Catastrophic Failures
Catastrophic Failures
Contents
Executive Summary 1. Introduction 2. Hasselt Bridge 2.1 Summary Details 2.2 Background 2.3 Causes of Failure 2.4 Lessons Learnt 2.5 References 3. Schenectady T2 Tanker 3.1 Summary Details 3.2 Background 3.3 Causes of Failure 3.4 Lessons Learnt 3.5 References 4. Fawley Crude Oil Storage Tank 4.1 Summary Details 4.2 Background 4.3 Causes of Failure 4.4 Lessons Learnt 4.5 References 5. World Concord Tanker 5.1 Summary Details 5.2 Background 5.3 Causes of Failure 5.4 Lessons Learnt 5.5 References 6. The Kings Bridge 6.1 Summary Details 6.2 Background 6.3 Causes of Failure 6.4 Lessons Learnt 6.5 References
7. Sizewell Boiler 7.1 Summary Details 7.2 Background 7.3 Causes of Failure 7.4 Lessons Learnt 7.5 References 8. John Thompson Pressure Vessel 8.1 Summary Details 8.2 Background 8.3 Causes of Failure 8.4 Lessons Learnt 8.5 References 9. Cockenzie Power Station Boiler Drum 9.1 Summary Details 9.2 Background 9.3 Causes of Failure 9.4 Lessons Learnt 9.5 References 10. Typpi Oy Ammonia Plant Water Coolers 10.1 Summary Details 10.2 Background 10.3 Causes of Failure 10.4 Lessons Learnt 10.5 References 11. Robert Jenkins Pressure Vessel 11.1 Summary Details 11.2 Background 11.3 Causes of Failure 11.4 Lessons Learnt 11.5 References 12. M V Kurdistan Tanker 12.1 Summary Details 12.2 Background 12.3 Causes of Failure 12.4 Lessons Learnt 12.5 References 13. Alexander L Keilland Accommodation Platform 13.1 Summary Details 13.2 Background 13.3 Causes of Failure 13.4 Lessons Learnt 13.5 References 14. Union Oil Amine Absorber Tower
14.1 Summary Details 14.2 Background 14.3 Causes of Failure 14.4 Lessons Learnt 14.5 References 15. Ashland Storage Tank 15.1 Summary Details 15.2 Background 15.3 Causes of Failure 15.4 Lessons Learnt 15.5 References 16. Summary and Conclusions 17. Acknowledgements
Executive Summary
A series of fourteen case studies are described, where failure has occurred by fracture, and the lessons which can be learnt from these failures are discussed.
Background
Fortunately, catastrophic structural failures are rare. However, when significant structures such as pressure vessels, storage tanks, bridges or ships fail, the ramifications can be extensive, in terms of human injury, together with loss of capital revenue. In order to reduce the incidence of costly failures in the future, it is important to learn from past events. These lessons are incorporated into industrial and national codes of practice, and are valuable to practising engineers responsible for the management of critical structural plant.
Objectives
To describe the events relating to significant structural failures, together with the associated failure investigations. To summarise the lessons which can be drawn from these failures.
Approach
This report describes a series of fourteen industrial failures, where the mechanism of failure was by catastrophic fast fracture (for example, see Fig. 10 in main text). Failure case studies are presented for six pressure vessels, three ships, two bridges, two storage tanks and one offshore rig, in chronological order. For each case study, the failure events are described, together with an account of the main contributing factors and failure mechanisms. (Fracture mechanics analyses of the failures are not included in this report, see TWI Members' Report 512). The lessons which can be learnt from these failures are discussed.
Discussion
A range of issues have been identified which have contributed significantly to the structural failures described in this report: Fracture toughness is of particular importance for welded fabrications, where fracture toughness is dependent on chemical composition, microstructure, joint configuration, loading rate and temperature. Low fracture toughness was a factor which contributed to most of the failures which have been discussed in this report. All of the failures which have been described in this report were associated with welds. Weldments are associated with a higher risk of fracture due to the combination of complex metallurgy, welding residual stresses, stress concentrations and higher constraint associated with the joint configurations, together with the inherent flaws which are present in all welds.
Many of the failures occurred at relatively low temperatures (-20 to 13(C). Ferritic steels undergo a transition from ductile behaviour at higher temperatures to brittle behaviour at lower temperature. Many of the failures occurred during hydrotests. The environmental/service conditions to which critical structures are exposed are important. These include any factors which could lead to embrittlement of the component materials during its anticipated lifetime. The effective management of fracture control in critical structures implies an ongoing commitment to effective maintenance, inspection and quality assurance, with regard to issues relating to management of fracture risk.
Main conclusions
The lessons which are learnt from structural failures influence the industrial and national codes of practice for design, fabrication and operation of critical plant. Structural failures have also resulted in the development of 'fitness-for-purpose' assessment methods, such as BSI PD 6493:1991 'Guidance on methods for assessing the acceptability of flaws in fusion welded structures'. These methods are based on fracture mechanics principles, and allow the significance of weld flaws to be assessed in terms of structural integrity assessment. PD 6493-type methods are used extensively, on an international basis, for many applications, including pressure vessels, pipelines, storage tanks, ships, bridges, buildings and other structural components.
Recommendations
In order to reduce the incidence of costly failures in the future, it is important to learn from past events. These lessons need to be incorporated into industrial and national codes of practice, and are valuable to practising engineers responsible for the management of critical structural plant. Top of page
1. Introduction
Fortunately, catastrophic structural failures are rare. However, when significant structures such as pressure vessels, pipelines, bridges or ships fail, the ramifications can be extensive, in terms of human injury, together with loss of capital and revenue. In order to reduce the incidence of costly failures in the future, it is important to learn from past events. These lessons are incorporated into industrial and national codes of practice, and are valuable to practising engineers responsible for the management of critical structural plant. This report describes a series of fourteen industrial failures, where the mechanism of failure was by catastrophic fast fracture. Failure case studies are presented for six pressure vessels, three ships, two bridges, two storage tanks and one offshore rig, in chronological order. For each case study, the failure events are described, together with an account of the main contributing factors and failure mechanisms. The lessons which can be learnt from these failures are discussed. For fracture mechanics analyses of some of the failures described in this report, the reader is referred to Part III of the TWI Members' Report 512/1995 by Challenger, Phaal and Garwood (see section 16 for full reference).
2. Hasselt Bridge
2.1 Summary Details
Failed structure: Date: Place: Conditions: Failure mode: Cause: Vierendeel truss welded steel bridge
14 March 1938 Hasselt, Belgium Light load but cold weather, about -20C Brittle fracture Low toughness steel subject to multiaxial restraint and residual stresses in the presence of weld defects Consequences: Complete collapse of bridge
2.2 Background
The Hasselt Bridge over the Albert Canal in Hasselt, Belgium collapsed at about 8.20am on the 14 March 1938 (see Fig. 1). Witnesses saw a crack open in a lower chord of the bridge (between the 3rd and 4th verticals) accompanied by a loud report. This failure of the lower chord transferred the load to the upper chord and six minutes later the bridge fell into the canal in three sections taking with it a tramcar and a number of pedestrians. All of the people on the bridge survived. The bridge was one of approximately 50 Vierendeel truss bridges built across the Albert Canal. The Fig. 1 Hasselt Bridge bridge consisted of straight lower chords, supporting failure the deck, and two parallel curved upper chords. The upper and lower chords were connected by vertical girders, the bridge having no diagonal members. The bridge, of span 75m, was designed to carry road and light railway traffic. It was erected between 1935 and 1936 and commissioned in January 1937. The structure was all-welded, the upper and lower chords being box girders made from welded plate I-beams. The girders of the upper chords were 1050mm wide and 1090mm deep with a maximum material thickness of 55mm. The lower chord girders were deeper (1290mm) and the maximum steel thickness was 45mm. The verticals were made from welded I-beams joined by a plate at the centre of the webs. The steel was a Belgium St-42 grade non-killed Bessemer steel with specified tensile strength between 365 and 435N/mm2.
The fractures in the lower chord, which was the first part of the structure to fail, were associated with connections to verticals (see Fig. 2). Fracture initiation is thought to have occurred in the weld joining the flanges of a vertical to those of the lower chord girder. Residual stress levels measured in similar undamaged joints were very significant. These, combined with the high stress concentrations at the weld resulting from poor joint design and welding procedures, the inherent rigidity of the bridge, the low material toughness at the ambient temperature and the presence of defects, led to failure of the lower chord and subsequent collapse of the bridge.
In January 1940, two other Vierdendeel truss bridges over the Albert Canal failed but did not collapse. In the first at Herenthals-Oolen, failure initiated in the lower flange of the lower chord at the joint to a wind brace. At the time the bridge was unloaded and the ambient temperature was -14C. The bridge was subsequently blown up during the German invasion of Belgium. The second bridge was at Kaulille and was built of rolled I-beams rather than plate girders. Cracking occurred in the lower chord and was not associated with any welds. This factor pointed to the importance of using steels with adequate notch toughness regardless of the possibility of welding defects or not.
2.5 References
Author Bondy O Shank M E Busch H, Reuleke W Reeve L Title 'Collapse of an all-welded bridge at Hasselt, Belgium'. Engineering, 145, 17 June, 1938, pp.670-671, 682. 'A critical survey of brittle failure in carbon plate steel structures other than ships'. Welding Research Council Bulletin No.17, January 1954. 'Investigation of failure in a welded bridge'. Welding Journal, 25 (8), August 1946, pp.463s-465s 'Examination of welded steel specimens from the Hasselt Bridge'. Quarterly Trans Inst Welding, Vol.3, January 1940, pp.3-13.
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3. Schenectady T2 Tanker
3.1 Summary Details
Failed structure: World War II T2 type welded steel tanker Date: Place: Conditions: Failure mode: Cause: Consequences: 16 January 1943 Portland, Oregon, USA Still water at ~4C, air temperature ~-3C Brittle fracture Poor weld quality combined with stress concentration Temporary loss of ship
3.2 Background
At 11pm on the 16 January 1943, a few days after completing sea trials, the 152m long T2 tanker 'Schenectady' broke in two amidships while lying at the outfitting dock in the constructors yard in Portland, Oregon, USA (see Fig. 3). The temperature of the harbour water was about 4C and the conditions were still. The air temperature was approximately -3C and the winds were light.
Fig. Schenectady T2 tanker 3 failure The failure was sudden and accompanied by a report that was heard a mile away. The fracture extended through the deck, the sides of the hull, the longitudinal bulkheads and the bottom girders. The vessel jack-knifed, hinging on the bottom plate which had remained intact. The central part of the ship rose clear of the water so no flooding of the hull through the fracture occurred. The Schenectady was built by the Kaiser Company as part of the huge World War II emergency ship building programme. This programme produced 2580 Liberty ships, 414 Victory ships and 530 T2 tankers over the years 1941-1946. Although fractures in the emergency programme ships had been reported, the Schenectady was the first catastrophic failure, made all the more impressive by the still conditions under which it occurred. Then, in March 1943, a sister ship to the Schenectady' the 'Esso Manhattan', broke in two at the entrance to New York harbour in sea conditions described as very moderate.
3.5 References
Author Anon Title 'The design and method of construction of welded steel merchant vessels'. Final Report of a Board of Investigation ordered by the Secretary of the Navy, Government Printing Office, Washington DC, 1947. (Reprinted in part in Welding Journal, 26, No.7, July 1947).
Williams M L 'Investigation of structural failures of welded ships'. Welding Journal, and Ellinger October 1953, pp.498s-527s. GA Brown D P Hodgson J and Boyd G M Tipper C F Pellini W S 'Observations on experience with welded ships'. Welding Journal, September 1952, pp.765-782. 'Brittle fracture in welded ships - an empirical approach from recent experience'. Quarterly Trans INA, Vol. 100, No. 3, July 1958. 'The brittle fracture story'. Cambridge University Press, 1962 'Guidelines for fracture-reliable design of steel structures'. The Welding Institute, Abington, Cambridge, UK, 1983.
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4.2 Background On 12 February 1952 a large all-welded oilstorage tank collapsed during hydrotest at the Esso Petroleum plant at Fawley in Hampshire (see Fig. 4). Hydrotesting had commenced on 30 January following completion of the tank, but was halted when a 0.6m long vertical crack appeared in the bottom two strakes. The tank was emptied and the crack repaired. When the hydrotest was recommenced on the Fig. Fawley crude oil storage tank 11 February, the air temperature was near 4 failure freezing and the water temperature +4C. The tank split when the water reached 90% of the tank height, a continuous vertical fracture running through the parent plate of every strake. The shell was torn from the tank bottom and collapsed on the surrounding band, leaving the roof lying on the base. The cylindrical tank was 42m in diameter and 16m high. The bottom was conical with a 0.6m fall at the centre and roof was a detached fully floating pontoon. The tank shell consisted of nine strakes made from butt welded plates measuring 1.8m x 7.2m. The strakes were progressively thinner from bottom to top, being aligned to produce a flush internal surface. The bottom strake was 28mm thick and the top 6mm. The construction of the tank was according to API Code 12C. The material used was a BS 13 steel with specified tensile strength in the range 430 to 510MPa, equivalent to ASTM A7 or A283 steel. Plate edge preparation for welding was carried out prior to rolling the plates to the required radius. The shell welds were full penetration double or single V welds, depending on the plate thickness. No-preheating was used except to dry the plates or remove frost. Boat
shaped samples were cut from the welds of the lower courses for inspection, leaving grooves that were repair welded. All boat samples, bar one, were satisfactory.
The failures also highlighted the importance of material toughness for storage tanks, and the introduction of the use of materials with minimum Charpy V properties greatly improved the safety of these structures.
4.5 References
Author Anon Feely F J and Northup M S Anon Title 'Failure of a large welded oil-storage tank', British Welding Journal, June 1955, pp.254-263. 'Why storage tanks fail'. Oil and Gas Journal, Vol.1, February 1954, pp.73-77. 'Learing from experience. Industry reviews fracture avoidance practices for large tanks: Part 1 and Part 2'. Metal Construction, December 1987 and January 1988. 'Locally intensified strain ageing of C and C:Mn steels and weld metals'. OMAE 95 Conference, Copenhagen, June 1995.
5.2 Background
The World Concord left the Mersey on the afternoon of the 26 November 1954 and set off southward down the Irish Channel. The vessel was in 'Winter Ballast Departure Condition', as recommended by the builders, carrying about 18000 tonnes water ballast. In the evening, warnings of severe south-westerly gales were received. The master took on more ballast and reduced the engine speed. By midnight the wind force was 8-9 on the Beaufort scale and waves were about 10m high. The engine speed was reduced further. In the early hours of 27 November, two very large waves hit the ship. The master estimated that the crest of the first wave was under the centre of the ship when the second wave broke over the fore of the ship. There was a loud rumbling noise and the vessel broke in half (see Fig. 5). Both parts remained afloat, although they did collide. No casualties were reported. Fig. World Concord 5 tanker failure The World Concord was built by Vickers Armstrong Ltd in Barrow-in-Furness. It was a single deck, all-welded, single screw steam turbine oil tanker, 199m long with a registered tonnage of 11700 tonnes. At the time of its failure, it was the largest tanker in the world. The vessel framing consisted of longitudinals approximately 0.8m apart and transverse webs positioned about 3m apart. Transverse bulkheads were located every 12m along the vessel's length. There were ten cargo tanks each with starboard, centre and port compartments. The steel plating for the hull and deck was 20 to 31mm thick. The bilge strakes, deck stringers and shear strakes were of 'special quality' steel meeting the requirements of Section 7 of the Rules for Quality and Testing Materials used by Lloyd's Register in
1950 with the extra condition of 0.23% maximum C content. The remaining plates were of 'ordinary shipbuilding quality' by early 1950s standards. The World Concord was repaired and operated under another name until 1974.
5.5 References
Author McCallum J Top of page Title 'A Case Background - The World Concord'. RINA Spring Meetings 1981.
6.2 Background
On the morning of the 10th July 1962, after 15 months in service, the steel girders of a span near one end of the Kings Bridge in Melbourne, Australia failed under the weight of a passing 48 tonne vehicle and dropped by 30cm (see Figures 6 and 7). Complete collapse of the span was prevented by the concrete deck catching on the vertical wall slabs under the bridge. The bridge was closed to traffic pending investigations and repair.
The Kings Bridge, which has three sections, was built between 1957 and 1961. The failure occurred in the 1km long high-level section which was constructed of alternate cantilever and suspended spans. The failed span had four suspended steel plate girders approximately 30m in length which were supported by cantilevers extending from the adjacent spans. Each girder was made up of two flange plates welded to a web plate.
Vertical stiffeners were welded to the web at regular intervals. To increase the thickness in the region of maximum stress, cover plates had been welded to the lower flanges of the girders over their central portions.
6.5 References
Author Title
Burren W H et al 'Report of the Committee of Investigation on the failure of Kings Bridge'. Welding Fabrication and Design, Vol.6, No.2, October 1962. Anon Madison R B and Irwin G R Top of page Report of Royal Commission into the Failure of King's Bridge, Victoria, 1963. 'Fracture analysis of Kings Bridge, Melbourne'. Journal of the Structural Division, ASCE, Vol.97, No.ST9, September 1971.
7. Sizewell Boiler
7.1 Summary Details
Date: Place: Conditions: Cause: 31 May 1963 Sizewell Nuclear Power Station Hydrotest at 13C Probably shock loading of vessel
7.2 Background
On Friday 31 May 1963, boiler No.2A at the Sizewell Nuclear Power Station failed during hydrostatic testing (see Fig. 8). The full test pressure of 31 bar had been almost reached, the test pressure being set at 1.5 times the design pressure. The water temperature at the time of failure was approximately 13C. Fig. 8 Sizewell boiler failure The failure affected two strakes near one end of the cylindrical portion of the boiler. The cracking in these strakes was fairly extensive and such that a section of the vessel wall about 5.5m long was pushed out by the escaping water and left attached by a relatively small ligament. Witnesses reported hearing a loud bang and seeing the failed end of the boiler lift off the test frame by about 5cm before falling back. The overall length of the boiler was 28.6m and the internal diameter of the central cylindrical shell was 6.85m. It was made from a Mn-Cr-Mo-V steel, 57mm thick in the shell section. The plates for the shell were supplied in the normalised condition and, after welding, they underwent a post-weld heat treatment at 600C. The specified minimum tensile strength of the steel was 525N/mm2 and the Charpy V notch requirement was for 27J absorbed energy at -10C.
The thermal sleeves were set-through pipes of approximately 100mm outside diameter. These were fillet welded to the boiler shell on the inner and outer surfaces. Investigation of the thermal sleeves and attachment welds in the regions of fracture initiation revealed no significant defects. Non-destructive testing of all other thermal sleeves in the boiler indicated that these were also free of defects. Fig. Sizewell boiler failure 9 (fracture face) The investigators into the failure were satisfied that the material and fabrication procedures met the required standards and so the stress conditions in the vessel were investigated. Strain gauge measurements were made on another of the four boilers for the No.2 reactor. These indicated that the maximum stress in the region of the failure was about 300N/mm2. Such a stress level was too low to account for the failure in the absence of significant defects. The metallographic examination of the material, both in the region of the failure and distant from it, showed the presence of twinning bands in considerable numbers. This was interpreted as evidence of shock loading of the vessel. The vessel had been supported during hydrotesting on eight piers made of steel I beams. Curved chocks were fitted to the top of each pier to support the vessel and the position of the chocks was adjusted via jacking screws. After the failure, chocks from the three piers at the fractured end of the boiler were found to be dislodged. Witnesses had seen the chocks from the two piers closest to the end of the vessel fall off when the boiler lifted and fell back during the failure. It was postulated that the third dislodged chock, which had been located at the centre of the failed section, had been insufficiently tightened and was pushed out under the weight of the water-filled vessel. The sudden collapse of support effectively caused shock loading of the boiler as the loads were redistributed. The material, although defect free and of acceptable quality, could not withstand these shock loading conditions. This was considered to be the only explanation of the failure which fitted all of the observations.
7.5 References
Author Title West of Scotland Iron and Steel Institute: 'Special report on the failure of a boiler during hydrostatic test at Sizewell Nuclear Power Station', 1964. Smith N and Hamilton I G 'Failures in heavy pressure vessels during manufacture and hydraulic testing'. West of Scotland Iron and Steel Institute Journal, Vol.76, 1968-69.
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8.2 Background
In December 1965 a large pressure vessel being manufactured by John Thompson (Wolverhampton) Limited for the ICI Immingham plant fractured during a hydraulic test (see Fig. 10). Damage to the vessel was extensive with four large pieces being thrown from the vessel. One of these, weighing approximately 2 tonnes, went Fig. John Thompson pressure through the workshop wall and landed some 46m 10 vessel failure away. One minor casualty was reported. The vessel consisted of a plain shell of 1.7m inside diameter made from cylindrical strakes of 150mm thick silicon killed Mn-Cr-Mo-V steel. The end closures were forged, one end being a flange with a flat cover. The forging material was similar to the shell steel, however, a higher carbon content of 0.2% was used in the flange forging in order to meet the strength requirements in the thickest section. The forgings were supplied in a normalised and tempered condition. The overall length of the vessel was 18.2m and it weighed 167 tonnes. It had been destined for use as an ammonia converter with a design pressure of 35N/mm2 at 120C. The proof test requirement was for 48N/mm2 gauge pressure at ambient temperature (not less than 7C) but the testing of the vessel was troubled by leaks from the bolted flange joint and several re-pressurisations were required. At the first attainment of 34N/mm2 pressure, the vessel failed accompanied by 'a kind of dull thud'. No one present noticed anything unusual before the failure. The ambient and water temperatures at the time were determined to be less than 10C. The failure occurred at the flange end of the vessel. The flange forging was cracked through in two locations, the first two shell strakes broke into several pieces and cracking extended into the third strake.
Lessons learnt
The British Welding Research Association report of the investigation into this failure proposed that fracture mechanics principles be used when setting fracture avoidance criteria for thick high strength steels. It also recommended carrying out pressure tests at temperatures above the ductile-brittle transition temperature of the vessel material in order to reduce the risk of failure.
8.5 References
Author Title
Anon
'Brittle fracture of a thick walled pressure vessel'. BWRA Bulletin, Vol.7, No.6, June 1966.
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9.2 Background
On the 6 May 1966, a boiler drum manufactured by Babcock and Wilcox Ltd failed during hydrotest at the Cockenzie Power Station in Scotland (see Fig. 11). The boiler was at approximately 270 bar gauge pressure, about 96% of the full test pressure, when the failure occurred. Fig. Cockenzie power station The ambient temperature was 7C. One end of the 22.8m long boiler drum split, with two 11 boiler drum failure longitudinal brittle fractures extending about 4.9m. The connecting pipework prevented the pieces of failed plate from being thrown any distance and no one was injured. The boiler drum was made of six cylindrical courses of 1.7m inside diameter, fabricated in 140mm thick Mn-Cr-Mo-V steel (Ducol W30). The drumheads were pressed from the same steel but slightly thicker (152mm). Production of the vessel involved manufacturing two halves consisting of three courses plus drumhead each. The two halves were furnace post-weld heat treated before being joined together. The closing circumferential weld was then locally post-weld heat treated. Each course had four set-through nozzle attachments which were welded by the manual metal arc process. These welds were tested internally and externally using magnetic particle inspection. One weld was found to contain a crack and, as the associated nozzle was also found to be deeply seamed, the whole nozzle was replaced. An angle bracket attachment close to the nozzle was cut down to a stub to improve access during welding of the replacement nozzle and subsequently reattached. The repair was carried out prior to the furnace post-weld heat treatment (PWHT). The boiler drum was inspected during its fabrication by both the manufacturer and independent insurance company surveyors, but no non-destructive testing was
performed after the final heat treatment. The manufacturers carried out an hydraulic pressure test at 11/2 times the design pressure in June 1964 prior to delivery to the power station in October 1964. The first on-site pressure tests were undertaken in March 1966 once the boiler erection was sufficiently advanced to allow it. Faulty welds in the superheater area remote from the drum were found and repaired. The boiler was fully pressurised on 1 April and passed by the surveyors except for a number of tube defects. The boiler was pressurised again on the 22 April to check that the repairs, which were not associated with the drum, were satisfactory. The failure of the drum occurred during the final pressure test on the 6 May.
9.5 References
Author Smith N and Hamilton I G Anon Title 'Failure in heavy pressure vessels during manufacture and hydraulic testing'. West of Scotland Iron and Steel Institute Journal, Vol.7, 1968-69. 'Report on the brittle fracture of a high-pressure boiler drum at Cockenzie Power Station'. Welding Research Abroad, Vol.XIII, No.8, October 1967.
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Failure mode: Brittle fracture Causes: Consequences: Loss of vessels; temporary shut-down of plant
10.2 Background
A set of four high pressure heat exchangers at the Typpi Oy ammonia plant in Oulu, Finland failed on the 19 March 1970 (see Fig. 13). The plant had been restarted after a two-week shut-down and had been running at the process pressure of 230 bar (58% of the hydrotest pressure) for about an hour when the head chambers of the water coolers fractured suddenly. Pieces of two of the head chambers (A and B) were thrown up to 250m and the third chamber (C) showed extensive cracking around the nozzles. The fourth cooler (D) appeared undamaged. Personnel working near the heat exchangers did not hear Fig. Typpi Oy ammonia or see any signs of leakage prior to the failure and the 13 plant water cooler records showed the process conditions to be normal. The inlet temperature of the effluent was +10C and its outlet failure temperature +3C. The ambient temperature was 3C below zero. The head chambers were forged slightly oversized from a creep resisting Ni-Mo-V steel and normalised at 920C. Following rough machining to close to the final dimensions (outside diameter 1090mm, length 1100mm with thickness 85-150mm), the forgings were heat treated at 950C for four hours, oil quenched, tempered at 675C and finally air cooled. Following visual and ultrasonic inspection, the final machining was carried out. A mild steel overlay was deposited on the tube-plate face using manual metal arc (MMA) welding. The last weld metal to be deposited was around the circumference of the tube-plate, where it joined the chamber barrel. Following welding of other attachments to the chamber (except the tubes), the chamber was given a post-weld heat treatment at 560-580C. The weld overlay around the circumference of the tubeplate was then skimmed and the whole area inspected with a dye penetrant prior to the
attachment of the tubes. Final inspection by ultrasonics and dye penetrant testing was carried out before leak testing and hydrostatic testing of the assembled water cooler.
10.5 References
Author Moisio T Title 'Brittle fracture in a failed ammonia plant'. Metal Construction and British Welding Journal, January 1972, pp.3-10.
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11.2 Background
A large pressure vessel manufactured for export by Robert Jenkins and Co Ltd in Rotherham failed during pressure testing at the company's works on the 6 November 1970 (see Fig. 15). At the time of failure, the water temperature was approximately 12C and the gauge pressure was 29 bar, 85% of the required value. The vessel had been under pressurisation for 7 1/2 hours and contained 171,000 litres of water which were released into the workshop causing considerable damage. The vessel was 34m long in two sections which were joined by a flanged and bolted connection. One section was ~4.5m in diameter with a wall thickness of 41mm. The second Fig. Robert Jenkins section, in which the failure occurred, was 2.7m in diameter 15 Pressure vessel with a wall thickness of 28mm. The vessel was constructed failure according to ASME Section VIII. The larger diameter section was post-weld heat treated, while the failed section was in the as-welded condition. The failure initiated in the vicinity of the fillet weld of a manhole compensating plate on the main shell. The fracture, which was brittle, extended in two directions through the strake containing the manhole into the adjacent strake on one side and the dished end on the other before arresting. The overall length of the fracture was 4.3m with a subsidiary crack of 1.5m long present on the other side of the manhole. The vessel material was a C-Mn ASTM 515 Grade 70 (1967) steel for intermediate and high temperature use produced in the UK to coarse grained practice and supplied in the as-rolled condition. The yield strength of the material was in the region of 300N/mm2 and the Charpy properties of the strake in which the fracture initiated were
poor: 8-20J longitudinal and 11-14J transverse at 10C with fracture appearances of at least 90% crystallinity.
11.5 References
Author Banks B Title 'Pressure vessel failure during hydrotest'. Welding and Metal Fabrication, January 1973.
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12.2 Background
On the morning of 15 March 1979 the motor tanker M V Kurdistan left Point Tupper in Nova Scotia bound for Sept-Isles, Quebec. The tanker was carrying a heated cargo of oil for the first time. The weather conditions were not good and the ship was rolling heavily. At about 12.30 the Kurdistan came to the edge of an ice field but, after travelling 2.5km into the ice, the ship was brought to a halt. The ship was turned around and headed back towards the open sea. At 13.50 the Kurdistan cleared the edge of the ice belt and put full ahead. Almost immediately there was a thud and a shudder during a downward pitch of the vessel. (The sea conditions were described as 'very heavy swell'). Oil started to escape from a vertical crack in the sides of No.3 wing tanks. The crack came up to about 3.6m below the main deck level.
Fig. 16
To reduce the loss, the transfer of oil from No.3 wing tanks to the No.4 tanks was undertaken `while the ship continued on its course. At 18.40 a second shudder was felt and the transfer of oil was stopped. The weather conditions had improved and the wave height was 2m. At 21.30 the ship broke in two: a shudder was felt and the bow rose, hinging about the deck at the No.3 cargo tanks before finally separating from the stern. Almost eight hours had elapsed between the initial fracture of the vessel's shell and its breaking in
two (see Fig. 16). The Kurdistan was built to construction class 'Ice Class I' and completed in 1973. The vessel was longitudinally framed except for the sides where the framing was transverse. With six cargo tanks, each divided into two wing tanks and a centre tank,
the overall length of the ship was approximately 182m. The Kurdistan was built almost entirely in Grade A steel (no Charpy requirements). The bottom shell was 19.5mm thick and the bilge strake 14.7mm. The bilge keel over a length of ship including the region failure consisted of 125 x 11mm ground flat bars butt welded end to end and overlapped on the underside by 300 x 13mm bulb plates, attached by intermittent welding. The bilge keel was connected edge- on to the bilge strake by continuous fillet welds above and below. The design of the keel called for a 25mm crack arrest hole to be drilled in each butt weld joining the ground bars.
This failure showed two important failings of the requirements for ships of the size of the Kurdistan built as First Year Ice Class vessels. Firstly that the ship could be built entirely of Class A steel with no notch impact requirements and, secondly, that no calculation of thermal stresses was required for cargoes at temperatures below 65C. Furthermore, this failure showed how critical the quality of workmanship can be even for a detail of apparently little significance such as the bilge keel.
12.5 References
Author Corlett E CB Title 'Kurdistan - The Anatomy of a Marine Disaster'. The Royal Institute of Navel Architects, Spring Meetings 1987. 'The use of yielding fracture mechanics in post failure analysis'. ASME Pressure Vessel and Pipeline Technology, 1985, p.20. Top of page
13.2 Background
On the evening of 27 March 1980, one of the five columns of the 'Alexander L Kielland' accommodation platform anchored in the North Sea, broke off (see Fig. 18). (The five columns were the principal buoyancy elements of the platform). The platform immediately heeled over to an angle of 30-35 and then continued to heel and sink Fig. Alexander L Kielland accommodation slowly. Twenty minutes after 18 platform the loss of column D, the platform capsized. Of the seven lifeboats on board, only two were launched successfully albeit with great difficulty in part due to bad weather conditions (one landed upside down in the water). Some inflatable rafts launched themselves due to the listing of the platform. A massive international air and sea rescue operation was undertaken. Of the 212 men on board the platform when it failed, 123 died. The Alexander L Kielland was a semi-submersible mobile rig of the Pentagone type, a design which had been developed in France. The rig was built between 1973 and 1976 in France for an American operator. Although it was designed as a drilling rig, it was only ever operated as an accommodation platform during its four years in service. The platform had five columns, of overall height of 35.6m, mounted on 22m diameter pontoons. The columns were positioned at the apexes of a pentagon with braces running between adjacent columns and the deck or hull. Accommodation units and a drilling tower were mounted on the deck.
ii. iii.
i. Fatigue crack growth in brace D6 initiating from pre-existing cracks in the fillet welds between a hydrophone support and the brace Final, mainly ductile, fracture of brace D6 Subsequent failure of five remaining braces joining the column to the structure by plastic collapse
Brace D6 and the hydrophone support were both made from a C-Mn structural steel (equivalent to a Lloyds' ship steel Grade EH) with a minimum specified yield strength of 355N/mm2. The brace was 2.6m in diameter with a wall thickness of 26mm. The hydrophone support was 20mm thick with a diameter of 325mm and was set-through the brace. It was attached to the brace by two fillet welds, one on the outside of the brace and the other on the inside. Examination of these fillet welds revealed poor penetration into the hydrophone tube material and an unsatisfactory weld bead shape. Significant cracking was also found which was dated to the time of fabrication by the presence of paint on the fracture surfaces. Fatigue crack growth in brace D6 originated at the hydrophone support weld and extended, in the latter stages partly by ductile tearing, around approximately 2/3 of the circumference of the brace until final failure took place by brittle fracture. The chemical compositions of the brace and hydrophone material were within specification, as were the Charpy and in-plane tensile properties. The throughthickness ductility of the hydrophone material (which was not specified) was, however, poor. This, combined with its through-thickness tensile strength being lower than the in-plane strength of the brace material and with sub-standard welding, led to partial cracking of the fillet weld during fabrication.
13.5 References
Author Norges Offentlige Utredninger Moan T Title 'Alexander L Keilland' - ulykken'. Report NOU 1981:11, 1981. 'The progressive structural failure of the Alexander L Kielland platform'. Case Histories in Offshore Engineering, ed, G. Mauer, Springer-Verlag, 1985.
Almar-Naess A, Haagensen 'Investigation of the Alexander L Kielland failure P J, Lian B, Moan T and metallurgical and fracture analysis'. Proc. 14th Annual Simonsen T Offshore Technology Conference, Vol.2, 1982, p.79 Top of page
14.2 Background
On the evening of Monday 23 July 1984, the Union Oil Co refinery near Lemont, Illinois, USA was seriously damaged by an explosion and fire. Seventeen people working at the refinery were killed and the property damage was estimated to be over $100 million (see Fig. 20). The explosion was caused by the ignition of a large cloud of flammable gas (a mixture of propane and butane) which had leaked from a ruptured amine-absorber pressure vessel.
An operator working near the absorber tower noticed gas escaping from a horizontal crack about 150mm long near the bottom of the vessel and tried to close off the main inlet valve. The crack grew to 600mm and he initiated evacuation of the area. As the company fire fighters arrived, the absorber tower cracked further and a large amount of gas was released. The gas ignited in a massive explosion which sent the upper part of the tower into the air, landing over a kilometre away. The explosion was felt over 20 kilometres away and the blaze which followed sent flames 150m into the sky.
The absorber tower first went into service in 1970. It was a cylindrical vessel 2.6m in diameter and of overall height 16.8m (see Fig. 21). The shell section consisted of six courses of 25mm thick ASTM A516 Grade 70 steel. These were joined by full penetration submerged arc welds in the as-welded condition. The vessel, built to ASME Section VIII, was designed to strip H2S from the propane/butane gas mixture passing through it. Monoethanolamine (MEA) was fed through the tower as part of this process. The operating conditions were 1.4N/mm2 internal pressure at 38C. The environment in the tower was corrosive. Soon after the amine absorber tower entered service, hydrogen blisters were found in the lower two courses of the shell and laminations were detected in the steel. The growth of hydrogen blisters continued and in 1974 the second course of the tower was replaced on site using manual metal arc Fig. Union Oil amine welding with no preheat or post-weld heat-treatment 21 absorber tower (PWHT). In 1976 a Monel liner to reduce corrosion was fitted in the bottom head and first course of the tower but it did not cover the repair section.
however, reveal much reduced CTOD fracture toughness values in the range of approximately 0.070-0.080mm at 38C. A later fracture mechanics assessment of the tower found that when residual stresses were taken into account, failure was predicted at the level of CTOD measured in non-hydrogen charged specimens. Taking all of these findings into account, it can be concluded that this failure occurred because the welding procedure used when replacing a section of the vessel caused the formation of a hard microstructure in the HAZ of the weld. This hard region was susceptible to hydrogen assisted cracking resulting in growth of large cracks in the vessel. The uncracked material in the vicinity of the existing cracks had low toughness due to hydrogen embrittlement and failed at the applied CTOD in the vessel arising from the operating pressure and residual stresses associated with the weld.
14.5 References
Author McHenry H I, Read D T and Shives T R Anon Title 'Failure analysis of an amine-absorber pressure vessel'. Materials Performance, Vol.26, No.8, August 1987, pp.1824. 'Weld failure in pressure vessel generates revealing report'. Welding Journal, 1 April 1984, pp.57-60.
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Consequences: Major environmental pollution for which Ashland Petroleum Co. assumed full financial responsibility; loss of tank
15.2 Background
On the 2 January 1988, tank No. 1338 at the Ashland Petroleum Company's Floreffe terminal in Pennsylvania was being filled to capacity with diesel fuel oil for the first time since its re-erection at this site the previous August. The temperature of the oil was 8C and the air temperature was -3C. At 5.00pm, when the oil level was almost at the operating maximum, the tank shell fractured vertically without warning. The tank shell parted from the bottom plate at the connecting welds and, under the force of the escaping oil, moved sideways about 35m. The tank roof to shell joint remained sufficiently intact for the roof to move with the shell. The escaping oil flowed over the surrounding dykes damaging an adjacent tank and passed through storm sewers into the Monongahela River and then the Ohio River. The total spillage was estimated at 15.2 million litres, causing severe harm to the environment and affecting the drinking water supply. The tank had been built originally at Whiskey Island in Ohio some time in the 1930s1940s. It was a 36m diameter cylindrical tank with a flat bottom and supported conical roof. The shell was approximately 14.4m high and consisted of six courses of welded plate, each plate being about 2.4m x 9.6m. The plate thickness in the bottom course was 21mm and 6mm in the top course. The thicknesses of courses 2 to 5 lay in between these. The tank capacity was 16000m3 or 16 million litres and until 1986 it had been used to hold distillate oils and heavier distillates. In 1986 the tank was taken down by oxyacetylene cutting adjacent to the original welds and then reassembled by welding in Floreffe, keeping the plates in the same order.
Examination of the fracture faces in the tank shell showed them to be flat and perpendicular to the plate surfaces, with the characteristic chevron markings of brittle fracture (see Fig. 22). The chevron markings pointed back to a flaw below the weld between the 1st and 2nd courses, at the point where a vertical weld on the 2nd course met the circumferential weld. The flaw was described as being 'dime-size' or about the size of a 5 pence piece and its orientation was in the vertical direction of the tank. Metallographic studies of the flaw revealed it to be due to flame cutting, rather Fig. Ashland storage tank than welding but, surprisingly, not the flame cutting 22 (fracture face) of the dismantling procedure. The flaw had been present in the steel plate prior to being welded when the tank was originally built. Charpy V notch tests and drop-weight tests (Pellini) to measure the nil-ductility transition (NDT) temperature were performed on the shell plate. The parent material was an ASTM A10 steel, either rimmed or semi-killed. The NDT temperature was found to be +10C and at +3C, the estimated temperature of the tank wall at failure, the Charpy tests showed low energy absorption. However, engineering defect assessments using fracture toughness values measured at +3C indicated that the stress due to the hydrostatic pressure alone (approximately 80N/mm2) would not have been sufficient to trigger failure. Soil foundation analyses were carried out which ruled out subsidence as a contributory factor. Attention was then turned to the influence that the weld adjacent to the flaw may have had. Welding residual stresses may be as high as yield strength level. In the case of the Ashland tank this could have meant that the flaw was subject to a stress level of approximately 240N/mm2. Furthermore, the effect of the welding heat cycle on the material at the crack tip was thought to have caused locally intensified strain-ageing embrittlement to which steels of this type and vintage are susceptible. This was confirmed when low fracture toughness values were measured on shell plate samples simulating this form of embrittlement. It was finally concluded that the failure was due to the material immediately surrounding the flaw being of particularly low toughness, with crack initiation occurring under the combined effect of hydrostatic and residual stresses. As the tank was operating below the NDT temperature of the shell plate, the crack emerging from the locally embrittled area could not be arrested.
15.5 References
Title 'Battelle determines cause of Ashland tank failure'. Oil and Gas Journal, September 1988, pp.49-54.
ii.
Many of the failures occurred at relatively low temperatures (-20 to 13C), including the Hasselt and Kings bridges, Fawley and Ashland storage tanks, Schenectady and M V Kurdistan tankers, Typpi Oy ammonia water coolers, together with the Sizewell, John Thompson, Cockenzie and Robert Jenkins pressure vessels. Ferritic steels undergo a transition from ductile behaviour at higher temperatures to brittle behaviour at lower temperature. The decrease in fracture toughness associate with this transition can be significant, over a fairly small temperature range. The absolute value of this fracture toughness transition temperature varies, depending on the steel composition, joint geometry, environment and loading rate. For these reasons, Charpy impact energy requirements in fabrication codes are typically specified at specific temperatures relative to the service temperature, to ensure that the material toughness is sufficient. iv. Proof testing Many of the failures occurred during hydrotest, including the Fawley storage tank and the Sizewell, John Thompson, Cockenzie and Robert Jenkins pressure vessels. It could be maintained that these hydrotests were successful, in that they prevented potential catastrophic failure in service. However, hydrotest failures are expensive, and appropriate lessons must be learnt to ensure procedures are modified to reduce this risk (i.e. restrictions on minimum temperature for testing, maximum pressurisation rates, improved inspection, etc., to facilitate repair prior to hydrotest). Nevertheless, as the Typpi Oy failure demonstrated, the benefit of a proof test may be removed by stress corrosion and other forms of crack extension in service. v. Environment/service conditions The environmental/service conditions to which critical structures are exposed is important. This includes any factors which could lead to embrittlement of the component during its anticipated lifetime (for example, the Union Oil amine absorber tower and Typpi Oy ammonia plant water coolers, were hydrogen embrittlement was a major contributing factor, and the Sizewell pressure vessel and World Concord ship, where dynamic loading was considered to be a factor. vi. Maintenance/inspection/quality assurance The effective management of fracture control in critical structures implies an on-going commitment for effective maintenance, with regard to issues relating to management of fracture risk (i.e. identification of critical components and joints, regular inspection, etc.). Poor maintenance was identified as a major contributing factor to the amine absorber pressure vessel failure. Particular attention should be given to these issues if a change of service conditions of life extension is planned. Table 1 indicates which of these six factors played a role in each of the failure cases described in this report.
The lessons which are learnt from structural failures influence the industrial and national codes of practice for design, fabrication and operation of critical plant. For instance, the amine absorber tower failure resulted in widespread changes to industrial codes for plant maintenance, while the Cockenzie boiler drum failure resulted in the requirement for inspection after post-weld heat treatment, and the specification of minimum temperatures for hydrotesting. The failure of the Fawley storage tank, and the Schenectady and World Concord tankers resulted in extensive research into fracture mechanics, leading to the requirements for adequate notch toughness in critical fabrications. Structural failures have also resulted in the development of 'fitness-for-purpose' assessment methods, such as BSI PD 6493:1991. These methods are based on fracture mechanics principles, and allow the significance of weld flaws to be assessed in terms of structural integrity assessment. PD 6493-type methods are used extensively, on an international basis, for many applications, including pressure vessels, pipelines, storage tanks, ships, bridges, buildings and other structural components.
16.1 References
Author Title BSI PD 6493:1991: 'Guidance on methods for assessing the acceptability of flaws in fusion welded structures', British Standards Institution, London, 1991. Challenger N V, "Appraisal of PD 6493:1991 fracture assessment procedures. Phaal R and Garwood Part III: assessment of actual failures", TWI Research Report SJ 512/1995. Table 1: Summary of factors contributing to failures Failure Case Hasselt Bridge Schenectady T2 Tanker Fawley Crude Oil Storage Tank(s) World Concord Tanker Kings Bridge Sizewell Boiler Factors Contributing to Failure i, ii, iii i, ii, iii i, ii, iii, iv i, ii, iii, v i, ii, iii, vi ii, iii, iv, v
John Thompson Pressure Vessel Cockenzie Power Station Boiler Drum Typpi Oy Ammonia Plant Water Coolers Robert Jenkins Pressure Vessel MV Kurdistan Tanker Alexander L Kielland Accommodation Platform Union Oil Amine Absorber Tower Ashland Storage Tank Top of page
i, ii, iii, iv ii, iv, vi i, ii, iii, v, vi i, ii, iii, iv, v i, ii, iii, v, vi ii, v, vi i, ii, v, vi i, ii, iii
17. Acknowledgements
The work described in this report was carried out within the TWI Core Research Programme, funded by the Industrial Members of TWI. The photograph in Fig. 22 is reproduced courtesy of Battelle Memorial Institute and Ashland Petroleum Company.
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