Study of Feasibility of Six Sigma Implementation in A Manufacturing Industry: A Case Study
Study of Feasibility of Six Sigma Implementation in A Manufacturing Industry: A Case Study
Dept. of Mechanical Engineering, National Institute of Technology, Silchar, Assam, India. E-mail: [email protected], [email protected], [email protected]
Abstract- This paper discusses the implementation of Six-sigma methodology in reducing rejection in a welding electrode manufacturing industry. The Six-sigma DMAIC (define measure analyse improve control) approach has been used to achieve this result. This paper explains the step-by-step approach of Six-sigma implementation in this manufacturing process for improving quality level. This resulted in reduction of rejection, and thus, reduced the Defect Per Million Output (DPMO) from 28356.96 to 1666.67. This had resulted in increasing the sigma level from 3.41 to 4.43, without any huge capital investment. During this study, data were collected on all possible causes and was analysed and thereby conclusions were made. Implementation of Six-sigma methodology has resulted in large financial savings for the industry. Keywords- Six-sigma; DMAIC; Regression Analysis; Process Capability; sigma level; fishbone diagram; SIPOC diagram; Pareto Chart.
I. INTRODUCTION Six-sigma is a disciplined, systematic, data-driven approach to process improvement adopted by organisations world over. Motorola introduced the concept of six-sigma in the mid-1980s as a powerful business strategy to improve quality. Six-sigma continues to be the best-known approach for process improvement. Implementation of Six-sigma methodology has a significant impact on profitability and customer satisfaction, if successfully deployed. It takes users away from intuition-based decisions to fact-based decisions. This paper discusses a case study conducted in a welding electrode manufacturing industry with the aim of reducing rejection, and thereby increasing its sigma level, using Six-Sigma methodology. The application of the Six-sigma problem solving methodology, DMAIC, reduced the rejection and thereby improved productivity. Various statistical techniques were applied to analyse the data and to identify solutions at different stages. II. DEFINE PHASE This phase includes identifying the key problem areas and defining quality characteristics. A. Problem Description The problem encountered in the manufacture of welding electrodes is the large number of rejection of the units after manufacturing. The occurrence of rejection of welding electrodes was due to nonconformance of diameter with respect to the required standard specifications. B. Identifying Key Quality Characteristics (QCH) The diameter of the welding electrode is a key QCH. The upper specification limit (USL) is 4.10 mm, and the lower specification limit (LSL) is 3.90 mm. C. Process Mapping The process mapping with Supply-Input-ProcessOutput-Customer (SIPOC) provides a picture of the steps needed to create the output of the process. Fig. 1 shows the SIPOC diagram.
III. MEASURE PHASE This phase is concerned with selecting appropriate product characteristics, studying the accuracy of measurement system, making necessary measurements, recording the data, and establishing a baseline of the process capability or sigma level for the process. A. Probability Plot The probability plot of the diameter readings of a 4x450 mm welding electrode lot, produced on a certain day is shown in Fig. 2. The plot shows that the diameter values do not follow normal distribution pattern, hence, needs to be studied upon more carefully.
International Journal of Mechanical and Industrial Engineering (IJMIE) ISSN No. 2231-6477, Vol-3, Iss-1, 2013 96
A. Current Process Capability A vital part of an overall quality improving program is process capability analysis by which the capability of a process can be measured and assessed. The process capability index CP enjoys a broad base of acceptance in the industry. The CP is obtained from CP = (USL - LSL) / 6 The standard deviation is estimated by = R/ d2 (2) (1)
Other findings from the Measure phase are: Current Sigma Level = 3.41 DPMO = 28356.96 IV. ANALYSE PHASE The objective of analyse phase in this study is to identify the root causes that creates the dimensional variation of the welding electrodes. The Taguchi methods are utilized in this phase. A. Pareto Chart Analysis Data analysis was carried out in this phase to find the reasons for rejection of welding electrodes. It arises due to defects viz., diameter variation, defective coating, eccentricity and moisture content. Pareto analysis on the various types of defects is shown in Fig. 4. It is found that diameter variation caused the major portion in rejection of the welding electrodes.
Where, d2 is constant related to sample size, while R is CL value in R chart. Here, = 3.41. The estimators of CPL, CPU and CPK are expressed by CPL = (x - LSL) / 3 CPU = (USL - x) /3 CPK = min (CPL, CPU) (3) (4) (5)
CP value greater than 1 means that the process uses up less than 100 percent of the specification band, i.e. relatively less non conforming points will be observed. Whereas, CP value less than 1, means the process uses up more than the specification band. CPK value is less than CP value, means that the process is off centred, but capable, and has to be confirmed with more no. of samples. Whereas, CPK value less than zero means that the entire process mean lies outside the specifications, hence, the process is incapable. The process capability chart for electrodes of diameter 4 mm is drawn. As per calculation, the values obtained are CP = 0.05138, CPL = 0.01035, CPU = 0.00919, and CPK = 0.00919. The process capability plot is shown in Fig. 3. It can be seen that the process uses up more than the specification band. It can also be deciphered that the process is off-centred, but capable.
Figure 4. Pareto Diagram of Defects
C. Fishbone (Ishikawa) Diagram Analysis The tool that is used for the analysis of the causes of variation of diameter of the welding electrode is the Cause-and-Effect diagram or fishbone diagram as shown in Fig. 5. D. Regression Analysis Data were collected on process parameters like silicate percentage, extrusion pressure (kg/mm2), baking temperature (C), ratio of diameter of electrode to diameter of rod (D/d), and void diameter (mm). The effects of the process parameters on the diameter variation were validated by a regression analysis. Table 1 shows the Minitab output of the regression analysis. Table 2 shows the ANOVA results.
International Journal of Mechanical and Industrial Engineering (IJMIE) ISSN No. 2231-6477, Vol-3, Iss-1, 2013 97
.Since, the p-values for void diameter and silicate percentage, from the regression analysis were found to be very less, it was concluded that these variables significantly results in the diameter variation.
TABLE I.
V. IMPROVE PHASE During this phase, solutions were identified for all root causes selected during analyse phase. The feasible solutions were implemented and results were obtained. B. Brainstorming Session In this phase detailed discussions and brainstorming sessions were carried out. Solutions were identified for all selected root causes. The possible solutions are listed as under. Constituent chemicals should be accurately weighed for dry mix. Thorough mixing and accurate percentage of silicate is to be introduced in wet mix. Wire-drawing is to be carried out by skilled worker only. Nozzle diameter is to be checked frequently for wear and tear. Replace entire nozzle if diameter is more that tolerance limit. No materials should stick inside nozzle. Oven temperature must be between 250 to 300C. Storage trays must be of proper condition. Electrodes should be saved from physical damage. Exposure of electrode to air should be for minimum time span. Packaging of electrodes should be done as soon as possible. A risk analysis was conducted for identifying possible negative side effects of the solutions. No risk as such, has been associated with any of the identified solutions.
: Minitab Output of Regression Analysis The regression equation is Diameter (mm) = 4.74 - 0.0383 silicate % 0.641 D/d + 0.150 Void Diameter (mm) 0.000068 Baking Temperature SE of tpCoeffici Predictor coefficie statis val ent nts tic ue 0 4.742 0.582 8. .01 Constant 5 1 15 5 0 0.018 .18 silicate % 0.03832 93 2.02 0 0 0.552 .36 D/d 0.6415 1 1.16 5 0 Void 0.149 0.039 3. .06 Diameter 98 89 76 4 (mm) 0 Baking 0.000 .82 Temperat 0.00006 2760 0.25 77 9 ure S = 0.00623757 R-Sq = 99.8% R-Sq(adj) = 99.4% TABLE- II : Analysis of Variance D Source SS MS F F
0.009880 5 0.000038 9
253.9 5 C. Process Capability After Implementation This phase aims at adjusting the process mean on target. Process mean can be adjusted on target by improving the factors that have significant effects on the mean. The process capability chart of the 4x450 mm welding electrode drawn after the
2 6
International Journal of Mechanical and Industrial Engineering (IJMIE) ISSN No. 2231-6477, Vol-3, Iss-1, 2013 98
implementation of the solutions is shown in Fig. 6. The DPMO of the process was found to be 1666.67 and the corresponding sigma level was calculated to be 4.43.
VI. CONTROL PHASE The real challenge of Six Sigma implementation is not in making improvements in the process but in sustaining the achieved results. In this phase, the process control charts and Pareto charts are regularly utilized for monitoring diameter readings. In addition, quantity and quality of silicate has to be maintained to produce proper quality coating material, which is a dominating factor causing unwanted diameter variation. Also, regarding the problem of nozzle wear, it is to be monitored that its diameter remains within specification limits, otherwise to be replaced by a new nozzle. A. Visible Results The implementation of the various tools and brainstorming sessions has resulted in the improvement of the manufacturing process, and also on the industry as a whole. The comparison of sigma level before and after undertaking the study is depicted in Fig. 9.
D. Dot Plot A dot plot which was drawn for comparing the process before and after the study is shown in Fig.7. The dot plot shows a significant reduction in dimensional variation after implementation of the study.
VII. CONCLUSION
Figure 7. Dot Plot for Electrode Diameter
E. Pareto Chart After Improvement After implementation of the solutions, the reasons for rejection were analysed with the Pareto chart. The Pareto chart after improvement is shown in Fig. 8.
The paper is concerned with the detailed analysis of the problem of rejection of welding electrodes due to the variations in diameter of the manufactured units. Analysis was carried out with the help of statistical tools like normality testing, process capability analysis using process capability tools and studying the process capability ratios and fish-bone diagram. The normality test carried out on the diameter values showed that the data was not normally distributed. The capability of the process was determined using process capability charts and ratios and it also throws light on some of the important facts concerning the performance of the manufacturing process at present and in future. The probable causes of the problem were deciphered by drawing and analysing the cause-and-effect diagram. Regression analysis helped in finding the severity of each causes. Pareto charts helped in analysing the reasons associated with the main defect, i.e.
International Journal of Mechanical and Industrial Engineering (IJMIE) ISSN No. 2231-6477, Vol-3, Iss-1, 2013 99
variation of diameter of welding electrode. Some of the dominating factors causing rejection of the welding electrodes were the non-conforming diameter, resulting from improper nozzle condition and bad quality of coating material prepared. To conclude we can say, the six-sigma methodology including Taguchi methods has proved to be an effective approach for improving the quality of the welding electrodes that are manufactured in the concerned industry. REFERENCE
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