Process Control
Process Control
Abstract: This paper describes the digester chip level control problem and shows a MPC system
implementation for the level control.
The objective with implemented chip level control system is to stabilize the transport conditions
in the bottom of the digester by using the chip feed and not the blow flow as the primary manip-
ulated variable. The results indicate a smoother digester operation and a reduction of the kappa
number variations compared with the original control system.
were used to deal with extreme level con- Chip feed rate and fibre discharge rate as consistency control were described.
ditions. No primary control of the blow MV Discussions with operating personnel
line consistency was presented. The Fuchs et al. [13] used the chip metering indicate that large blow flow manipula-
results showed a decrease in chip and speed as the primary manipulated vari- tions could disturb the chip column
black liquor flow variations to the digester able for the chip level control. They point- movement and change the mass and ener-
by manipulating blow flow compared to ed out that it is important to have a stable gy balances. The results showed a
the original control system. According to fibre discharge rate in order to stabilize decrease of 50 % in blow flow manipula-
Belanger et al. [9] this control system was the residence time in the cooking zones tions, but the expected improvements in
abandoned because of bad reliability of of the digester. The manipulations of the pulp quality were not achieved (a slight
the STR, but Belanger mentioned noth- blow flow were minimized, but a very slow increase in kappa variations). The MIMO
ing about any problems with the selected feed-forward signal was added to the fibre GPC controller was disabled after six
control strategy. discharge target (blow flow target) based month of operation. According to Allison
Belanger et. al. [9] made a comparison on the difference between the nominal et al. [6] the bad chip level measurement
between using the blow flow and the production and the actual production i.e. (strain gauge measurement) and the fact
digester bottom scraper as the primary the chip meter speed. Manipulating the that the mill had been experimenting
manipulated variable for the chip level digester bottom scraper, with some cor- with a number of new grades were con-
control (using a STR control structure). rection of the bottom dilution flow when tributing factors to why the GPC was
The two alternatives showed similar the scraper speed was at its limits, primar- switched off.
results regarding top separator amperage ily controlled the blow line consistency. Lundqvist [10] presents a chip level
(level measurement) variations but the No specific results were shown regarding control strategy that utilizes both the chip
digester bottom scraper (outlet device) the level control performance. meter speed and the blow flow as manip-
was selected because of different practical Al-Shaikh et al. [11] presented a control ulated variables depending on the size of
reasons. The operators also preferred the strategy where the chip meter speed was the chip density variations. At small chip
bottom scraper as the primary MV used as the primary manipulated variable density and wood property variations, the
because of the more steady blow flow. for short-term level variations, and the chip meter is used as primary MV and the
Controlling dilution flow, where the set blow flow ratio, for long term variations. blow flow is kept constant. If the chip den-
point was ratioed to the scraper set point, The chip meter speed sets the production sity varies considerably, the blow flow is
aimed to stabilize the blow flow consisten- target, with a limited bias added for the used as MV and the chip meter is kept
cy. The dilution controller output was level control. When the accumulated constant. The tuning of the mix of the two
slowly changing the blow flow set point. error for the chip meter speed (from the MVs should be done regarding the chip
The STR controller increased the stability nominal production speed) exceeds a level response characteristics and with the
of the production. certain limit the blow flow ratio target is kappa number chosen as the control per-
Allison et al. [7] designed an adaptive adjusted to maintain target production. formance criterion.
controller based on a generalized predic- The blow line constistency was not direct- Amirthalingam et al. [2,3] discussed
tive control structure (GPC). The blow ly controlled. how chip level control relates to pulp
flow was used as the primary manipulated Allison et al. [6] used both the chip quality parameters such as the kappa
variable. No clear motive was presented meter speed and the blow flow as manip- number. They proposed that the manipu-
regarding why the blow flow was selected. ulated variables. The chip meter and the lated variable for the chip level control
The blow flow set point is set by the GPC blow flow simultaneously reacted to level should be selected according to the origin
together with the production feed forward disturbances, but with the chip meter of the disturbance, e.g. if a change in the
signal and a proportional feedback signal slowly returning to steady state produc- digester chip level is caused by a change
from the digester top separator current. tion rate and with blow flow to compen- in chip bulk density, the right action
No primary control of the blow line con- sate for the persistent load disturbance. would be to change the chip metering
sistency was presented. The adaptive con- The GPC was set to constrain the chip speed. However if a disturbance in the
troller showed improvement of the chip meter speed about the production target chip level were caused by a change in the
level control by means of a closer mean speed. The motive for the use of the chip fibre discharge rate (change in blow line
value to level target and a reduction of the meter was to reduce blow flow manipula- pulp consistency), the right action would
standard deviation of the chip level signal. tions. No specifications about blow line be to change the blow flow (or digester
FIG. 2. Digester chip level control system. FIG. 3. MPC controller structure.
FIG. 4. Step response for the differential pressure. FIG. 5. Step response for digester level.
The impregnation vessel chip level is also which is used for the output predictions in the matrix contains the dynamic model
set up as a constraint variable with an and to relate the MVs to the CVs. The that relates the MVs with CVs and CTs.
upper and lower limit. If a violation of data used for the modelling and design The prediction horizon for the MPC con-
these limits is detected, the bottom scrap- has been generated by step response troller was set to 50 minutes (100 control
er will react powerfully, together with the experiments. The possibilities of using intervals). The prediction horizon for the
dilution flow, to bring the level within the more sophisticated data generation tools level constraint variables was set to 30 and
limits again. When the level is within the like PRBS signals were limited. Figures 4 20 minutes to make that control function
limits, the scraper speed is slowly brought through 6 show the step responses for the less restrictive. The MPC algorithms are
back to a target speed to move more of chip levels and the differential pressure. described in Maciejowski [1].
the average control action onto the dilu- The step response figures show that
tion flow (FC5.2). The impregnation ves- the digester and impregnation vessel level RESULTS AND DISCUSSION
sel scraper speed is both a manipulated process can be characterized as an inte- The MPC controller has been running
variable and a control variable in the MPC grator process with a time delay at the since start-up in mid December 2003. The
controller, Table II. input. The time delay is, however, longer back up level control system in the
The constraint variable can be seen, in than physically expected. That could be Siemens DCS system was installed in
this case, as a safety function to prevent explained by the time it takes to acceler- August 2003 and was running until the
plugging of the impregnation vessel. That ate the chip column in the impregnation MPC controller was installed. The original
allows a smoother control action for the vessel and the compaction of the chip col- digester level control system, with the blow
set-point control. It is not very critical to umn in the digester due to chip column flow as the primary manipulated variable,
have a tight level control of the impreg- elasticity [8]. The chip column elasticity is still available for the operators but has
nation vessel, and that also gives the pos- can possibly be modelled as a second not been in operation since the start-up of
sibility of using the impregnation vessel as order system. An integrating process with the new level control strategy.
a buffer for chip feed variations into the dead time was selected as the model struc- Table III shows some figures regarding
digester system. ture for the models needed in the MPC the standard deviation for the chip meter
design, except for the differential pres- speed [rpm], blow flow [m3/h], kappa
Step response modeling and MPC con- sure control, where a first order model number, digester chip level [m] and pulp
troller design structure was used. consistency [%]. The standard deviation
A key element in the design of the MPC Table II shows the controller design calculations are made from periods of
controller is the dynamic process model, matrix for MPC controller where each cell equal length and similar production rates
TABLE II: MPC controller design matrix. TABLE III: Comparison between old level control system
(2003) and new level control system (2004).
was used as the primary manipulated variable for the level con-
trol, instead of the blow flow, which was used in the original lev-
el control system. A comparison of production data for January
to February 2004 and the same period in 2003 indicates that the
new control strategy decreases the kappa number variations. A
smoother digester operation (stated by the operators) together
with an increased focus, from the operators, on the complete
digester mass balance control was probably two contributing fac-
tors for the reduction of the kappa number variations. Even if
the chip level variations did not decrease significantly, the reduc-
tion of the blow flow manipulations and pulp consistency varia-
(40 to 46 t/h) during January and February in 2003 and 2004 tions probably stabilized the chip column movement and the
(sample time 20 minutes). conditions in the digester bottom.
The results show a clear reduction of blow flow manipula- The MPC controller implementation has improved the con-
tions and pulp consistency variations. The reasons for the reduc- trol of the impregnation vessel chip level. With the constraint
tion in kappa number variations may need a closer investigation functionality in the MPC scheme it has been possible to combine
of the overall production conditions. The digester operators disturbances reduction with safety function control in the same
confidence for the new control system is high and they state that control algorithm.
the digester operation has been smoother this winter period The future work regarding the level control system will be to
than previous ones. Modify and improve the control function for the blow flow
Figure 7 shows a trend plot of the digester level control. The and implement that function into the MPC controller
production bias (chip meter speed) is manipulated to control the Improve the pulp consistency control by utilizing dilution flow
digester level. The blow flow set point is adjusted at time 16:48 and bottom scraper motor amperage.
when the production bias is outside the +/- 1 t/h control limits. Utilize gain scheduling for improved tuning at low production
Figure 8 shows how the blow line pulp consistency is controlled rates
by manipulating the digester bottom scraper speed. The goal is to Start-up of the digester and MPC controller performance
keep the pulp consistency within +/- 0.25 %. The digester bottom monitoring project.
dilution flow may need to be involved in the pulp consistency con-
trol function to improve control performance [13]. ACKNOWLEDGEMENT
The impregnation vessel chip level is primary controlled by The authors would like to thank the digester operators and pro-
the bottom dilution flow (FC5.2 in Fig. 2) but with the bottom cess engineers at M-real Husum Mill for their assistance, and the
scraper acting on the upper and lower limit. In the beginning of Network for Process Intelligence (NPI) at Mid Sweden Univer-
the trend plot, Fig. 9, the scraper speed increases to correct a sity, rnskldsvik, Sweden for their financial support. A special
detected violation of the upper constraint limit. When the level thanks goes to Capstone Technology, Seattle USA, for the use of
is back within the limits the scraper speed slowly returns to tar- their MPC software.
get speed, which is set to 3 rpm.
LITERATURE
CONCLUSIONS AND FUTURE WORK 1. MACIEJOWSKI, J.M. Predictive Control with Constraints. Harlow, UK. Prentice Hall,
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This paper describes the implementation of a new control strat- 2. AMIRTHALINGAM, R., LEE, J. H. Inferential Control of A Continuous Pulp
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The objective of the new control strategy was to stabilize the ence (2000).
transport process in the bottom of the digester. The chip feed 3. AMIRTHALINGAM, R., LEE, J. H. Subspace Identification Based Inferential
FIG. 8. Blow line pulp consistency control. FIG. 9. Impregnation vessel level control.
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