5 9 Ravichandran Slides PDF
5 9 Ravichandran Slides PDF
Process Evolution
through
- A Case Study in
Alternator Manufacturing
by
Dr N Ravichandran
Chief Executive Officer
Lucas-TVS
Lucas TVS Ltd
Padi, Chennai 600 050, India
Dr. N. Ravichandran
Lucas-TVS Ltd
Contents
1.0 Overview of Lucas-TVS
2.0 Introduction about Alternator
3.0 Problem definition
4.0 Diagnostic approach – Shainin Method
50
5.0 Root Cause - Validation
6.0 Improvement approach – Taguchi Method
7.0 Result Validation
80
8.0 Standardisation
9.0 Conclusion
10.0 Overview of Shainin Tools
Dr. N. Ravichandran
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Lucas-TVS Ltd
1 0 Overview
1.0 O e ie of Lucas
L cas - TVS
Dr. N. Ravichandran
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Lucas-TVS Ltd
Dr. N. Ravichandran
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Lucas-TVS Ltd
Dr. N. Ravichandran
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Lucas-TVS Ltd
Annual Units
Products
((In Lacs))
Alternators 25.30
Starters 33.90
Wipers 22.10
Dr. N. Ravichandran
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Lucas-TVS Ltd
Dr. N. Ravichandran
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Lucas-TVS Ltd
Dr. N. Ravichandran
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Lucas-TVS Ltd
1.4 Recognitions
g & Awards
TS 16949 OHSAS 18001 ISO 14001 Deming Award
Dr. N. Ravichandran
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Lucas-TVS Ltd
Case Study -
Dr. N. Ravichandran
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Lucas-TVS Ltd
Dr. N. Ravichandran
Lucas-TVS Ltd
30 P
3.0 Problem
bl Definition
D fi iti
Dr. N. Ravichandran
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Lucas-TVS Ltd
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Rej no
60
15
Cum
40
10
88% of rejection 5 28 1 1 1 1 20
due to 0 0
Initial Cut
C t in Failure
Fail e Initial cut in WL Not on Mild glow Bind Pulley
Damage
Dr. N. Ravichandran
Lucas-TVS Ltd
Dr. N. Ravichandran
Lucas-TVS Ltd
Dr. N. Ravichandran
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Lucas-TVS Ltd
R
Rotor wire
i cut Positive diode shorting
Carbon brush broken
Slip ring burr
Regulator A terminal damaged
Lucas-TVS Ltd
Si
Since Pil
Pilott R
Run - all
ll the
th parts
t have
h been
b checked
h k d for
f conformance
f prior
i tot assembly.
bl
Hence, to cut short time & effort Shainin Approach is Preferred
Dr. N. Ravichandran
Lucas-TVS Ltd
¾ First phase of Elimination – Identify Assembly Process If D/d Ratio < 1.25
which is contributing OR
Using D/d Ratio by disassembling &
reassembling Twice - BOB / WOW
Constituent Parts If D/d Ratio > 1.25
Lucas-TVS Ltd
BOB WOW
WL Current O/P WL Current O/P
Initial assembly 0 31
0.31 0 08
0.08
After 1st re-assembly 0.39 0.06
Specification of
After 2nd re-assembly 0.28 0.05 WL current O/P
Median 0.33 0.065 > 0.12 amps
Range 0.11 0.03
D / d Test:
Difference between the medians (D): 0.33 – 0.065 = 0.265
Average range (d) : (0.11+0.03) / 2 = 0.07
1. Rotor assemblyy
2. Regulator Rectifier Assembly
3. Stator Assembly
Dr. N. Ravichandran
Lucas-TVS Ltd
First
1 0.32 0.06
Reaaseembly
Second
2 0 28
0.28 0 05
0.05 Hence Stator
reassembly
ROTOR is the Culprit
3 0.23 0.06 RED X
INTERCHANGE
Bring back to
4 0.25 0.05
original
RECTIFIER &
5 0.29 0.08
REGULATOR
Bring back to Inference:
6 0.32 0.06
original
Total Reversal
7 STATOR ASSY 0.06 0.32
when Stator is
Bring back to Interchanged
8 0.3 0.07
original
9 Capping Run 0.07 0.31
Dr. N. Ravichandran
Lucas-TVS Ltd
Lucas-TVS Ltd
Stator
Stator Stator Stator
S.No. Basket ID ovality
Basket ID Overhang ID
OD Features Compared
G1 119.10 99.2 15.24 95.39 0.07
G2 119.20 99.16 15.35 95.37 0.06
G3 118.95 99.17 15.39 95.38 0.065
G4 119.18 99.21 15.49 95.37 0.055
G5 119.14 99.36 15.65 95.39 0.06
G6 118.98 99.24 15.47 95.38 0.065
B1 118.93 99.14 15.45 95.44 0.05
B2 118.99 99.2 15.33 95.43 0.065
B3 119.1 99.18 15.21 95.44 0.06
B4 119.13 99.32 15.31 95.43 0.07
B5 119.17 99.22 15.27 95.425 0.065
B6 119 08
119.08 99 29
99.29 15 55
15.55 95 44
95.44 0 065
0.065
Dr. N. Ravichandran
Lucas-TVS Ltd
Inference:
¾ Stator ID is the only feature contributing significant @ 99.7 % confidence
¾ If the ID of the stator core is near to the top limit of the speciation – the defect occurs
ID Spec: 95.33 to 95.44 mm dia
Dr. N. Ravichandran
Lucas-TVS Ltd
Six presumed Assembled the significant part conforming to (WOW) Bad unit
Bad units With values
l & other
th partst random
d
Six p
presumed Assembled the significant part conforming to (BOB) Good unit
Good units With values & other parts random
Dr. N. Ravichandran
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Lucas-TVS Ltd
er
with Current ( C ) and 6 n
C5 95 44
95.44 NOT OK B2 95.39
95 39 OK
6 / 6 OK
6 / 6 NOT
B6 95 37
95.37 OK C6 95 435
95.435 NOT OK
Inference: If the ID of the stator core is near to the top limit of the speciation – the defect
occurs – this is validated.
validated
Cp
p = 1.44 Cpk
p = 1.25
Root Cause:
• Stators having ID near to the design target are Good.
• Whereas ID near to the top limit but still within specification are leading to defect
• And Stator ID p
population
p spreads
p up
p to the top
p limit of the specification
p
Dr. N. Ravichandran
Lucas-TVS Ltd
Dr. N. Ravichandran
30
Lucas-TVS Ltd
Die Cushion
pressure
Component loading Ram down During Dwell time Ram up
Lucas-TVS Ltd
6 7 D D E
6 7
STANDARD LINEAR GRAPH MODIFIED LINEAR GRAPH
A B C D E
Factors Ram Pr Dwell time 1*2 Hardness 1*4 Die cushion Initial p
pack
Column No. 1 2 3 4 5 6 7
Exp 1 1 1 1 1 1 1 1
Exp 2 1 1 1 2 2 2 2
E
Exp 3 1 2 2 1 1 2 2
Exp 4 1 2 2 2 2 1 1
Exp 5 2 1 2 1 2 1 2
Exp 6 2 1 2 2 1 2 1
Exp 7 2 2 1 1 2 2 1
Exp 8 2 2 1 2 1 1 2
Dr. N. Ravichandran
Lucas-TVS Ltd
Stator ID ID Ovality
cusion
Dwell time
dness
m Pr
(mm) (mm)
1**2
1**4
Ram
Hard
Die c
95 33 - 95
95.33 95.44
44 01M
0.1 Max
Replication Replication
Col mn
Column 1 2 3 4 5 6 7 A B A B
Exp 7 2 2 1 1 2 2 1 95.39
95 39 95.38
95 38 0.04
0 04 0.045
0 045 Burr noticed
Exp 8 2 2 1 2 1 1 2 95.33 95.34 0.04 0.04
Dr. N. Ravichandran
Lucas-TVS Ltd
Lucas-TVS Ltd
95 36
95.36 ¾ From the Response
p graph
g p the optimum
p level of the significant
g factor is
95 26
95.26
chosen
Dwell time
7 0 Result Validation
7.0
Dr. N. Ravichandran
37
Lucas-TVS Ltd
Cp Cpk
Before 1.44 1.25
After 2.02 1.75
Inference:
The selected Optimum levels have yielded the desired reduction in variation
Dr. N. Ravichandran
Lucas-TVS Ltd
Lucas-TVS Ltd
8 0 Standardisation
8.0
Dr. N. Ravichandran
40
Lucas-TVS Ltd
Dr. N. Ravichandran
Lucas-TVS Ltd
9 0 Conclusion
9.0
Dr. N. Ravichandran
42
Lucas-TVS Ltd
¾ Initial Production trial run of a new product – yielded low first pass yield.
¾ Major contribution of defect being from Initial Cut in Failure – Warning Lamp Not Off
¾ Cause & effect diagram indicated contribution from both process as well as parts
parts.
¾ Shainin Clue Generating Experiments conducted - to quickly funnel down to the culprit
¾ Variation from the design target of Stator ID is identified as the root cause
Dr. N. Ravichandran
Lucas-TVS Ltd
EOQ 2011
¾ A new product with new performance standards – demands new process standards.
¾ Shainin clue Generating tools – enhances the process of identifying the unknown cause
¾ Shainin Tools generates clue from the available product & process
¾ Taguchi OA enhances the optimization process once the unknown cause is identified
Future Study :
¾ Taguchi Parameter designed experiment is to be conducted – to make the process more robust
– irrespective of variation in noise factors.
¾ A study
t d for
f iintegrating
t ti various
i problem
bl solving
l i tools
t l are required.
i d
Dr. N. Ravichandran
Lucas-TVS Ltd
Dr. N. Ravichandran
45
Lucas-TVS Ltd
FACTS FROM
ENGINEERS’
PRODUCT / C bi d with
Combined ith D t t
Detect SOLUTION
PROCESS KNOWLEDGE
Dr. N. Ravichandran
Lucas-TVS Ltd
COMPONENT
MULTI - VARI SEARCH
TO FILTER CYCLICAL ; TO FILTER PRODUCT PARAMETERS WHEN
POSITIONAL & TEMPORAL COMPONENTS ARE INTERCHANGEABLE
VARIATION
PAIRED
COMPARISON
TO FILTER PRODUCT
PARAMETERS
CONCENTRATION PRODUCT
CHART PROCESS SEARCH
TO FILTER VARIATION TO FILTER PROCESS
WITHIN UNIT PARAMETERS
Dr. N. Ravichandran
WHEN VARIABLES ARE UNKNOWN & MANY
Lucas-TVS Ltd
VARIABLES
SEARCH FULL FACTORIAL
B vs C
TEST
ONE VARIABLE
B vs C
TEST
Dr. N. Ravichandran
Lucas-TVS Ltd
RSM
SCATTER PLOTS RESPONSE SURFACE
METHODOLOGY
WITH NO INTERACTION OF WITH INTERACTION OF
FACTORS FACTORS
Dr. N. Ravichandran
Lucas-TVS Ltd
Dr. N. Ravichandran