Maintainer: Cross-Wired Side-Stick Almost Brings Down Airbus A320
Maintainer: Cross-Wired Side-Stick Almost Brings Down Airbus A320
Transports Canada
Aviation Safety
Maintainer
Learn from the mistakes of others and avoid making them yourself . . . Issue 2/2004
TP 3658E
ISSN 0823-5538
1
institutionalized, and I believe that he is right. If you review the mishaps incurred by your organization large or smallin the last year, you will recognize that most, if not all, were predictable, and therefore preventable. Mr. DiLollo states that, the company has to commit to conducting its operations efficiently and in a manner that ensures the safety of its employees, customers, suppliers and aircraft. The SMS must be used to systematically reinforce safety as a corporate and individual core value. This will be achieved best by adopting the philosophy that all incidents can be prevented; management is responsible for the prevention of incidents; all hazards can be safeguarded; training is essential; safety is good business; working safely is a condition of employment; safety and quality are interdependent; safe conduct will be recognized and rewarded. How do I apply it on the floor? First, you have to stick with the published rules, procedures and recommendations. They are, after all, well proven and can take most hazards out of your work. Second, try to report any safety issues that you may encounter and that may not have been documented or reported and that, to your mind, may pose a threat to safety. Discuss them with your superior and colleagues; keep notes and check to see that something is done. The changes have to take place in the workplace. Safety issues have to be documented and addressed. There has to be more communication in order to reduce risks. SMS is an educational process by which all involved learn and improve their performance through the experience of others. Make better use of checklists, adopt tool and accessory management programs, improve and ensure channels of communication, discuss human factors, ensure recurrent training, and everyone will benefit. SMS enables you to recognize the potential for errors in your workplace, and helps you establish defences to ensure that those errors do not result in accidents or incidents with ensuing losses for everyone. Mr. DiLollos company has adopted what it calls a Five S safety activity guide on the floor: to sort, straighten, sweep, standardize and sustain the effort. Think about adopting something similar. Do like the military and take all the precautions against hazards. Safety is a team effort that can be planned.
Transport Canada
Transports Canada
The Aviation Safety Maintainer is published quarterly by Civil Aviation, Transport Canada, and is distributed to all Canadian licensed AMEs. The contents do not necessarily reflect official policy and, unless stated, should not be construed as regulations or directives. Letters with comments and suggestions are invited. Correspondents should provide name, address and telephone number. The editor reserves the right to edit all published articles. Name and address will be withheld from publication at the writers request. Address correspondence related to articles in this issue to: Editor: Serge Beauchamp Aviation Safety Maintainer Transport Canada (AARQ) Ottawa ON K1A 0N8 Tel.: 613 990-9495 Fax: 613 991-4280 E-mail: [email protected] Internet: www.tc.gc.ca/maint Reprints are encouraged, but credit must be given to the Maintainer. Please forward one copy of the reprinted article to the Editor.
Serge Beauchamp
Regional System Safety Offices Atlantic Box 42 Moncton NB E1C 8K6 506 851-7110 Quebec 700 Leigh Capreol Dorval QC H4Y 1G7 514 633-3249 Ontario 4900 Yonge St., Suite 300 Toronto ON M2N 6A5 416 952-0175 Prairie & Northern Box 8550 344 Edmonton St. Winnipeg MB R3C 0P6 204 983-5870 Canada Place 1100-9700 Jasper Ave. Edmonton AB T5J 4E6 780 495-3861 Pacific 3600 Lysander Lane Richmond BC V7B 1C3 604 666-9517
IN THIS ISSUE
Page
Cross-Wired Side-Stick Almost Brings Down Airbus A320 . . . . . . . . . . . . . . 1 The Safety Culture . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 2 Letter to the editor . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 3 Mechanical Happenings. . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 4 Suspected Unapproved Parts (SUPs) Down a Bell 206B Helicopter One Casualty. . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 6 Safety Chain BrokenLoss of Aircraft . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 7 Ben McCarty Wins Transport Canada Aviation Safety Award. . . . . . . . . . . . 8 Unscheduled Maintenance Costs to Airlines Can Be Horrific . . . . . . . . . . . 9 Take Five: Personal Minimums Checklists . . . . . . . . . . . . . . . . . . . . . tear-off
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Mechanical Happenings
The following aircraft incidents are a heads-up for aircraft maintenance engineers (AME). They focus on the maintenance outcome of the incident and do not include all of the facts of each incident. In most cases of component failures, it is assumed that a service difficulty report (SDR) was submitted, as it is a Canadian Aviation Regulations (CARs) requirement. AS350BAThe helicopter was in its initial climb phase after a normal take-off sequence, when suddenly all engine power was lost. The pilot immediately executed an autorotation in the only area available; it was slightly upslope and littered with rocks and dirt. Due to the low altitude for autorotation, the pilot was unable to prevent a very hard landing and serious injury to himself. As a result of an inspection of the engine by the U.S. National Transportation Safety Board (NTSB), investigators determined that the engine gas generator compressor turbine shaft had seized. The engine had been overhauled 61 hrs prior to the accident. The aft support bearing of the gas generator turbine shaft was found dislodged from the bearing support cage. Further investigation revealed that the circlip used to retain the bearing in the cage was not present and there was no evidence that it had been installed during the overhaul. The total loss of engine power was due, in this case, to the failure by the manufacturers repair station personnel to ensure that the engine had been assembled properly. Were check sheets used? Were the engine techs properly trained? How about inspection after assembly: could it be improved? Can anyone afford such accidents? A safety management system (SMS) would have helped identify any weaknesses in the system and
most likely would have prevented such a mishap. AS350BAThe helicopter had departed a helipad located on an offshore oil platform. The pilot was 3 min away from landing at a refuelling helipad situated offshore on another platform when he transmitted two distress calls indicating that he was going down. There were no witnesses to the accident and 9 min later the helicopter was found floating inverted in 3- to 4-ft swells. Shortly thereafter, it sank but was later recovered. Investigation found that there were no anomalies with the airframe and flight controls, but examination of the engine revealed that the first- and second-stage turbine blades were fractured due to extreme heating. One blade of the second-stage turbine disk had liberated from its retention slot, and all the blade roots and retention slots of this disk exhibited permanent outboard deformation due to a combination of centripetal forces from the engine rotation and from excessive heat. In contrast, the blade roots and the retention slots of the first-stage turbine disk did not exhibit evidence of deformation, most likely since they were located further away from the heat source. The rear bearing assembly located aft of the second stage disk was contaminated with coke. The coking suggests that oil was leaking from the engine and migrating from the rear bearing assembly. The aft side of the second-stage turbine disk displayed dark stain marks in the form of streaks. A passage exists that would allow oil to flow from the rear bearing to the aft face of the second-stage turbine disk. Oil that strikes the disk would flow into the hot stream of gases and auto-ignite, starting a fire. Oil migration in this engine can occur if the rear bearing scavenge and vent tubes
become blocked; however, in this case, these were checked and found free of contamination. AS350BAThe helicopter was on a ferry flight from the Elbow River Ranger Station, Alberta, to the Highwood Ranger Station with the pilot and engineer on board. The pilot noticed the engine chip light illuminate, and was preparing for a precautionary landing when he heard a loud bang, and the engine (Turbomeca Ariel 1B1) failed. In the ensuing hard landing from about 40 ft above ground level (AGL), the tail boom and the right-hand (RH) landing skid were damaged, but there were no injuries to the pilot or engineer. Maintenance reported that the engine had seized up. The Transportation Safety Board of Canada (TSB) will observe the engine teardown. Airbus 320 (SDR 20031223002) During the take-off run, numerous circuit breakers tripped on 121 V and 122 V circuit breaker panels and a burning odor could be smelled. The F/Os primary flight display (PFD), elevator and aileron computer (ELAC), reverser No. 2 and fuel pumps became inoperative. The aircraft was able to return for landing without further incident. Maintenance personnel investigated the deficiencies and found a loose Allen key that had fallen across the terminals of several circuit breakers and had welded itself to them. A total of 25 components had to be replaced. The entire electrical system had to be checked and verified for conformity. All systems were checked serviceable and the aircraft was returned to service. The adoption of a tool management training program will help lower the risks caused by foreign object damage (FOD). Beech King Air C90AThe aircraft was in cruise flight at flight level (FL) 220 en route
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from Winnipeg, Manitoba, to Prince Albert, Saskatchewan, when the crew heard a loud bang followed by a sudden severe tail vibration. The crew disconnected the autopilot and applied forward nose-down pressure on the control column in an effort to reduce the vibration. The crew declared an emergency and requested a diversion to Dauphin, Manitoba, 25 NM NE of their position. The aircraft landed safely. Maintenance personnel were dispatched and initial indications are that the left elevator trim tab actuator rod had failed in flight when it was subjected to excessive bending loads caused by a trim tab horn inner bushing seizure. It is recommended that the bolt securing the assembly be removed in order to allow for a complete inspection of the rod and rod end clevis, along with the trim tab horn and the inner bushing, at each inspection interval prescribed by the aircraft maintenance program. Bell 204BThe helicopter had departed on a smoke patrol in support of forest fire-fighting operations. The helicopter was established in cruise flight at 3 000 ft when, approximately 15 to 20 min into the flight, a banging noise was heard coming from the tail area, followed by a slow and smooth 30 yaw to the left. The pilot gently applied opposite pedal and was able to correct the yaw. The banging was not repetitive, but was heard as pedal was applied. The pilot landed the helicopter straight ahead in a swampy area. The helicopter landed without incurring further damage or injury to the occupants. An examination of the helicopter revealed that one of the tail rotor pitch link bolts (AN 174-15 or subsequent) was missing and that the pitch link was hanging free from the tail rotor horn, but still attached on the opposite end to the crosshead assembly. One, or both, of the tail rotors had
struck the tail boom several times in flight causing the banging noise heard by the pilot, and damage to the tail boom. The tail boom and tail rotor assembly are to be replaced in situ, but it could have been much worse. Bell 206BThe helicopter was approximately 1 000 ft AGL, on a reconnaissance flight over a forest fire in Alberta, when the engine (Allison 250-C20) decelerated to minimum idle speed. A forced landing was conducted onto a muskeg area adjacent to the fire and on touchdown the main rotor struck and severed the tail boom. The pilot and passenger were uninjured. The field investigation discovered that the compressor pressure (Pc) line from the engine governor to the fuel control unit had separated. Bellanca 17-30A Super VikingThe aircraft had just departed Runway 31 at Regina Airport, Saskatchewan, when the pilot noticed smoke in the cockpit, accompanied by a strong electrical burning odor and a complete loss of engine power. The pilot declared an emergency and turned off the aircrafts master switch to shut off all electrics. The pilot lowered the landing gear manually but was not able to make it back to the runway. The pilot set the aircraft down beside the runway, striking a drainage ditch during the landing roll. The main landing gear collapsed, but the pilot was able to exit the aircraft uninjured. A post-occurrence examination of the aircraft discovered that the exhaust stub on the back of the left muffler assembly had fractured and broken off, causing the tail pipe to detach. Hot exhaust gases were directed onto the wiring harness in the engine compartment that contained the engine magneto P leads. The wiring harness burnt and the P leads shorted out, effectively shutting off the engine. The inspection of the exhaust system is best performed with the unit assem-
bly removed from the engine. Its integrity, along with that of gaskets, the hold down nuts, studs and exhaust shrouds can then be confirmed. The time spent inspecting the unit is far less costly than a forced landing or severe injuries following such a failure. Boeing 727 (SDR 20040102001) The crew retracted the landing gear after takeoff and noticed that the nose landing gear light showed the gear extended. The pilot advised the tower that he was returning for landing and extended the gears with confirmation of no fault indication. He landed without incident. An inspection revealed that the nose landing gear lock-pin was still installed and had prevented the nose gear from retracting. The pin was removed and the aircraft was returned to service. The company has initiated changes to its preflight checklist procedures. Had the lock-pin been equipped with a red warning flag, it most likely would have been seen on the preflight check. Boeing 737 (SDR 20040115003) On arrival at the gate, the ground power unit was plugged in. When the auxiliary power unit (APU) bleed air and pneumatics were selected, the cockpit and cabin quickly filled with smoke. The captain then selected APU electrical and the first officer (F/O) contacted ground control to request emergency response services (ERS). The smoke then cleared. Maintenance was called and investigation seemed to indicate that the APU inlet had been contaminated earlier with de-icing fluid. The crew snagged the deficiency as per the minimum equipment list (MEL) and a ground run of the APU showed that the unit was serviceable. Flight monitoring of the APU and maintenance performance runs cleared the deficiency and the aircraft was returned to service with no further incidents to report.
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of the fastener itself. The hydrogen probably originated from the cadmium plating operation, and was retained or not removed during subsequent baking treatments. When hydrogen is dissolved in steel, it promotes the creation of hairline cracks and a loss of ductility of the material. The TSB determined that the failed screw did not meet the strength specifications of the part drawing. The ultimate tensile strength of the screw was significantly greater than the maximum specified. Four additional screws of the same type were recovered from the fuel control unit and did not conform to the strength specifications. The failed screws and the other screws used for fastening the cover of the fuel control unit were all unapproved parts. The fuel control manufacturer was able to establish that these fasteners had been installed at their overhaul facility on the west coast and came from a large bulk purchase from a parts supplier. Examination of more sample screws from this shipment indicated that the entire lot did not conform with the screw drawing requirements for heat treatment, marking of an X on the head and pitch diameter shank dimensions under the screw head. When a bench test of the fuel control unit was conducted with one of the screw heads missing, it began to leak when the fuel flow reached about 177 pounds per hour (pph). When the leaking started, the fuel flow decreased to 111 pph and at that fuel flow, the manufacturer of the engine determined that the engine was only producing about 101 horsepower. After the crash, a number of low-energy signaturesindicative of low main-rotor RPM (revolution per minute)were observed on the wreckage and in the impact area. The fuel leakage was sufficient to decrease the output of the engine below that required for sustained flight. It is believed that the failure of the fuel control unit ratio-lever cover during the flight would have resulted in a sudden spray of fuel into the engine compartment, producing a strong jet fuel smell in the cockpit through the cabin heater ducts. It is probable that the pilot carried out an immediate autorotation landing, but because the cluttered area available to him did not allow for a glide to a clear area, he may have tried to stretch the glide and impacted the top of a fence with the lower vertical fin of the tail rotor near the landing area. He was not wearing a helmet at the time and may have been temporarily immobilized by the initial impact. He was unable to exit the damaged helicopter in time, and lost his life. The Transport Canada SUP program needs your help in its quest to ensure the continued airworthiness of aircraft. Be alert! Inspect all parts for conformity to the type design before installing them on an aircraft or aeronautical component. Report SUP using the Service Difficulty Reporting (SDR) Program form.
implemented so that tragedies like this not be repeated. Civil aviation authorities do the utmost to assist operators in structuring their flight operations and maintenance organization in a way that accidents risks are minimized, if not almost ruled out completely. Once this system is in place, the daily responsibility of maintaining the high level of consciousness of the professional values necessary to maintain this level of safety rests with each individual team member. Investigators found that the accident airplane entered a maintenance check with an elevator control system rigged to achieve full elevator travel in the downward direction. However, the airplanes elevator control system was incorrectly rigged during maintenance, and the incorrect rigging restricted the airplanes downward elevator travel to about one-half of the travel specified by the airplane manufacturer. Air Midwest had contracted the services of "a FAA Approved Repair Station (AMO)." This organization was to supply the quality assurance, inspectors, parts personnel, site manager and mechanics in order to meet the carriers maintenance requirements. The NTSB investigation revealed that the mechanic was not properly trained and had no previous experience on the BE1900D airplane. On the night that the elevator control rigging was performed on the BE1900D, the inspector was training the mechanic for the first time. He also had to carry out multiple tasks on other aircraft. The inspector had worked a total of 44 hr in the three days prior to the release of the aircraft. He reported that he had suffered from a cold and had taken cold medicine in the days prior to the shift when the work was performed. Do you think that fatigue could have influenced the way that the inspector performed his work? How often are you put in a similar situation? On January 6, two days prior to the crash, the mechanic who carried out the work was confronted
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with his first BE1900D Detail 6 inspection. He said that when he was assigned the task, his on-the-job log was not signed off for the task, as he had never received any on-the-job training for it. He confirmed that he had previous rigging experience on other aircraft and had expected that rigging of the BE1900D would present no major hurdle. He felt that he was properly trained to accomplish this task. History would prove him wrong. When he was asked whether he felt that he was properly overseen during the task and he replied, When I needed help, there was somebody around. The foreman reported assigning the mechanic the responsibility of the rigging based on the mechanics past experience of this task on other types of aircraft. The foremans responsibilities did not include training mechanics. He worked 15 hr during the shift in which the accident aircraft was in the hangar. The least this foreman could have done was review the rigging procedures, as spelled out in the current BE1900D manual, with the mechanic. Maintenance procedures and human factors have to be taken into consideration in order to reduce risk. In hindsight, can we not say that most maintenance errors that weve experienced were predictable, and therefore preventable? Would it have helped the mechanic to use a checklist? The NTSB faulted the U.S. Federal Aviation Administration (FAA) for lack of oversight of the work being performed at Air Midwests maintenance facility in Huntington, Virginia. Serious deficiencies of Air Midwests maintenance training program had been found and it lead to the accident aircraft maintenance check. The mechanic lacked the knowledge and he failed to communicate his need for assistance. How easy it is to be put in such a position and react in a similar manner today, when there is constant pressure to perform, and communication may be interpreted as a sign of weakness? The AMO that was contracted to do the work had a high personnel-turnover rate, which may have played a role in the hiring of a mechanic who was not duly certified to perform the Detail 6 inspection on the BE1900D.
The air carrier is ultimately responsible for the maintenance of its aircraft and, although it did transfer the performance of the maintenance to a third party, it still had to ensure sufficient oversight to ensure compliance with the norms. We can address several administrative issues such as quality assurance, inspection, training, employee selection, maintenance processes, company policies, enforcement of the norms, but the end results will always be the same when an AMO fails to adopt sound administrative principles based on safety first. A safety management system (SMS) has to serve as the basis for all administrative structures in the air transport industry. What could have prevented such a tragedy? Accidents are more complex than you might think. How often do you think of the many human factors that come into play before you set out to perform a task? Is everyone around you as keen on ensuring that the work is carried out in the best possible manner, every time? What would you think of the idea of consulting a list of factors that could influence the outcome of a task? If this list would spell out things that you should know or organize before you set out on the floor or before you proceed to your workbench, would you consult it every time? The maintenance of aircraft and of their complex systems is a critical business and you have to use all available resources to assist in achieving the quality-level necessary for safety. With this objective in mind, System Safety has borrowed an idea from the FAA. We believe that it will help you achieve your goal. At the end of this issue of the Maintainer, you will find a personal minimums checklist in the form of a tear-out. We believe that it should be part of your toolkit, as it is just as essential as any tool to ensure that a job is done to perfection. Take a look at it, as it lists things to review before and after a maintenance job; the minimums that is! A personal minimum checklist will assist you in your work. Use it for performance, efficiency and safety.
vibration and believed that they had had a bird strike. Soon after, air traffic control (ATC) reported foreign object damage (FOD) on the runway following the aircrafts departure. The runway was closed and the missing wing section was recovered. Meanwhile, the crew safely returned the aircraft for landing. Investigation revealed that the lower attachment screws had not been installed and that inspection had failed to observe the discrepancy. If there been a procedure in which work cards were used to report that each step of the job had been completed, inspected and signed off, the risk of such an occurrence happening would have been lower. The maintenance system and maintenance personnel failed. It is hoped that this company adopts a safety management system (SMS) that includes a maintenance error management program. This should assist them in identifying all of the factors that came into play during this event and prevent them from ever happening again. We are all responsible for safety; it has to be foremost in our mind when we set out to perform maintenance on these complex aircraft and systems. Costs of unscheduled maintenance are horrific. Can we afford to go on and be part of this when all that is required is a little more care? Be part of the solution, not part of the problem.
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