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Bosch VP30 Troubleshooting

The document describes troubleshooting a Ford Mondeo that would not start or run. Measurements with an oscilloscope revealed that activating the fuel injection valve caused the voltage to the fuel pump ECM to drop, causing it to malfunction. Bypassing the wiring and relay supplying power to the ECM solved the problem, indicating a faulty connection was intermittently cutting power to the ECM.

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75% found this document useful (4 votes)
6K views8 pages

Bosch VP30 Troubleshooting

The document describes troubleshooting a Ford Mondeo that would not start or run. Measurements with an oscilloscope revealed that activating the fuel injection valve caused the voltage to the fuel pump ECM to drop, causing it to malfunction. Bypassing the wiring and relay supplying power to the ECM solved the problem, indicating a faulty connection was intermittently cutting power to the ECM.

Uploaded by

Jason Velasquez
Copyright
© © All Rights Reserved
We take content rights seriously. If you suspect this is your content, claim it here.
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Download as DOCX, PDF, TXT or read online on Scribd
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Introduction

In modern cars with sophisticated and complex components, troubleshooting requires powerful tools. Most signal
lines between components carry modulated signals, signals that (quickly) vary in amplitude to transfer information.
Checking the validity of these signals cannot be done using a voltmeter, but requires a good automotive diagnostic
oscilloscope, that will show how the signal actually looks like.

This article will show that using a lab scope was essential finding the cause of the problem with a Ford Mondeo 2.0
TDdi which would no longer run.

Problem description
The owner of the car got stranded during a trip abroad with a car that would no longer start or run. Fearing that
wrong fuel was tanked, the tank was emptied and the fuel system cleaned. The proper fuel was added but the engine
would still not start.

Since wrong fuel was used, damage to the fuel pump was suspected. The high pressure fuel pump was replaced, but
the engine still would not start. The garage kept on working in an attempt to solve the problem. In the end, the pump
was again replaced and even a new engine was installed in the car, but it still would not run.

Time to proper diagnose the problems in this car, using the right tools.

Background information
The 2.0 liter Duratorq Turbo Diesel direct injection engine in this car uses a Bosch VP30 axial-piston distributor
injection pump. This pump has its own Electronic Control Module (ECM), which is connected to the engine
management ECM by a CAN bus. When operating, fuel is compressed to a high pressure (up to 120 bar) and then
distributed to the cylinder(s) that require fuel. The high pressure of the fuel causes the injector to open and fuel is
injected in the cylinder. The pump has a special valve in the high pressure area. When it is closed (active state), the
pressure is allowed to build up. When it is open (inactive state), the pressure will drop, causing the injector to close
and the fuel to flow back to the input side. By activating the valve (closing the return) the moment of injection and
the amount of injected fuel (duration of the closed state) can be controlled. The moment of closing the valve and the
duration of the closed state are determined by two inputs:

 the exact position of the crankshaft, through a crankshaft position pulse generated by the engine management
ECM
 information on the required amount of injected fuel, sent via the CAN bus.

The pump has its own speed and position sensor (a Hall sensor) which signal is used as feedback of the injection
advance device to the engine ECM as well as signal when the engine is in "limb home mode" when the crankshaft
sensor is defective. Therefore, the connector of this pump has two terminals which carry a 12 V square wave signal.
Figure 1: VP30 distributor fuel injection pump

Measuring
The first thing to check is the fault code memory. It contained two errors:

 U1900 CAN Communication Bus Fault


 U0109 Lost communication with Fuel Pump Control Module

After clearing the error codes, the engine was cranked again, but it would still not start. The same error codes
immediately returned. The fuel pump control module receives information about the amount of fuel to inject and the
injection timing from the engine ECM by CAN bus, both are essential signals to let the engine run. Therefore these
errors are important and not to be ignored.

It was decided to measure the valve control signal (Ch1) and the crankshaft position signal (Ch2) on the pump, as
well as the CAN bus (Ch3 and Ch4) on the pump. The CAN bus contains a differential signal, to reduce the
influence of external disturbances. Ch3 measured the CAN-High signal and Ch3 measured the CAN-Low signal.
The CAN-Low signal is then subtracted from the CAN-high signal by an Add/Subtract I/O in the software, to get the
actual CAN signal. The three signals are shown in figure 2.
Figure 2: Missing pulses in the valve control signal

The valve is controlled using a active low signal. Each time the signal is pulled to 0 V, the valve is activated. When
the valve is deactivated again, the solenoid in the valve creates a high inductive peak in positive direction, which is
normal for this signal and can be ignored.

There is a repeating pattern visible of two valve activations and then some idle time. The engine has four cylinders
so one would expect a repeating pattern of four valve activations, there is something wrong in the valve activation
signal. It is also visible that after each second valve activation, a lot of activity is visible on the CAN bus. The
crankshaft position signal appears to be OK. Apparently something goes wrong when the valve is activated, causing
the pump ECM to stop function properly and losing CAN communication.

Timing issue?

Thinking that this might be caused by a timing issue, another measurement was performed. Ch1 was connected to
the valve control signal, Ch2 to the pump advance signal of the pump and Ch3 to the crankshaft signal of the engine.
The measured signals are shown in figure 3.
Figure 3: Pump advance signal fails after closing valve

It is clearly visible that the pump advance signal fails after each valve activation. This signal is generated in the
pump ECM. The fact that it fails after activating the valve, reinforces the idea that activating the valve causes the
pump ECM to malfunction, not a timing issue.

Checking the valve

The valve is activated by driving a current through a solenoid. When the valve control signal is pulled low, a current
starts flowing through the solenoid. This solenoid has a low resistance (0.2 to 0.3 Ohm), causing a high current to
flow. A problem may occur when the control signal is not pulled to zero properly, but in this situation the signal was
pulled low enough. Therefore, the power signal to the valve and the ground signal of the pump were measured.

Warning: Always use a lab scope when checking pulsating signals, never use a voltmeter. A voltmeter will show
an average value over time, which hides what is actually happening. An oscilloscope will show exactly what is
happening.
Figure 4: Valve power spikes when valve is activated

Figure 4 shows the measurement on the valve control signal (Ch1, top), the valve solenoid power (Ch2, middle) and
the pump ECM ground (Ch3, bottom). All were measured against the battery ground, to be able to detect voltage
losses.

When the valve is activated, the valve solenoid power drops significantly. This is barely visible due to the short
duration of the voltage drop. The pump ECM ground also shows a little spike, but that remains small.
Figure 5: Pump power drops when valve is activated

The measurement was repeated and this time the pump ECM power was measured instead of the valve solenoid
power. The pump ECM power showed the same voltage drop, indicating that this drop was caused outside the pump.
Zooming in on a single valve control pulse shows exactly what happens, see figure 5. When the current flows
through the valve solenoid, the ECM power drops shortly from 10 V to 5.28 V and at the same time the ground level
rises to 0.76 V. That leaves only 4.5 V to power the ECM. The ECM cannot operate on such a low voltage and stops
working. That explains why valve control pulses were missing and the CAN bus communication was lost.

Cause
There had to be a problem in the positive power to the pump ECM. According to the wiring diagram, the power to
the pump is controlled by a relay. A bad contact in this relay or the wiring to the relay had to cause the large voltage
drop. The wiring and the relay were bypassed by connecting a wire from the pump ECM power terminal directly to
the positive terminal of the battery. The engine started immediately and the signals looked a lot better now (see
figure 6).
Figure 6: Perfect situation with extra power wire

Solution
Now the relay and corresponding part of the harness was bypassed, the problem was gone, indicating that one of
them had a bad contact, causing the voltage drop that shut down the pump ECM. The garage was advised to check
and repair or replace the wiring harness and the relay.

Conclusion
Properly diagnosing a problem using the right tools can make a huge difference. This car probably never required a
new fuel pump and engine, just a new relay or a piece of wiring harness repaired. It would have saved a lot of time
and money.

If the pump power was measured using a multimeter, it would have indicated a voltage level of approximately 10 V,
which would not have alarmed anyone. However, by measuring the power using a good automotive oscilloscope
like the Automotive Test Scope ATS5004D, the short but significant power drops on the pump ECM power became
visible, leading to the cause of the problems in this car.
R. Metzelaar

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