Aeroderivative Gas Turbine Analysis and Test
Aeroderivative Gas Turbine Analysis and Test
The staff of Mechanical Solutions, Inc. has background and experience in the
analysis and testing of aeroderivative gas turbines, such as the popular FT-4,
LM2500, and LM6000 PC units. One of MSI’s principals was one of the design
analysis team-members for the original ground-based and marine-based
conversions of the FT-4. Generally, problems with these units are installation or
system related. MSI’s ability to separate and evaluate rotordynamic, casing, and
support structure effects allows such problems as well as any warranty issues to
be quickly identified, such that responsibilities can be determined, and appropriate
fixes can be developed and implemented.
In a new power plant overseas, two newly installed aeroderivative gas turbine/
generator sets were experiencing sudden and dramatic increases in vibration level
over certain operating torque ranges. Blame was at first fixed on the engine
rotordynamics. MSI performed impulse excitation of the operating engine casing
and rotor, using its time-averaged pulse (TAP ) technique. Forward and backward
TM
critical speeds of the rotor were determined, along with rotor modal damping. It
was clearly shown that rotordynamics was not the issue. Very detailed
experimental modal analysis (EMA) was then performed on the engine casing,
engine supports, I-beam support structure, and turbine bay foundation. Complex
mode shapes were constructed and animated, and modal damping was
determined, for all natural frequencies in the running speed range. In addition,
operating deflection shapes (ODS) of vibration amplitude and phase were
produced based on measurements at many casing and support locations.
This was repeated for various torque conditions, including both problem and non-
problem conditions. EMA and ODS animations were compared, allowing the
identification of excitation force locations and system nonlinearities. Situations
were identified in which the support structure was behaving much more flexibly
than it was designed to. Strain gages on support struts were used to verify these
conclusions. A fix was designed by MSI to fundamentally and completely cure the
problem, on a permanent basis at all operating conditions.
A major petrochemical company had a serious gear box failure problem in some
service water pumps, driven at variable speed by a steam turbine though a right
angle 1:1 gear box and hollow drive shafting. Many experts from the pump, turbine,
and gear manufacturers had attempted without success to understand and cure
the problem over a 3 year period. Replacement of the gear boxes with some built
to more stringent standards had no effect. External consultants, using test or
analysis also had failed to solve the problem. Analysis by Msi engineers of
torsional and lateral rotor and structural frequencies confirmed earlier consultant
findings that the design should be sound in this regard. Torsional modal testing,
using testing techniques that could be applied while the pump/gear/turbine
operated, found that all rotor
system natural frequencies
were close to their predicted
values, and with even more
damping than
predicted.However, impact
modal testing on the hollow drive shaft showed that it had a "bell-mode" at the gear
meshing frequency, where the hollow shaft ovalized with very little damping,
causing the shaft length to change through the "poisson effect". The driving force
was shown by the test to be the combined torsional and axial load from the
bull/pinion gear meshing. The drive shaft was filled with grease to damp out this
unusual vibration. The gear box noise immediate fell a factor of five, and all gear
box problems ceased.
Following a lengthy period of service, the LP stages of a nuclear plant boiler feed
pump turbine were found to have suffered erosion damage. A mechanical redesign
of those stages was undertaken by Msi engineers. Analytical modal analysis found
the first several natural frequencies for each stator blade. A possible vibration
problem in one redesigned turbine blade was discovered, and was avoided by
shortening the blade chord. The casing stresses were also investigated, and the
alteration in stress field was determined due to modification of the inner casing.
Both the casing and stator blade stress analyses were performed for worst case
pressure and transient thermal loading. The stator blade vibration and stress
analyses and casing stress analysis predicted that all aspects of the redesigned LP
turbine components should perform satisfactorily in terms of structural and
reliability characteristics.