Hydro-Turbine Main Shaft Axial Seals of
Hydro-Turbine Main Shaft Axial Seals of
Hydro-Turbine Main Shaft Axial Seals of
Water flow, Q is in s m /
3
, where
p
C - Specific heat of water =4180Nm/kg-C, - density of water=
1000kg/m^3, AT temperature rise allowance (5degC), V rubbing speed of sealing face (m/s), and
- coefficient of friction (0.1 to 0.15).
The throttle valve in the water injection system is an important component and its characteristics should
be carefully chosen as it can provide a degree of self-adjustment to the injection water pressure. The
pressure drop through the throttle valve is proportional to the flow rate so assuming the injection water
pump maintains a constant supply pressure, the pressure after the throttle valve is then related to the
flowrate. If for some reason the leakage across the seal should increase then the pressure drop through
the throttle valve will correspondingly also increase. The pressure of injection water at the seal is
therefore decreased and the force balance on the seal is altered so the closing forces predominate. Lower
water pressure and a closed seal both act to reduce the water leakage until conditions at the seal become
re-balanced. Similarly, the reverse occurs should the leakage reduce.
Injection water pressure must be carefully selected to maintain sufficient leakage through the seal for
cooling purposes through the whole turbine operating range.
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6.0 Case study of performance of a carbon axial shaft seal retrofitted with Thordon SXL
Towards the end of 2003 Thordon Bearings Inc (TBI) were contacted by the operators of one of the
largest hydro-electrical power plants in the world in connection with retrofitting the seal on one of their
operating Francis-type vertical turbines. The existing seal was an axial face type using a segmented
carbon ring with average diameter 4000mm. The seal leakage was high and the segments were suffering
from severe abrasive wear from sand in the water. The segmented carbon seal is very brittle and there
was concern about the extreme care required when performing maintenance work.
Figure-6a shows the arrangement of the original seal. Two carbon rings, each comprised of many small
segments, were installed into two separate grooves of the steel carrier ring.
Figure-6b shows the modified arrangement suggested by TBI. The two carbon rings and their steel
carrier were replaced by a single ring of profiled SXL material. The SXL ring comprised of only six
segments.
A major consideration of the proposed change was that the original steel ring was about 400kg in weight
while the SXL sealing ring was less than 100kg, a difference of over 300kg to the balancing conditions of
the seal. Thordons engineers carefully examined the force balance conditions. The study indicated
that changes to the original springs would be unnecessary as calculations indicated the existing spring
force would be sufficient to keep the sealing face closed.
The seal was installed by the end of 2005 and the plant engineers had created a detail plan to test the
seals performance during re-start of the turbine and in service. Accordingly, the seal was tested under
different conditions. As the turbine was re-started, the leakage rate and temperature increase of leakage
water were carefully recorded for still stand condition, runner operating at 15 rpm and at full speed (90
rpm), all results were satisfactory.
The cooling water pressure, water supply flow, leakage rate and temperature increase were all then
carefully monitored for the next year, during first two months the reading were taken daily and for the
months thereafter, the reading interval was extended to twice a week. Initial feedback from the plant
Figure 6a Figure 6b
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engineers were that conditions all seemed satisfactory and the leakage was less than from the previous
carbon seal. The original seal leaked about 140 L/min.
After some time, the operators again contacted TBI with concerns that the leakage rate had further
reduced. While delighted that the leakage was small they were concerned that was perhaps too low. And
would compromise the longevity of the seal as they thought perhaps it would overheat.
With review of the temperature rise within the injection water and its outlet temperature, TBI advised that
it seemed the seal was not overheating and operation of the machine should continue.
Leakage rates continued to fluctuate a little but were always considerably less than from the previous
carbon seal. Figure -7 was measured leakage data from 20. December 2005 to 02 Aug. 2006. The water
temperature was measured during the same period of time. Inlet water is the water injected into central
groove of seal and outlet water is the leakage water. The record is presented in Figure -8.
The cooling water flow was kept constantly at 240 L/min with a pressure at 3.0 bars. The leakage is about
4% to 38% of this injection water. This means there was significant counter flow into turbine and
effectively block abrasive from entering into seal.
Figure-7: Measured leakage rate
After one years operation, the turbine was taken apart for inspection by end of 2006.
After opening the seal, the sealing face to the turbine water was clean and since the machining marks
were still visible there had been negligible wear if any. The sealing face on the leakage side however had
several regions that appeared discolored dark and there were some film like material partially adhered /
detached from the seal face. It was immediately suspected (incorrectly) that these were indications of
overheat and seal problems.
Most of the discoloration and the adhering films however were removed with simple cleaning and the
sealing surface then appeared very smooth.
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Figure -8: Measured inlet and outlet water temperature
Figure -9, shows the seal after cleaning. The sealing face on left is the leakage side towards the shaft,
the sealing face to the right is to the turbine water.
Figure 9: Sealing faces after cleaning
The brown coloured film substance taken from the sealing surface was sent to Thordon for composition
study. Thordon tested the content of substance and it was determined 60% of it was organic from the
process water and 40% was SXL material removed from sealing surface.
Precise dimensional measurements of the seal were recorded and only one small section had worn by
0.1mm, wear in other areas was effectively undetectable. Accordingly, it was predicted that the seal
should work for the 20 years requirement.
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In light of the successful installation, the operators similarly changed the seal for one of the sister turbines
in earlier 2007 and now these two turbines are all running satisfactorily.
7.0 Conclusions
A turbine axial shaft seal using elastic polymer offers great advantages to the turbine operator. It provides
1. robust construction
2. fewer segments required for larger sizes
3. simple material manufacture with standard conventional machining techniques
4. reliable operation and long life
5. economical
For reliable and long operation, optimum design must consider all components of the overall arrangement,
force balance, and careful component selection.
Thordon Bearings Inc is pleased to review enquiries from turbine operators, turbine manufacturers,
turbine repairers and seal suppliers for incorporation of Thordon materials to enhance the operating
characteristics of the machinery.
(Feb 09, 2009)
References:
/1/ Crane Packing Company, Packing and Mechanical seals, Norton Grove, Illinois, 1973
/2/ Arne Kjolle, Hydropower in Norway, Mechanical Equipment, Trondheim, Dec. 2001
/3/ N. N. Kovalev, Hydro-Turbines, Design and Construction, Israel Program for Scientific
Translations Jerusalem 1965
/4/ Mark Syer, Sealing the deal for Kaplan turbines, International water and dam construction, March
2006, Progressive Media Markets Ltd
/5/ A. A. Zakharov, Adjustment of a bronze-graphite Turbine shaft seal after repair, Hydro-technical
Construction, Vol. 29, No 4. 1995
/6/ B. B. Aitkeev, Operation of shaft seals in hydroelectric sets of the UCH-KURGAN HPP, Power
Technology and Engineering, Vol. 36, No 2. 2002
/7/ V. Ya. Monchares and A. I. Sitnyanskii, Increase of operational reliability of turbine components
at the VILYUI-2 hydroelectric station, Gidrotekhnicheskoe Stroitelstvo, No. 9, pp, 5-8,
September, 1985
/8/ I. S. Gurbanov, Experience in the operation of hydraulic structure and equipment of hydroelectric
stations, Gidrotekhnicheskoe Stroitelstvo, No. 1, pp, 28-29, January, 1984
/9/ Cheng-Jun Li, Sealing the Shaft , International Water Power and Dam Construction, June 1996,
pp, 26 - 27
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Authors:
Guojun (Gary) Ren is a senior Applications Engineer. Gary worked as an engineer with ThyssenKrupp
Elevator before joining Thordon bearings Inc. in 2001. Gary acquired his Ph.D. of mechanical
engineering from University of Stuttgart in Germany in 1996.
Ken Ogle is the Engineering Director for Thordon Bearings Inc. Previously Ken climbed the ranks as a
sea-going Engineering Officer with the P&O Steam Navigation Company before working as Senior
surveyor in the Technical Investigation Dept of Lloyds Register of Shipping.