minimize volume and provide high performance, a fuel with a high
energy density is also desired. Another desired aspect of the fuel is that it be opaque in
order to prevent subsurface heating by radiation effects from the flame and to reduce the
visible signature. This opaque characteristic is especially critical in low light conditions,
since there is no outer casing to block the visible or infrared emissions of the combustion
process. In addition, it is required that the fuel pyrolysis temperature be high enough to
A potential candidate for a fuel which can meet these requirements is one which
combines Plexiglas with a high energy metal. The Plexiglas would function as the fuel
binder and provide the required structural strength and stiffness. To enhance the energy
output of the fuel, particles of a high energy metal, such as aluminum or boron would be
combined with the Plexiglas. Plexiglas contains 32 % oxygen by weight. The oxidizer
should enhance surface ignition of the boron and provide improved combustion efficiency.
To enhance the structural strength of the fuel, nylon fibers or other appropriate fibers
could possibly be added in small amounts without significantly affecting the combustion
To test the feasibility of having the IRSFRJ fuel also function as the outer casing
of the motor, a simulated solid-fuel integral-rocket ramjet motor case was constructed for
use on a test stand. Figure 4 describes this apparatus. The fuel grain consisted of a
burning rate of 0.673 in/sec at 500 psi was used for the booster. Because of the limited
propellant available an end-burning booster grain design was utilized, and the exhaust
nozzle was sized to provide a nominal chamber pressure of 500 psi versus 1000 - 1500
psi in an actual motor design. The propellant was ignited using a pyrotechnic and a
pressure-time trace of the run was recorded on an analog recorder. This test was
conducted to determine the behavior of the Plexiglas when exposed to the high
The non-ejectable port cover apparatus was constructed of stainless steel and was
mounted on a static ramjet test stand. A schematic of the apparatus with the port cover
closed is shown in Figure 5 while Figure 6 shows the port cover in the open position.
The overall design of the port cover apparatus was uncomplicated and rugged, with
was utilized and the air flows from the twin inlets of the test stand were joined together
10
CD
11
Fuel Grain Housing
12
Figure 6. Non-ejectable port cover apparatus in the open position.
13
A sliding cylinder functioned as the port cover. Opening of the port cover, to allow
for transition from the boost-phase to the sustain-phase, was activated by loss of boost
pressure in the combustion chamber. The port cover was held in the closed position by
a steel pin which could be retracted by a pneumatic device as shown in Figure 7. Port
cover actuation was accomplished by withdrawing the pin and permitting the pressurized
piston chamber to pull the port cover rearward. High temperature O-rings were used
throughout the apparatus to withstand the high operating temperatures of the booster and
Initial functional testing of the apparatus consisted of mounting it to the test stand
and attaching a sealed fuel grain. The ability of the apparatus to maintain prescribed inlet
pressures without leakage into the motor cavity was validated using pressurized air. The
sealed fuel grain was then replaced with an open grain to allow for testing the proper
mechanical operation of the apparatus with air flowing through the system. Controlling
of the test sequence and of the actuating port cover was handled by a Hewlett Packard
automatic data acquisition and control system. Repeated tests were conducted using cold
air to properly sequence the opening of the port cover and related functions and to insure
consistent and correct operation of the apparatus before conducting an actual test firing.
The goal of next phase of the testing of the apparatus was to determine the chamber
pressure characteristics of the boost-phase. Limitations of the test facility and the
booster design. A nozzleless booster design allows for a propellant grain geometry which
provides initial high booster chamber pressures, though the pressure drops off rapidly.
14
Pneumatic Pin Retractor
15
It also makes it physically possible to use a single exhaust nozzle sized for the lower
ejectable booster nozzle. Two modifications were made to simulate a nozzleless booster
design in this situation. First, the operating chamber pressures of the booster and the
sustainer phases were closely matched. Secondly, the nozzle was constructed of Plexiglas
and was designed to erode during the booster phase. This allowed the nozzle to be
initially sized for proper rocket motor booster-phase pressure and then increase in area
enough to allow for correct chamber pressure and high enough flow rates during operation
The boost propellant grain was a centered-perforated design and measured 2 inches
in length with a web of 0.25 inches. A 0.25 in deep and 0.25 in length sliver of the
Plexiglas fuel grain was removed from a recess at the forward end of the combustor, and
the vacated space was filled with propellant. This was done to insure that once the
booster propellant grain was consumed and the port cover was opened, that there would
still be some propellant burning in the chamber to assist in the ignition of the sustainer
fuel. The propellant was bonded to the Plexiglas fuel grain with RTV. Figure 8 shows
the booster and sustainer grain configuration. A test run was conducted by igniting the
solid propellant with a pyrotechnic and recording the chamber pressure trace on an analog
recorder. The behavior of the eroding Plexiglas nozzle was also to be recorded. With
this knowledge, the proper sequencing of the port cover opening was determined and
16
Figure 8. Caseless booster and sustainer grain configuration.
17
To perform the full transition run, inlet air conditions were simulated for a missile
velocity of Mach 2.5 at an altitude of 20,000 ft. The inlet air was allowed to rest against
the side of the closed port cover and an upstream bypass valve on the test stand allowed
the hot, high pressure air to be vented to the atmosphere until the port cover was opened.
The geometry of the fuel and propellant grains and the nozzle were kept the same as in
the earlier boost-only run. The Hewlett Packard automated data acquisition and control
system was programmed to monitor the inlet air temperature and pressure and the
combustion chamber pressure. The system also controlled the operation of the bypass
valve and port cover. Pre-run activities involved the calibration of pressure transducers
and thermocouples and setting the correct flow rates of air, heater fuel and make up
oxygen. The nominal mass flow rate of the air was set for 0.25 lbm/sec and the
temperature of the air was set at 1020 degrees Rankine. The air mass flux (G) in the
2
chamber port was expected to be 0.142 lbm/in sec and the fuel-air ratio at these
conditions was to be 0.054. The initial boost pressure was designed to be 170 psi with
progressive burning tempered by the effects of the eroding exhaust nozzle throat area.
The full transition test began by initiating the program which controlled the
operation of the Hewlett Packard data acquisition and control system. The ignition of the
boost propellant was accomplished manually. The data acquisition and control system
monitored the chamber pressure rise, and upon reaching 90 psi, the system then began
monitoring for a pressure drop down to 75 psi. At this pressure, the commands were
given by the control system to extract the port cover retaining pin, and simultaneously
18
close the bypass valve. The hot air entering the combustion chamber, in combination
with the small sliver of propellant still burning, was to ignite the Plexiglas and enable the
initiation of the sustainer phase of the run. After a short sustainer run time, the
combustion process was halted by opening the bypass valve and purging the combustion
chamber with nitrogen. Figure 9a and 9b show photographs of the test apparatus
complete with the fuel grain connected to the static test stand.
19
test stand
Figure 9a. Photograph of the IRSFRJ test apparatus and static
20
Figure 9b. Photograph of the IRSFRJ test apparatus
21
V. DISCUSSION OF RESULTS
A. THEORETICAL STUDY
A total of six final missile configurations were generated. Three flight mission
profiles were considered and missiles using the two types of fuel available in the software
were generated for each flight profile. Table 2 below describes the three flight profiles.
TABLE 2
For each missile considered, the design software generates nine different engine
configurations based on the input data. The selection criteria used to choose one of these
nine configurations was to minimize missile weight with a fixed range restraint.
Appendix A contains the complete printout of the results for the six missile configurations
22
Some of the characteristics common to all of the generated missiles are listed
below:
2
o Wing Planform Area - 0.50 ft
2
o Tail Planform Area - 0.25 ft
TABLE 3
MISSILE 1 2 3 4 5 6
23
The results indicated clearly that the design goals of the missile were met. In all
cases, the boron based fuel provided equal missile performance with the hydrocarbon
based fuel, but with less fuel required and a reduced fuel grain length, which consequent-
ly, reduces the overall length of the missile. One item to note is the weight of the
required motor case. The case weight for all configurations was approximately 10 % of
the total missile weight. Elimination of this motor casing by utilizing a caseless design
The comparison of the boron and HTPB based fuels utilized in the missile design
software and the proposed caseless fuel composed of Plexiglas and boron was based on
the grain geometry generated for missile number one detailed above. Comparisons were
made for three performance parameters; jet specific impulse, net fuel specific impulse
and specific thrust. Curves for each parameter, as it varied with the fuel-air ratio, were
produced and the results for the two fuels were overlaid onto each other. The resulting
graphs are contained in Appendix B. The jet specific impulse is defined by:
FJBt^K u e^ u e
(1)
m e m e gc gc
This value is obtained directly from PEPCODE. Figure 14, Appendix B shows the
24
variation of jet specific impulse with changing fuel-air ratio. The fuel-air ratio is defined
as:
fuel
f (2)
The result is shown varying with the fuel-air ratio in Figure 15, Appendix B. The last
performance parameter to be analyzed was the net fuel specific impulse. This is obtained
by dividing the specific thrust by the fuel-air ratio and is given by:
j = Fnet (4)
'"fuel
The change in fuel specific impulse with the fuel-air ratio is shown in Figure 16,
Appendix B.
The first performance comparison between the fuels was made by assuming the
grain geometries, as defined in missile one above, were the same for both fuels and the
regression rates for both fuels were also equal. The fuel-air ratio was 0.131 for the
boron/HTPB fuel but changed to 0.160 for the boron/Plexiglass fuel and the fuel
regression rate for both was taken as 0.0153 in/sec. The results for the three performance
25
TABLE 4
In this case, the fuels performed quite similarly with the boron/Plexiglas fuel providing
slightly better specific thrust. The boron/HTPB fuel had an advantage in the range
parameter of fuel specific impulse. The more dense boron/Plexiglas fuel would cause a
In the second performance comparison, the fuel grain geometry and the fuel-air ratio
were kept the same for both fuels. This results in a different fuel regression rate and burn
time for the two fuels. The burn time increased from 50.7 seconds for the boron/HTPB
fuel to 62.2 seconds for the boron/Plexiglas fuel, about a 23 % increase. The
TABLE 5
26
Once again, the values of the performance parameters of the two fuels were closely
matched. If the regression rate, thus burn time of the two fuels were also kept the same,
then the use of the boron (Plexiglas fuel would allow the fuel grain length to be reduced
by 16.5 7c while maintaining the same performance level as the boron/HTPB fuel.
One possible problem area involved in using a caseless fuel grain with Plexiglas as
a major ingredient, is that its pyrolysis temperature is relatively low (600-650 degrees
Kelvin). At a flight regime of Mach 2.5 at an altitude of 20,000 feet, the missile would
conditions, external erosion of the fuel grain due to aerodynamic heating should not be
a problem. One possible solution for higher Mach number or lower altitude conditions
would be to bond a light-weight insulator to the outside of the fuel grain. This would add
very little to the weight of the missile, while only slightly increasing the cost and
The above calculations have shown that a 60 Tr boron and 40 9r Plexiglas fuel grain
should be able to provide the needed performance while also providing adequate material
properties for a caseless motor design. Of course, the latter will have to be substantiated
B. EXPERIMENTAL RESULTS
The initial test to determine the compatibility with the booster combustion product
gases was successful. One test firing was made and Figure 10 shows the chamber
pressure-time trace. Peak pressure reached approximately 550 psi and the total burn time
27
was about one second. Examination of the Plexiglas fuel grain after the test firing
showed that the structural integrity of the grain was maintained and very little ablation
of the Plexiglas occurred when exposed to the high temperature propellant combustion
products.
The next series of test firings was made to determine the chamber pressure
characteristics of the booster propellant grain and to determine the required sequence for
full transition to ramjet combustion. Two test firings were conducted. Figure 11 shows
the chamber pressure-time trace for one of the runs. The pressure-time trace showed that
the sliver of propellant, which was design to enhance ignition of the sustainer fuel grain
following the boost-phase, probably was consumed during booster tail-off. However,
visual study of the test firing with the aid of a video camera showed that the Plexiglas
grain remained very hot for several seconds after booster burnout. The results of the two
firings also showed that the reproducibility of the chamber pressure characteristics was
very good. The performance of the Plexiglas nozzle was as expected, with the nozzle
area increasing approximately 30 % during the booster operation. Thus, the final
sequencing of the port cover opening and related test stand activities could be made with
The full transition test firing was successful and the chamber pressure-time trace
results are shown in Figure 12. The transition between the boost-phase and the sustain-
phase occurred as anticipated. The initial bump in the chamber pressure during the
sustainer phase can be attributed to the sliver of boost propellant still burning and/or to
the rapid combustion of a hot, fluid layer of Plexiglas along the combustion chamber
28
surface formed during the boost-phase. The regressive ramjet chamber pressure
characteristic was due to the increasing exhaust nozzle throat area caused by the burning
of the Plexiglas nozzle. One very encouraging result was that the booster-sustainer
transition sequence was not critical. Booster chamber pressure completely decayed before
the air was introduced, and yet no difficulties were observed for ignition of the hot
Plexiglas grain surface. The integrity of the Plexiglas fuel grain and nozzle was
maintained throughout the run. Lack of time prevented additional test runs to be
conducted, but all indications seem to show that a high reproducibility of the results
would be expected.
29
CD
CD
LTD
C 2
CD
_ CD QJ
CD
CD
CD
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Figure 10. Chamber pressure-time trace for the caseless IRSFRJ feasibility test.
30
C5
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o
CD
00
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.
in
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Figure 11. Chamber pressure-time trace of the boost-phase of the IRSFRJ test
apparatus.
31
C=3
-r
CO
C )
CV?
O
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o
CO
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IT3
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Figure 12. Chamber pressure-time trace for the full transition test.
32
VI. CONCLUSIONS
The results of both the analytical study and the experimental investigation appeared
obtained. Obviously, more detailed design and testing are required to validate the
concept, especially concerning the structural capabilities of a caseless grain design which
must operate at high booster pressures. However, it appears that a small, low cost, solid-
fuel ramjet powered missile without ejecta can be designed and built which would provide
33
LIST OF REFERENCES
1. Myers, T. D., "Special Problems of Ramjet with Solid Fuel", AGARD Lecture Series
136, Ramjet and Ramrocket Propulsion Systems for Missiles, 1984.
2. Billing, Federick S., Tactical Missile Design Concepts, Vol. 4, Johns Hopkins APL
Technical Digest, November 3, 1983.
34
APPENDIX A - MISSILE DATA
TABLE 6
VARIABLE DEFINITIONS
CD Drag Coefficient
<s TT^I
<s
2 3a 3b 4a 4b 5 6
35
* * MISSILE
* l**i
SOLID FUEL RAMJET
* '
* RANGE OBJECTIVE= 2 *
MISSILE SELECTION CRITERIA IS MIN WEIGHT
MISSILE PARAMETERS:
WEIGHT= 76.9 LENGTH= 52 50 DIAMETER= 5.00 RANGE= 2 0.2 (NMI)
LAUNCH MACH= .3 LAUNCH ALT= 20000.0
CRUISE MACH=2 .3 CRUISE ALT= 20000.0
EOB VELOCITY=2 712.6 AVG. VELOCITY=2284.3
TAIL CHASE RANGE= 2 0.06 (NMI) MAX F-POLE=17.5(NMI)
MISSILE COMPONENTS:
PROPULSION:
BOOSTER
SUSTAINER PERFORMANCE
36
SUSTAIN DRAG COMPONENTS AT CRUISE MACH= 2.250
SREF= .1364(FT2)
TOTAL= .3540
INCLUDES 1.1 FACTOR FOR PROTUBERANCES ETC
,
37
* * MISSILE 2 * *
* >
* RANGE OBJECTIVE= 2 *
MISSILE SELECTION CRITERIA IS MIN WEIGHT
MISSILE PARAMETERS:
WEIGHT= 87.4 LENGTH= 6 3 21 DIAMETER= 5.00 RANGE= 2 0.2 (NMI)
LAUNCH MACH= .2 LAUNCH ALT= 100 00.0
CRUISE MACH=2.2 CRUISE ALT= 10000.0
EOB VELCCITY=2567 .2 AVG. VELOCITY=2 3 04.3
TAIL CHASE RANGE= 2 0.05(NMI) MAX F-POLE=18.3(NMI)
MISSILE COMPONENTS:
COMPONENT LENGTH (IN) WEIGHT(LBS)
PROPULSION:
BOOSTER
NOZZLELESS BURN TIME= 3.41
THRUST= 166 6. 8 (LBS) ATHROAT= 79(IN2).
SUSTAINER PERFORMANCE
38
SUSTAIN DRAG COMPONENTS AT CRUISE MACH= 2.200
SREF= .1364(FT2)
TOTAL CD= .3384
INCLUDES 1.1 FACTOR FOR PROTUBERANCES, ETC
39
* MISSILE 3 * * *
* *
SOLID FUEL RAMJET *
*
* RANGE OBJECTIVE= 12.0 *
MISSILE SELECTION CRITERIA IS MIN WEIGHT
MISSILE PARAMETERS:
WEIGHT= 81.5 LENGTH= 57.23 DIAMETER= 5.00 RANGE= 12.2(NMI)
LAUNCH MACH= .2 LAUNCH ALT= 2 000.0
CRUISE MACH=2.2 CRUISE ALT= 2000.0
EOB VELOCITY=2546.5 AVG. VELOCITY=22 83 .
MISSILE COMPONENTS:
COMPONENT LENGTH (IN) WEIGHT (LBS)
PROPULSION:
BOOSTER
NOZZLELESS BURN TIME= 3.24
THRUST= 1635. 5 (LBS) ATHROAT= .78(IN2)
ISP= 199.1(SEC) RANGE= .74 (NMI)
SUSTAINER PERFORMANCE
40
SUSTAIN DRAG COMPONENTS AT CRUISE MACH= 2.150
SREF= .1364(FT2)
TOTAL CD= .3357
INCLUDES 1.1 FACTOR FOR PROTUBERANCES ETC
,
41
* * MISSILE 4 * * *
*
SOLID FUEL RAMJET *
*
* RANGE OBJECTIVE= 2 0.0 *
MISSILE SELECTION CRITERIA IS MIN WEIGHT
MISSILE PARAMETERS:
WEIGHT= 77.2 LENGTH= 58.93 DIAMETER= 5.00 RANGE= 2 0.2(NMI)
LAUNCH MACH= .3 LAUNCH ALT= 2 0000.0
CRUISE MACH=2 .3 CRUISE ALT= 20000.0
EOB VELOCITY=26 7 6.5 AVG. VELOCITY=2 3 06 .8
TAIL CHASE RANGE= 2 0.05(NMI) MAX F-POLE=17.5(NMI)
MISSILE COMPONENTS:
PROPELLANT 24.0
FUEL 8.4
PROPULSION:
BOOSTER
NOZZLELESS BURN TIME= 3.2
THRUST= 157 8.6 (LBS) ATHROAT= 75(IN2)
.
SUSTAINER PERFORMANCE
42
SUSTAIN DRAG COMPONENTS AT CRUISE MACH= 2.300
SREF= .1364(FT2)
43
* * MISSILE 5 * * *
*
SOLID FUEL RAMJET *
*
* RANGE OBJECTIVE= 2 0.0 *
MISSILE SELECTION CRITERIA IS MIN WEIGHT
MISSILE PARAMETERS:
WEIGHT= 87.5 LENGTH= 74.13 DIAMETER= 5.00 RANGE= 2 0.2(NMI)
LAUNCH MACH= .3 LAUNCH ALT= 10000.0
CRUISE MACH=2.3 CRUISE ALT= 10000.0
EOB VELOCITY=2542.1 AVG. VELOCITY=2 391.8
TAIL CHASE RANGE= 2 0.04(NMI) MAX F-POLE=17.5(NMI)
MISSILE COMPONENTS:
COMPONENT LENGTH (IN) WEIGHT (LBS)
PROPULSION:
BOOSTER
NOZZLELESS BURN TIME= 3.2 6
THRUST= 1669. 7 (LBS) ATHROAT= 80(IN2)
.
SUSTAINER PERFORMANCE
44
SUSTAIN DRAG COMPONENTS AT CRUISE MACH= 2.300
SREF= .1364(FT2)
45
* * MISSILE 6 * * *
*
SOLID FUEL RAMJET *
*
* RANGE OBJECTIVE= 12.0 *
MISSILE SELECTION CRITERIA IS MIN WEIGHT
MISSILE PARAMETERS:
WEIGHT= 84.3 LENGTH= 67.55 DIAMETER^ 5.00 RANGE= 12.2(NMI)
LAUNCH MACH= .2 LAUNCH ALT= 2 00
CRUISE MACH=2.2 CRUISE ALT= 2000
EOB VELOCITY=2 517.6 AVG VELOCITY=2 308 .
MISSILE COMPONENTS:
COMPONENT LENGTH (IN) WEIGHT(LBS)
NONPROPULSION 15.0 22 5
PROPULSION ( 52.5) 61 8)
IRR COMBUSTOR + NOZZLE 50.0 11 9
INLET+AFT FAIRING ( 57.5) 5 2
MISCELLANEOUS 5
PLENUM 2.5 1 4
PROPELLANT 27 4
FUEL 10 9
PROPULSION
BOOSTER
NOZZLELESS BURN TIME= 3.33
THRUST= 1636.1 (LBS) ATHROAT= .78(IN2)
ISP= 199.1(SEC) RANGE= .75(NMI)
SUSTAINER PERFORMANCE
46
SUSTAIN DRAG COMPONENTS AT CRUISE MACH= 2.2 00
SREF= .1364(FT2)
TOTAL= .3364
INCLUDES 1.1 FACTOR FOR PROTUBERANCES ETC
,
47
APPENDIX B - PERFORMANCE CURVES
190.0
180.0
Oo
LL
h
CO i
1700
111
160.0
a Boron/HTPB
Boron/PMM
150.0 i l
r
48
140.0
130.0
C/)
^ 120.0
X
oS
jl^ 110.0
o
LU
CL
CO
100.0
90.0
FUEL-AIR RATIO
49
1900.0
1800.0
o
LJL^
LU ©
CO
LU
-J CO
HI -J
DD
U.Q-
LU
900.0
800.0
700.0
FUEL-AIR RATIO
50
INITIAL DISTRIBUTION LIST
51
Thesis
F89747 Fruge
c.l Design and testing of a
caseless solid-fuel
integral-rocket ramjet
engine for use in small
tactical missiles.
Thesis
F89747 Fruge
c.l Design and testing of
caseless solid-fuel
integral-rocket ramjet
engine for use in small
tactical missiles.