N4H7 APC Machine Report #M491029 After Reconditioning-1
N4H7 APC Machine Report #M491029 After Reconditioning-1
N4H7 APC Machine Report #M491029 After Reconditioning-1
# M491029
Remarks / Detail of parts to be
Sl no Unit Checking / measuring unit Explanation Remarks
status replaced/ adjusted
Checked & Found leveling error of 0.002 micron for the full travel of X
data axis ( When Y & z axis is kept at the
Machine levelling, OK
center of its stroke length & 0.004 in Z axis
direction when z axis moved to full stroke.
recorded in
Checked &
Table
data 1 Found 3 micron in X direction & 3 micron in Z direction for
Spindle head levelling Ok
recorded complete stroke
Checked &
data Found 40 microns displacement of spindle shaft during
Spindle knock out measurement Ok
recorded unclamp
Spindle taper blue match check Checked Found 80% of spindle taper seating by blue matching OK
Checked &
Spindle axial play check data Found zero micron play in spindle axial direction OK
recorded
Checked &
Spindle radial play check data Found 4 micron of spindle radial play Ok
recorded
Checked & Found 10 micron run out at 300 mm length of testbar,
Spindle run out check - at 300mm length of data 2 micron at near nose, 1 micron at inside taper & 1 Ok
test bar, near nose and at spindle taper recorded micron at spindle face
Checked &
data Recommended is 18.5
Needs to replace the
Tool clamping force measurement recorded Found 7.5 KN KN So needs to replace
disc springs after trials.
the Draw bar assembly
Checked &
data Found Max. 0.878 microns in X plane & Max. 2.8 microns
Spindle vibration measurement OK
recorded in Y plane
2 Spindle
Checked &
Spindle no load measurement data Found Max.load 7% at 8000 rpm OK
recorded
Checked &
Found max. difference of 3 rpm during spindle running at
Spindle speed verification with command speed data OK
recorded 8000 rpm
Checked &
data Adjusted to within 35 microns as against earlier 100
Spindle orientation measurement Ok
recorded microns
Spindle Bearing lubrication function check Checked Found 1 drop of oil for every 15 second Ok
Recommended is 0.2 Mpa
Micron Lube air pressure Checked Found 0.2 Mpa
and is ok
Micron Lube manifold pressure Checked Found 0.04Mpa Recommended is 0.1 Mpa
Checking by When tried to reduce the back lash by adjusting the worm So needs to replace the
NC Index Table Make
Auto shaft position the worm wheel movement getting tighten worm shaft assembly
B axis back lash measurement with table lift :Sudokama
collimeter and hence drawing more current. And the back lash is with the necessary parts
4 Index Table condition Model : RT# 246,A
and uneven throught the wheel ,found 18 r seconds after like bearings , O rings
Serial No. 037121
correcting adjustment with mechanical and parameter correction. and seals etc.
9 ATC arm
Removed the bend of the ATC shutter and adjusted the
Functioning of ATC shutter Checked Ok
cusioning of the Cylinder now found OK.
9 ATC arm
Check ATC alignment of arm with respect to checked and Done the resetting of the ARM position with respect to the
Found Ok
Spindle corrected Spindle.