Process Control Case Histories: An Insightful and Humorous Perspective From The Control Room
Process Control Case Histories: An Insightful and Humorous Perspective From The Control Room
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pH Control: A Magical Mystery Tour 5
As with any new system, start-up was not without bugs. Some
were of the common garden variety—like transposed wires and
incorrectly calibrated positioners. Others were of the magical mys-
tery type peculiar to pH systems.
For example, at high pH levels, the measurement went down-
scale as the strong base reagent flow increased. As you can imagine,
this drove the control system—and us—kind of crazy. The diffi-
culty turned out to be that the measuring electrodes in the in-line
loop were not specified with high-pH glass. Normally this would
cause the measurement to read low by about 1 pH at the upper end
of the scale. In our case, it caused a reversed response. This perfor-
mance was confirmed by the vendor and was corrected by replacing
the electrodes with low sodium ion error devices.
9. Large tanks are fine if you don’t have to control them; use
the volume upstream to reduce reagent consumption or the
volume downstream to reduce control error.
10. Install one or three but never two electrodes for a pH mea-
surement. Use middle signal selection for three measure-
ments for inherent protection for all types of an electrode
failure and minimization of error and noise.
2/4/10 3:14 PM
pH Control: A Magical Mystery Tour 9
pump. The pump was about 300 feet away from the mixer. This
distance caused a delay when the pump was activated—because
process fluid would backfill the injection piping and had to be
pushed out of the line before any reagent could be delivered. It
doesn’t take much fancy mathematics to figure that at one gallon
per hour, it takes an hour to push a gallon through a pipe. This led
to Fact of Life #4.
We also found a delay when the speed of the pump changed
but never really identified the cause. We would have blamed it on
air pockets, if there had been any. The answer probably lies in the
ketchup bottle—related to low flow of viscous fluids.
Anyway, we reduced the delays and resulting noise band by an
order of magnitude when we replaced the remote metering pump
with a close-coupled control valve. The valve was manipulated using
a ratio controller to proportion the reagent flow to the sump dis-
charge flow, correcting the ratio with the in-line pH loop.
Some noise still remained, due to poor distribution of the
injected reagent into the pipeline. This couldn’t be eliminated,
because it required making the injection port smaller so the reagent
velocity would be larger. Unfortunately, a hole small enough to do
the job was too small to keep from plugging. The noise was more
of a nuisance on the trend chart than in the system, so the record
was cleaned up by passing the measurement signal through an elec-
tronic filter.
We thought our problems were over, when magical mystery
reared its ugly head. As the miniature reagent valve was stroked
from closed to open, the reagent flow measurement momentarily
increased and then went to zero. The magnetic flowmeter was
immediately suspect—but came through with a clean bill of health;
we checked the wiring and found it to be correct; the vendor
examined and verified the integrity of the electronics; we tested the
meter on water and observed that it responded correctly. We than
tried changing valve trim, but several tests yielded the same results.
I was about to throw the tiny but costly trims away, leave the
engineering profession, and enter a seminary. During this period
of contemplation, I suddenly noticed what looked to be a reverse
taper on the trims. It was hard to tell for sure, because the parts
were small, but I confirmed the observation with a micrometer. In
designer said, “50 feet.” I gasped, “It’s not nice to kid an old engi-
neer.” He responded, “Who’s kidding?” I then asked, “Where’s
the agitator?” He replied, “You’re the only agitator on this proj-
ect.” I instantly knew I had a major problem.
Figure 1-3a shows how the pH was originally being controlled.
Axial agitation probably would have corrected the difficulties but
could not be provided economically because the tank was too tall.
A shorter tank would also have worked—again at a higher price
than the plant wanted to pay.
I decided that the best way to cope with the tank would be
to use its volume as a filter, estimating that it would attenuate the
hydrogen ion concentration oscillations of an in-line loop by a
factor of 10,000—4 pH units. A circulation pump was installed as
a low-deadtime in-line mixer. Influent and reagent were added to
the new suction; an injector probe was installed on the pump dis-
charge. The new system is shown in Figure 1-3b.
Is bigger better?
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pH Control: A Magical Mystery Tour 15
during buffering because the bottle was plastic. The problem was
solved by isolating the preamplifier enclosure from ground with a
plastic mounting plate.
The control system has performed well from start-up except for
periodic pluggage of the electrodes in an overflow sample line.
Liquid head is too low to achieve a sample velocity sufficient to
sweep the electrodes clean. A new electrode holder that provides
a large flat electrode surface will be tried. If that doesn’t work, we
may have to shake loose enough money to install a sample pump
and an injector electrode assembly.
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18 Process Control Case Histories
reagent delivery time and fed forward to establish the waste flow
set point.
To eliminate downtime due to electrode failures, a system
was installed using three measuring elements and voting logic to
establish the output signal. Use of three rather than two electrode
assemblies makes it possible to determine which signal to use, if the
electrode outputs disagree. This leads me to Fact of Life #10.
Control improved dramatically. Electrode failure due to etch-
ing that had occurred when the solution was acidic—at the unre-
corded lower portion of the square wave—also stopped. And the
use of voting logic to control using three electrode assemblies
has virtually eliminated downtime, even when an element becomes
nonfunctional.
REFERENCE
1. McMillan, G K. and Cameron, R.A.; Advanced pH Measurement and
Control. 3rd edition. ISA (Research Triangle Park NC), 2005.