Starting Large Synchronous Motors in Weak Power Systems
Starting Large Synchronous Motors in Weak Power Systems
Abstract –Utility company standards for power quality are original circuits for the remaining in-service equipment and
making it difficult for industrial users to start large induction lighting.
and synchronous motors due to high inrush current. This
paper will present a large oil company’s challenges starting A. Utility Constraints
large motors driven by the utility company in a relatively
weak power system in East Texas while not violating the During Front End Engineering Design (FEED), it was
Utility company’s standards. A workable solution is an air discovered that the Utility had the following constraints for
cooled pulse width modulated (PWM) voltage source the proposed 138kV substation:
variable frequency drive (VFD) system designed to start
multiple large horsepower, medium voltage synchronous 1) Limited available short circuit current: Calculated
motors without any measurable voltage flicker. Various to be 7,459A three phase @138kV which would
combinations of motor design (induction vs. synchronous) & affect the large motor (8.1 kHP to 17.5 kHP)
starting methods are reviewed and final design schematic starting ability;
diagrams are documented. Challenges encountered during
the design & start-up are described and solutions with final 2) Strict voltage flicker requirements: Requested to
performance details are provided. limit voltage flicker (dimming of lights resulting
from voltage drops) to 1-1/2%. This rule limited
Index Terms — motor starting, weak power systems, the ability to start the large compressor motors
adjustable speed drive, variable frequency drive, variable without special starting methods;
speed drive, VFD, synchronous motor 3) Limited available transmission line capacity to the
facility: 63MW at 90% power factor (per the utility
I. INTRODUCTION contract) without a major rebuild of the existing
138 kV transmission lines. Note that the total plant
A large Oil and Gas Company undertook a major upgrade demand load is currently over 60 MW and rising @
of a 1940’s vintage gas plant in East Texas installing four 99% power factor.
15 kV electric driven centrifugal compressors ranging from
8,100 to 17,500 HP. The objective of the project was to In summary, the Utility did not have a “stiff” system but did
both increase the capacity of the plant and replace obsolete have very stringent flicker requirements. A “stiff” system is
& high maintenance large (over 5,000 HP) existing gas more immune to flicker during high current inrush when
engine driven compressors. Additionally, eight new 5kV starting large motors. The project had a significant
compressors were installed including all requisite 480V challenge to start the loaded compressor motors and
ancillary and lighting system loads. Electrical demand maintain power quality standards imposed by the Utility.
increased over fifteen fold from less than 4 MW to about 60
MW with over 65% of that total attributable to the four new II. ALTERNATIVES & FINAL DESIGN
15 kV centrifugal compressors. Lower anticipated life cycle
operating costs (investment vs. maintenance and up time) A. Motor Starting Alternatives Considered
pointed to electric in lieu of gas drivers for the new
compressors. It was desired to start the four compressors Multiple motor starting alternatives were considered to
loaded or in recycle to eliminate emissions associated with address the voltage flicker limits. Some options were
blowing down (unloading) the compressors. Compressor considered only in passing and others were investigated
speed turn down was not required for this installation. The more thoroughly as follows:
existing plant electrical distribution system was upgraded 1) Auxiliary Starting Motors (Diesel or electric): One
and expanded with a new 138 kV substation and all of the option considered was to install “pony” motors to
associated 15 kV, 5 kV, & 480V electrical infrastructure bring large motors up to partial speed before
(switchgear, MCC, cables, and tray). transferring to the normal bus. This option was
Upon project completion, there was essentially a new quickly discounted by inspection due to the
electrical distribution system retaining only a fraction of the excessive field equipment requirements,
02725.,/292/76
bypass scheme tested as that requires feed
back from a motor.
3) Drive Inrush: To reduce the 1200% power up
inrush current of the drive internal input &/26('75$16,7,21
transformer, a current limiting reactor with shorting
%<3$66
contactor was utilized to limit the inrush to 75% of
drive full load current rating.
9) VFD remains energized for 30 minutes during 2) Multiple differently sized motors with different
which time Step#s 1 & 2 are bypassed and the protection settings and multiplexed breaker
VFD is immediately available to start another controls.
motor by going to the Step# 3 breakers for the 3) Synchronous motor with associated individual
following motor (i.e. 52-B2 & 52-B3). excitation controllers.
10) There is only a marginal temperature rise in the 4) On line uncoupled test mode for confirming VFD
VFD building during this 4 minute starting availability.
sequence.
As a result, this starting system has been performing as
This VFD starting method completely eliminated any designed consistently starting up each motor without any
potential for voltage flicker. Additional benefits of this failed starts or need for electrician assistance.
starting system were complete elimination of all motor and
coupling stresses as well as motor heating concerns during V. ACKNOWLEDGEMENTS
starts; in fact, the Max Starts/Hour feature in the motor
protection relays for the four VFD started motors was turned Matt Colosino owner of Crescent Power Systems with
off. Compressors were started multiple times per hour locations based in New Orleans and Houston was
during the commissioning and startup period with no rotor instrumental in bringing parties together for a successful
heating concerns. implementation.
These advantages provided by VFD starting over other Takashi Morishita, Toshiaki Oka, Mike Daskalos and Mark
starting methods reduced the commissioning time on the Rayner with Toshiba International Corporation were key
compressors; no starting delays were required for cooling design engineers for the VFD system and exciter package.
time for the motors during the multiple shutdowns and
restarts that occurred during testing of the compressor
VI. REFERENCES
controls and surge protection. There was never any wait
time between starts required for the motor to cool down.
[1] Kurt Ledoux and Frank Haydock, “New Technology
A single/common starting VFD was the most cost effective Assists the Design of Outdoor Rated Medium Voltage
solution versus dedicated starting VFD’s. The cost for four Drives”Paper T-00 PCIC in Toronto September, 2010, pages
dedicated VFD’s, one per compressor, far outweighed the 1-3.
additional investment required in switchgear and controls.
The VFD was sized to about 60% (10,000 HP) of the largest [2] Bill Pelton and Kurt LeDoux, “Performance Testing of a
motor knowing that if it could start the largest 17.5 kHP Sine Wave ASD in Submersible Pumping Applications”
motor, all of the other compressors would definitely start. In presented at the Gulf Coast Section Electric Submersible
fact, selection of sizing was over conservative on the VFD Pump Workshop held in Houston, TX April, 2002, pages 4-
as the compressor models showed that only 25% (4,400 11.
HP) of the largest motor horsepower was needed to start
any compressor fully unloaded. The larger 10 kHP VFD VII. VITA
was selected in order to start some of the smaller methane
gas compressors partially loaded to minimize any venting. Kurt LeDoux graduated from DeVry Institute of
The largest compressor was for nitrogen for which venting Technology with a BSEET degree in 1978 and started his
is not a concern (air is 78% nitrogen). career with Reliance Electric as a Service Engineer on Drive
Systems. He moved to Toshiba in 1982 and has held various
IV. CONCLUSIONS drive related positions in manufacturing, service and repair,
engineering, and quality control. He has authored many
Starting large motors has always been a challenge for technical papers, most regarding voltage stress issues using
multiple reasons. There are more constraints for the design drives with long motor cables and step up transformers for
engineer than ever before: emissions requiring loaded the Society of Petroleum Engineers Electric Submersible
starts, limited utility capacity, and voltage flicker Pump Workshop. He is presently still at Toshiba working as
requirements. VFD technology is improving and is a viable Product Manager for Medium Voltage Drives.
alternative for the industrial user to mitigate the constraints
without reduction of motor life while allowing multiple
Paul W. Visser graduated from Texas A&M University in
1969 with separate BS degrees in both Electrical Engineering
and Nuclear Engineering. Upon graduation, he went to work
with Humble Oil & Refining Company (now ExxonMobil)
performing various electrical, controls, and even drilling &
workover engineering assignments onshore & offshore both
in the US and on loan to Saudi Aramco. He retired from
ExxonMobil and is now an independent Consulting Engineer.
He originally became a student member of IEEE in 1968 and
has been a Member of IEEE since 1986. Mr. Visser is a
registered professional engineer in the state of Texas.