0% found this document useful (0 votes)
82 views14 pages

1-Oct-20 Summary Downtime Detail Downtime Downtime % Waktu (Menit) Total Proses

The document summarizes downtime at a factory over two days. On the first day, the total downtime was 160 minutes or 100% of the time. The largest sources of downtime were preparation activities at 28% and issues with the bottom process at 38%. The second day saw 165 minutes or 100% of downtime. The largest sources on the second day were issues with the microperforation process at 18% and problems with both the preparation and bottom processes at 27%.

Uploaded by

Ade Ade
Copyright
© © All Rights Reserved
We take content rights seriously. If you suspect this is your content, claim it here.
Available Formats
Download as XLSX, PDF, TXT or read online on Scribd
0% found this document useful (0 votes)
82 views14 pages

1-Oct-20 Summary Downtime Detail Downtime Downtime % Waktu (Menit) Total Proses

The document summarizes downtime at a factory over two days. On the first day, the total downtime was 160 minutes or 100% of the time. The largest sources of downtime were preparation activities at 28% and issues with the bottom process at 38%. The second day saw 165 minutes or 100% of downtime. The largest sources on the second day were issues with the microperforation process at 18% and problems with both the preparation and bottom processes at 27%.

Uploaded by

Ade Ade
Copyright
© © All Rights Reserved
We take content rights seriously. If you suspect this is your content, claim it here.
Available Formats
Download as XLSX, PDF, TXT or read online on Scribd
You are on page 1/ 14

1-Oct-20

Summary Downtime Detail Downtime DOWNTIME


%
Waktu (Menit) TOTAL
Proses Bahan jelek
Setting Kantong
Persiapan 45 45 28%
Bahan telat
Printmark
UNWINDER 0 0%
MICROPERFORASI pembersihan/kalibrasi 30 30 19%
CUTTING trouble hole puncher
opener
perbaikan roll feeding 0 0%
belt putus/longgar
angin cutting kurang/mbulet
PREFOLDING bahan nyangkut di folding strip/grabber 0 0%
WING/OPENER wing patah/set oopening/ganti timng belt 25 25 16%
VALVE bahan miring/nyangkut/tidak lengket/press roll 0%
tidak motong
0
welding/preheating/rotary connection
belt putus/longgar
FORMING ukuran kantong tidak sesuai/kantong nyangkut 0 0%
COVER Press roll longgar/tidak lengket
welding/hidrolik
0 0%
bahan miring/nyangkut
belt putus/longgar/shaft aus/tidak motong
BOTTOM Press roll longgar
belt putus/longgar 15
welding 38%
60
ganti bearing 45
bahan miring/nyangkut
tidak motong/lengket
STACKER belt/pulley putus 0%
0
perbaikan sensor
Main machine stell belt lepas 0%
0
trouble rantai magnet
Listrik machine not referenced/servo drive 0%
0
heater/ssr
Spare part kosong bearing 0 0%

Total 160 100%

UNIT TOTAL DOWNTIME (menit) PROSENTASE


Proses 1726 41.6%
UNWINDER 0 0.0%
DOWNTIME MESIN STARKON HX

41.6%
MICROPERFORASI 30 DOWNTIME
0.7% MESIN STARKON HX
CUTTING 150 3.6%
PREFOLDING 15 41.6% 0.4%
WING/OPENER 135 3.3%
VALVE 245 5.9%

22.6%

10.9%
7.4%
5.9%
0.0% 3.6% 3.3% 0.0% 3.0% 0.0%
0.7% 0.4% 0.7%
es R SI NG G ER E
NG ER R ne tri
k g
os DE RA I IN N LV I V OM KE hi on
Pr IN O TT LD PE VA M CO TT AC ac Lis os
RF CU O O R
BO ST tk
NW PE EF G/ FO n
m
pa
r
U PR IN ai
RO W M ar
e
IC Sp
M
2-Oct-20
DOWNTIME
%
Waktu (Menit) TOTAL

45 45 27%

0 0%
0 0%

0 0%

0 0%
0 0%
30
18%
30

45 45 27%

45
45 27%

0%

0%

0%
0

0%
0

0%
0

0 0%

165 100%

RKON HX
RKON HX

22.6%

9%

0.0% 3.0% 0.0%


0.7% k
OM KE
R ne tri on
g
hi Lis os
TT AC ac
BO ST m rtk
n pa
ai e
M ar
Sp
1-Oct-20
Summary Downtime Detail Downtime DOWNTIME
%
Waktu (Menit) TOTAL
Proses Bahan jelek 30
Setting Kantong 45
persiapan 50 125 34%
Bahan telat
Printmark
UNWINDER 0 0%
MICROPERFORASI pembersihan 0 0%
CUTTING cutting fabrik tumpul
perbaikan plong
0 0%
folding
press roll longgar
Transport unit/opening perbaikan slider
perbaikan succer/stamp 60
pining stamp /magnet 120 180 49%
border wide
kantong miring/hand over
VALVE perbaikan vacum valve/preheating
ganti belt 0 0%
press roll valve/tidak motong/tidak lengket
FORMING ukuran kantong tidak sesuai/kantong nyangkut 0 0%
COVER vaccum/heater/tidak lengket 30
kalibrasi cutting
30 8%
press roll longgar
belt putus/longgar/mbulet
BOTTOM belt putus/longgar/mbulet
welding/tidak lengket 0 0%
vacumm
STACKER belt putus /nyangkut 0 0%
Main machine stell belt lepas 30 30 8%
Listrik motor pompa rusak/mesin macet/sensor trouble 0 0%
Spare part kosong 0 0%
Pneumatic Trouble selenoid
0 0%
Trouble air pressure
Total 365 100%

UNIT TOTAL DOWNTIME (menit) PROSENTASE


Proses 10220 72.0% DOWNTIME STRAKON 60
UNWINDER 0 0.0%
MICROPERFORASI 0 0.0% 72.0%
CUTTING 55 0.4%
Transport unit/opening 1755 12.4%
72.0%

VALVE 350 2.5%

12.4%
0.0% 0.0% 4.9% 0.0% 0.0% 0.0%
2.5% 1.9% 2.1% 3.6%
I 0.4% 0.3% c
es ER AS G in
g
LV
E G ER M
KE
R ne tri
k
on
g
ati
os ND
IN en IN V TO hi Lis
Pr I OR TT op VA RM CO T AC ac os um
W RF CU BO ST m tk e
UN PE it/ FO n pa
r Pn
un ai
CRO rt M ar
e
I po Sp
M s
an
Tr
2-Oct-20
DOWNTIME
%
Waktu (Menit) TOTAL

20 20 4%

0 0%
0 0%

0 0%

450 450 85%

0 0%

0 0%
60

60 11%

0 0%

0 0%
0 0%
0 0%
0 0%

0 0%

530 100%

DOWNTIME STRAKON 60

2.0%
2.0%

12.4%
0.0% 0.0% 4.9% 0.0% 0.0% 0.0%
2.5% 1.9% 2.1% 3.6%
I 0.4% 0.3% c
es ER AS G in
g
LV
E G ER M
KE
R ne tri
k
on
g
ati
ND
IN en IN V TO hi Lis
I OR TT op VA RM CO T AC ac os um
W RF CU BO ST m tk e
UN PE it/ FO n pa
r Pn
un ai
CRO rt M ar
e
I po Sp
M s
an
Tr
RESUME TROUBLE MESIN STARKON HX
BULAN 1-30 Sept 2020
NO PROBLEM
Bahan jelek
Setting Kantong
1 Proses
Persiapan
Bahan telat
trouble hole puncher
2 Unit cutting fabric opener
` perbaikan roll feeding
3 Unit prefolding bahan nyangkut di folding strip

4 microperforasi kotor dan kalibrasi ulang


5 unit opening wing patah/set oopening/ganti timng belt
bahan miring/nyangkut/tidak lengket
6 Unit valve tidak motong
belt putus/longgar
7 forming ukuran kantong tidak sesuai/kantong nyangkut

Press roll longgar


welding
8 Unit Cover
bahan miring/nyangkut
belt putus/longgar/shaft aus
Press roll longgar
belt putus/longgar
9 Unit Bottom
welding
bahan miring/nyangkut
stell belt lepas
10 Unit main machine

11 Listrik machine not referenced/servo drive fault


DAMPAK PROSENTASE

-Produksi tidak lancar/mesin sering berhenti 41.6%

3.6%
-cutting fabrik macet
-kantong nyangkut/mesin stop 0.4%

-AP kantong tidak sesuai spek 0.7%


-kantong tidak membuka 3.3%
-mesin stop
-kantong tidak sesuai spek 5.9%
-valve tidak lengket/nyangkut
-kantong tidak sesuai spesifikasi
7.4%

-cover idak lengket/nyangkut


10.9%
-cover patch miring

-bottom tidak lengket/nyangkut


-bottom patch miring
22.6%

-mesin stop 3.0%

-mesin tidak bisa start 0.7%


PERBAIKAN

-Perbaikan proses produksi dari unit sebelumnya (loom, laminasi & printing)

-setting regulator
-setting hole puncher
-setting roll feeding

-pembersihan bahan/setting folding strip

-pembersihan dan kalibrasi ulang


-penggantian wing
-setting ulang parameter welding
-kalibrasi cutting
-penggantian flat belt
-setting
-setting cutting & titik hisap
ulang forming

-penggantian/setting press roll


-setting cutting & titik hisap
-penggnatian flat belt

-penggantian/setting press roll


-setting cutting & titik hisap
-penggnatian flat belt

-perbaikan steel belt


-perbaikan pendingin kabinet, pembersihan servo dan inverter
-setting mechanical yang longgar
-pelumasan mesin
RESUME TROUBLE MESIN STARKON 60
BULAN 1-30 Sept 2020
NO PROBLEM
Bahan jelek
Setting Kantong
1 Proses persiapan
Bahan telat
Printmark
folding
2 Unit cutting fabric

3 Unit microperforasi kotor dan kalibrasi ulang


perbaikan slider
perbaikan succer/stamp
4 unit transport/opening pining stamp /magnet
border wide
kantong miring/hand over
perbaikan vacum valve
press roll valve/tidak motong
5 Unit valve

ukuran kantong tidak sesuai/kantong nyangkut


6 forming

vaccum/heater/tidak lengket
kalibrasi cutting
7 Unit cover
press roll longgar

belt putus/longgar/mbulet
8 Unit Bottom
welding/tidak lengket
trouble air pressure
9 Unit pneumatic

stell belt lepas


10
Unit main machine
DAMPAK PROSENTASE

-Produksi tidak lancar/mesin sering berhenti 72.02%

-mesin berhenti/fabrik nyangkut 0.39%

-AP kantong tidak sesuai spek 0.0%

-mesin sering handover/berhenti 12.37%

-valve tidak lengket


2.47%
-mesin stop

0.32%
-kantong tidak sesuai spesifikasi

4.86%
- cover tidak motong
-cover tidak lengket

-bottom tidak lengket 1.94%

-mesin stop/ suhu welding turun


3.56%

2.1%
-mesin stop
PERBAIKAN

-Perbaikan proses produksi dari unit sebelumnya (loom,


laminasi & printing)

-Perbaikan folding

-pembersihan dan kalibrasi ulang

-setting ulang posisi slider


-perbaikan lubricator
-penggantian succer yang rusak
-pembersihan selenoid valve
-setting ulang rantai magnet & puffer
-perbaikan pin magnet
-Perbaikan titik hisap
-penggantian press roll
-perbaikan posisi press roll

-setting ulang forming

-Perbaikan posisi titik hisap


-setting press roll
-kalibrasi cutting

-Penggantian belt
-perbaikan posisi titik hisap
-setting press roll
-pembersihan & penggantian air filter regulator

-pengencangan stell belt

You might also like