Advanced Process Control of PDF
Advanced Process Control of PDF
research-article2015
MAC0010.1177/0020294015571498Advanced Process Control of an Ethylene Cracking FurnaceAdvanced Process Control of an Ethylene Cracking Furnace
Themed Paper
Ping Li
School of Information and Control Engineering, Liaoning Shihua University, Fushun, China
[email protected]
Tian Li
School of Information and Control Engineering, Liaoning Shihua University, Fushun, China
Jiangtao Cao
School of Information and Control Engineering, Liaoning Shihua University, Fushun, China
The ethylene production plant is one of the most important units in petrochemical industry, and the ethylene cracking
furnace is the heart of the plant. The ethylene cracking furnace is a multivariable, strong coupling, and nonlinear pro-
cess, and therefore, it is difficult to be manipulated by traditional proportional–integral–derivative controls. This paper
reports a real application of advanced process control in five 470-kton/year SC-I tubular reactors. The advanced pro-
cess control deployed includes cracking outlet temperature control and feed volume control. This control system has
been operating since 2012. The variation of cracking outlet temperature has been reduced from ±5 to ±1 °C with a
setting time less than a few minutes even under a large-scale disturbance. The variation of feed volume has been
controlled within ±1%. As a result, the advanced process control system has achieved a total production increase by
0.3%.
transmitter
Figure 3. Total feed volume control and temperature balance control
ƸF1
Set point
ƸF2 Temperature
Increase/ ƸF3 balance
ƸF4
drop control
Total feed volume ƸF5 (Constrain condition:
flow control ƸF6 ěƸFi=0, Fimin≤Fi≤Fimaxˈ
ƸF7 ƸFimin≤ƸFi≤ƸFimax )
ƸF8
FC8 TI8
FC7 TI7
FC6 TI6
FC5 TI5
FC3 TI3
FC2 TI2
FC1 TI1
increase or drop volume control will designed by Zhejiang Supcon and eight inlet flow PI controllers FCi (i = 1, 2,
re-distribute the volume among the eight implemented in an industrial upper …, 8) shown in Figure 3 are
inlet pipes by re-setting their set-points. computer which sits over and is implemented in the DeltaV DCS.
connected with a DeltaV Distributed Ethylene cracking furnace’s actuators
Control System (DCS) in the form of and different measurement instruments
IV. System Implementation
OPC standard. All the conventional are connected through the cable to
The APC system is developed at the controllers such as the fuel gas pressure the DeltaV DCS with an OPC server,
platform of ESP-/SYS-A software PI controller shown in Figure 2 and the designed by Emerson. Figure 4
Figure 4. APC implementation Figure 5. Comparison results before and after APC system commissioning: (a) APC off and (b) APC
on
Upper Computer (ESP-/SYS-A)
Control Network
V. Application Results
The designed APC system has been
operating since 2012 in five 470-kton/year
SC-I ethylene cracking tubular furnaces in
a Chinese petrochemical company in the
northwest region. Before the APC system
was in operation, every conventional
controller for the ethylene cracking
furnace had to be judged individually from
experience of the operation. The following aims of prolonging life of the cracking improves the stability of the production
of the change in the operation was very furnace and extending interval cycle of process by reducing the fluctuation of the
slow, and the fluctuation of the COT and decoking. COT. We have to consider the optimal
the total feed volume was large. After the temperature profile along the tubular
APC is in operation, the operation of the reactor in the near future to further
VI. Conclusion improve the production efficiency.
system becomes easier and less
intensive. The change of COT before and This paper reports the design and
Funding
after the introduction of the COT control is application results of an APC system for
This research was supported by the project
shown in Figure 5. It is evident that the ethylene cracking furnace. The APC
of National Natural Science Foundation of
disparity of the average COT is reduced. consists of the COT control and the China (61203021) and National Natural
The fluctuation of the average COT has temperature balance control and total Science Foundation of Liaoning Province
been decreased from ±5 to ±1 °C. When feed volume control. The APC system is (2013020024).
a large disturbance occurs, temperature’s implemented in an industrial upper
fluctuation declines from ±10 to ±1 °C. computer sitting over the ordinary DCS. References
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production rate is increased by 0.3%. designed APC system meets the advanced process control system for ethylene
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