Casing-Running Challenges For Extended-Reach Wells
Casing-Running Challenges For Extended-Reach Wells
Casing-Running Challenges For Extended-Reach Wells
JULY 2004
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other wells in the field indicated cased-/openhole friction factors from 0.30/0.20 to
0.30/0.40. Data collection at that time was
fairly primitive, and a conservative approach
was adopted in the design of the Well PN1y
casing-running operation. The decision was
made that friction factors of 0.30/0.40 would
be appropriate for the first ERD casing run.
Drag analysis indicated that casing was
unlikely to reach depth unless friction-reduction measures were used.
A review of drilling and tripping torque
and drag data indicated that cased-/openhole friction-factor values of 0.25/0.12 provided a good match. The low openhole friction factor is typical of drilling the Horda
mudstone with OBM.
For drag-reduction purposes, the decision was made to spot pills of low-friction
beads along the bottom 900 m of open hole.
Additionally, 125 roller centralizers were
installed from 600 to 2145 m on 95/8-in.
casing with the shoe at total depth (TD).
This means that the rollers would be contained entirely within the 133/8-in. casing.
Also, the decision was made not to centralize the 95/8-in. casing inside the open hole
because this was considered detrimental to
drag. The centralizers reduce clearance and
increase overall string weight and stiffness.
After some expected drag along the first
1200 m of open hole, the running weight
spontaneously and dramatically recovered
at the same time that the drag-reduction
measures were meant to work. For this run,
cased-/openhole friction factors of 0.25/0.45
were calculated. Further analysis suggested
that friction factors of 0.05 could be attributed to the roller centralizers and beads.
The Well PN1x 81/2-in. sidetrack was
drilled through the Well PN1y casing
shoe and into the reservoir. Massive losses
again occurred, with ECDs recorded at
13.8 lbm/gal. The well was plugged back
and suspended.
The reservoir fracture gradient was
decreased from 14.6 to 13.5 lbm/gal. With
this constraint, it was not possible to continue the well in 81/2-in. hole size, because
ECDs of 14.2 lbm/gal could be expected at
the end of well.
Nine months later, operations recommenced with the Well PN1y casing string
being cut and pulled. Well PN1w was then
sidetracked from the pre-existing 133/8-in.
casing. The 121/4-in. overburden section
again was successfully drilled with an RSS
and revised ERD operational practices. The
previous Well PN1y casing-running success
provided an invaluable reference point. To be
conservative, 0.30/0.40 again were used as
cased-/openhole friction factors for planning
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JULY 2004