Explosion at The Conoco Humber Refinery - Lessons Learned PDF

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Health and Safety

Executive

The Explosion and Fire at the Conoco


Humber Refinery 16 th April 2001

HSE Investigation and the Lessons Learned

Jonathan Carter
Principal Specialist Inspector
HSE
Hazardous Industries Directorate
The Refinery

Incident

HSE Investigation

Lessons to be Learned
Conoco Humber Refinery, Immingham

Designed & constructed mid 1960s


Fully on line 1970
Key product specialised coke for aluminium &
steel production
Various expansions to current 12 m tpa capacity
Full range of integrated process units inc. FCCU,
HFA, HDS etc.
Total of 750 employed + up to 525 others
Normal daytime on-site population 800
Saturate Gas Plant (SGP)

Commissioned 1981 to improve gas recovery


In house process design
Separates light liquids by fractionation into
gasoline, butane, propane
3 columns in series, with intermediate reflux
drums
W413 de-ethaniser, 28 barg
W414 stabiliser, 10 barg
W415 propane/butane splitter, 17 barg
Throughput 12,000 bpsd
Incident

14.20 hrs Easter Monday 2001


Plant running normally, no recent upsets
Sudden release from de-ethaniser column
overheads line (P4363)
12m above ground, northern end of SGP
0.7 m downstream of water injection point
Upstream of X452 heat exchanger
Dispersed into adjacent plant by 7.2 ms -1
northerly wind
SGP - Fire

Explosion led to fire in SGP and surrounding


areas
Fire fuelled by other releases arising from blast
damage
Various fireball events due to hot failures of
large diameter lines
Fire continued for over 3 hours
Manual isolation of all failed lines eventually
eliminated fuel
Total release 180 tonnes of gas/liquid
Damage On Site

SGP widespread major damage - write off


Coker closed blow down system significant
damage
Minor damage to adjacent units
Minor structural damage to many buildings
including main admin. block, stores
Site wide damage to glazing - canteens, offices
Site wide damage to cladding, lagging - led to
asbestos contamination
Central control room blastproof - no damage
Damage On Site
Damage Off Site

Property damage up to 1500m distance


370 separate damage reports received
from local businesses and homeowners
Mainly glazing and minor structural
effects
Adjacent Lindsey Oil Refinery some
building damage but none to plant
Damaged reputation and trust
Injuries

1 3 day injury - employee in locker room cut by


flying glass
Various minor cuts & bruises
No off significant off-site injuries
Only 185 persons on site due to Bank Holiday
Most operators indoors preparing for shift
changeover
Nearest occupied building 175m (150 -200mb
OP), some structural damage but no collapse
Optimum timing for injury limitation
Source of Release

Water

P4363
Injection
Point

RELEASE

X452

W413
De-ethaniser
X453
Source of Release

Release Point ----


Source of Release
HSE Investigation
Vapour Cloud Explosion
Modelling of release and dispersion
Pipe failure equivalent to full bore release, 45
downwards, release rate 133 kg/s, reducing to
71 kg/s after 30s.
Max. flammable cloud size (10k m3) after 15s,
began contracting after 40s, max length 175m,
max width 80m at 75m dist (CFD model).
Congested volume ~5k m3, 500kg, max o/p
0.5bar.
Ignition 12-32s after release at fired furnace
(65m)
HSE Investigation
Vapour Cloud Explosion
Alternative wind speeds & directions modelled
3 m/s (same direction) & 3/7 m/s at 90.
In all cases max distance of flammable envelope
reduced
With 3 m/s crosswind max. volume increases to
15k m3
No other permanent ignition source within any
alternative flammable gas cloud
Concluded that outcome could not have been
significantly worse no risk of significant impact
on HF Akylation unit.
HSE Investigation
Cause of Release

Catastrophic rupture of 6 diameter


overhead pipe (P4363)
Pipe failed at elbow 67cm downstream of
water injection point
Mild steel pipe, original thickness 7.1mm,
reduced to min. 0.3mm, significant area
<1mm.
HSE Investigation
Cause of Release

Degradation due to corrosion-erosion


Various potential corrosive agents
present ammonia, chloride, hydrogen
sulphide
Injected water sweeping round pipe bend
constantly removing passive film of
corrosion products no dispersion
device.
HSE Investigation
Cause of Release
Conclusions and Key Lessons

Management of pipe work inspection


No effective system in place for SGP pipe work
inspection
Refinery inspection systems focused on
equipment
Pipe work systems not in line with
industry good practice
Knowledge and experience from other
plants not applied
Conclusions and Key Lessons

Insufficient condition data obtained to


verify integrity and inform future
inspection
Introduction of RBI requires comprehensive
condition data, large backlog of data not entered
into database
Default RBI assessment would have led to P4363
inspection but failure occurred first

Key lesson; High hazard pipe work requires


inspection to industry good practice
standard informed by adequate condition
data
Conclusions and Key Lessons

Management of change
Installation of P4363 water injection not
subject to MoC review

Quick-fix solution to fouling problem

No consideration of suitability of location, need for


dispersion device or corrosion potential
Conclusions and Key Lessons

Use of injection point not monitored or


controlled
Changed between continuous and intermittent by
operation staff
Information on use not provided to other
departments

Key lesson: Effective MoC systems are


needed for plant & process changes to
prevent un-assessed quick-fix
modifications.
Conclusions and Key Lessons

Management of corrosion
Arrangements not sufficiently thorough or
systematic
Action on specific alert about injection
point corrosion problems undermined by
inadequate knowledge of status and
mode of operation
Conclusions and Key Lessons

Resource provided for reviews and


monitoring but not sustained
Key lesson; Refinery corrosion
management requires systems and
resources to ensure that relevant
information and knowledge is identified
and acted on and that relevant processes
are monitored and reviewed
Conclusions and Key Lessons

Communication
Inadequate communication of the status
and usage of P4363 water injection point,
both within the operations department
itself and also with other departments
(notably inspection), resulted in its
exclusion from subsequent assessment.
Conclusions and Key Lessons

Information from the limited inspections


carried out on P4363 in 1994 was not
adequately recorded or communicated,
resulting in the recommended further
inspections not being carried out.
Key lesson; Accurate recording and
effective sharing of information and data
relevant to plant corrosion is essential for
major accident prevention.
Learning Points for HSE

Focus on pipe work integrity


Importance shown by this and other
incident investigations
HSE HID UK Refineries Pipework
Integrity Project, 2002/03 findings
detailed in SPC/Tech/Gen/33
Project extended to to other major
hazard chemical sites for 2005/06.
HSE Actions

Safety alert to industry via web site, once


immediate cause confirmed, on need for
effective pipe work inspection systems with
particular reference to injection points
Improvement Notice to implement adequate
pipework inspection regime.
Prosecution HSW S2 & 3 (COMAH Reg4 charge
not pursued). Guilty pleas, fine 2 X 400k, with
218k costs. June 2005.
Publish incident report on web site late 2005.
Any Questions?

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